ML20043G587

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Annual Operating Rept for Idaho State Univ for CY89. W/
ML20043G587
Person / Time
Site: Idaho State University
Issue date: 12/31/1989
From: Leviskas D
IDAHO STATE UNIV., POCATELLO, ID
To: Weiss S
NRC
References
NUDOCS 9006200461
Download: ML20043G587 (3)


Text

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  • so Idaho State University Pocatello, Idaho 83209-0009 College of Engineering t

Box 8060 (2081 236 2902 June 5, 1990

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11er-Division of Liter. sing Standardiention arnd-special=Ffo1Ects=Brw U.S.

Nuclear Regulatory Commission

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_m Washington

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20555 Dear Mr. "'

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'I Attached is the Annual Operating Report for the Idaho State l

University AGN-201 Nuclear Reactor, License R-llo, Docket No. 50-284, for the calendar year 1989.

Respectfully submitted,

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1 David Levinskas Reactor Supervisor DL/ tar cc:

V. Charyulu, Dean, College of, Engineering U.S.

Nuclear Regulatory Commission c/o Document Management Branch Washington, D.C.

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' 9006200461 091231 DR ADOCK 050 4

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ISUis An EqualOpportunity Employer r

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.n ANNUAL OPERATING REPORT FOR 1989 1.

Brief Narrative of Changes a.

There were no'_ changes to the facility design, perfor-mance characteristics or operating procedures relating to reactor safety during this reporting period.

b.

Results of major. surveillance tests and inspections.

1)

Channel tests on all safety channels were per-formed and all scram interlocks-were tested and i

found to be satisfactory and within specification.

2)

Power and period calibrations were performed with satisfactory results, i

3)

The shield tank was inspected and no leaks or ex-cessive corrosion were noted.

4) a)

The control rod drive mechanisms were inspec-

,o ted and tested with. satisfactory results.

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b)

Scram times were measured and found to be less-than 130 milliseconds, c)

Control and safety rod worths and run up times were measured; from these values the reactivity-insertion rate was determined to i

be less than 0.045%'per second for any rod.

d)

The shutdown-margin was determined to be-greater than 2.1% with the most reactive rod fully inserted.

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2.-

The total operating time for the. reactor during 1989 was l

nearly 102 hours0.00118 days <br />0.0283 hours <br />1.686508e-4 weeks <br />3.8811e-5 months <br /> with a total thermal energy output cf ap-1.

proximately 110 watt-hours.

The monthly breakdown of opera-1

' tion time follows:

i-Month Hours Month Hours l

January 13.7 July 0.8 February 14.9 August 5.0 March 11.9 September 11.8 1

April 11.4 October 12.9 L-May:

5.3 November 11.8 L'

June 0.5 December 1.6 3..

Unscheduled shutdowns Planned startups were delayed on three occasions (3/1, 4/12

& 6/27) due to weak and/or burned out tubes in channel 2.

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Safety.related maintenance-included the fol, lowing

- a.

Replacement of various tubes in channel 2 5.

Changes to the Facility a.-

There have been no changes to the facility as described in the application for license, b.

A novable' graphite plug was installed in an access port

j replacing an existing stationary graphite plug. -Three

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.small fuel disks were added to the top polyethylene I

disk in the core.

The total amount of fuel material 1

added was 59.62-gm.

The fuel addition changed the j

amount of U-235 in the core from 670.24 gm to 672.93 j

gm.

j The reactivity change associated with the graphite plug i

installation was measured and found to be -0.09% A k/k.

l The reactivity change associated with the fuel addition g

was measured and found to be +0.10% ak/k.

The net change in the excess reactivity of the reactor was

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+0.01% Ak/k.

c.

No new or untried experiments or tests were performed j

during the reporting period.

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6.

-Summary of' Safety Evaluations.

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The addition of 3 small fuel disks to the core was calcu-lated to produce a reactivity change of not greater than j

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+0.12% Ak/k.

Thas, the expected-excess. reactivity of the j

reactor after the fuel addition was estimated to be less than 0.45% Ak/k, which would not exceed.the technical y

specification of +0.65% Ak/k.

l The installation of the movable graphite plug was expected i

to' result in a' reactivity change of -0.13% Ak/k.

The Reac-1 tor Safety Cemmittee found that no unresolved safety issues i

existed for either change and-authorized procedures to.in-stall the graphite plug rirst and'then perform the fuel i

addition.

l 7.

- No radioactive effluents were released.or discharged to the environment during 1989.

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8.

No person using the facility received'a whole body exposure f

of. greater than.50 millirem during 1989; f

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Neutron and beta / gamma radiation surveys performed on the i ',

exterior walls of the faci?'<y indicated that maximum com-bined contact radiation le, s were less than 2 mrem /hr.

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