ML20043G587

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Annual Operating Rept for Idaho State Univ for CY89. W/ 900605 Ltr
ML20043G587
Person / Time
Site: Idaho State University
Issue date: 12/31/1989
From: Leviskas D
IDAHO STATE UNIV., POCATELLO, ID
To: Weiss S
NRC
References
NUDOCS 9006200461
Download: ML20043G587 (3)


Text

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Idaho State University ,

Pocatello, Idaho 83209-0009 College of Engineering t Box 8060 (2081 236 2902 June 5, 1990

-Ghar Snhou-L. g. uyss lJCk hY 11er-Division of Liter. sing Standardiention arnd-special=Ffo1Ects=Brw U.S.

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Nuclear Regulatory Commission

_m Washington -D.C. 20555 Dear Mr. "' _a 'I l

Attached is the Annual Operating Report for the Idaho State l University AGN-201 Nuclear Reactor, License R-llo, Docket No. 50-284, for the calendar year 1989. '

Respectfully submitted,

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1 David Levinskas Reactor Supervisor DL/ tar l

cc: V. Charyulu, Dean, College of, Engineering l U.S. Nuclear Regulatory Commission c/o Document Management Branch Washington, D.C. 20555 4

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' 9006200461 091231 4 DR ADOCK 050 I'

ISUis An EqualOpportunity Employer r o 1

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.n ANNUAL OPERATING REPORT '

FOR 1989

1. Brief Narrative of Changes <
a. There were no'_ changes to the facility design, perfor-mance characteristics or operating procedures relating to reactor safety during this reporting period. .
b. Results of major. surveillance tests and inspections. .
1) Channel tests on all safety channels were per-  ;

formed and all scram interlocks-were tested and i found to be satisfactory and within specification.

2) Power and period calibrations were performed with  !

satisfactory results, i

3) The shield tank was inspected and no leaks or ex-cessive corrosion were noted.
4) a) The control rod drive mechanisms were inspec-  ;

,o ted and tested with. satisfactory results.

l L b) Scram times were measured and found to be less-than 130 milliseconds, c) Control and safety rod worths and run up times were measured; from these values the reactivity-insertion rate was determined to i be less than 0.045%'per second for any rod.

d) The shutdown-margin was determined to be-greater than 2.1% with the most reactive rod fully inserted.

l L 2.- The total operating time for the. reactor during 1989 was l nearly 102 hours0.00118 days <br />0.0283 hours <br />1.686508e-4 weeks <br />3.8811e-5 months <br /> with a total thermal energy output cf ap-1.

1 proximately 110 watt-hours. The monthly breakdown of opera-

' tion time follows:

i-Month Hours Month Hours l January 13.7 July 0.8 February 14.9 August 5.0 l March 11.9 September 11.8 1

, April 11.4 October 12.9 L- '

May: 5.3 November 11.8  ;

L' June 0.5 December 1.6 i 3.. Unscheduled shutdowns Planned startups were delayed on three occasions (3/1, 4/12 1 1

& 6/27) due to weak and/or burned out tubes in channel 2.

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4. . Safety.related maintenance-included the fol, lowing

- a. Replacement of various tubes in channel 2

5. Changes to the Facility a.- There have been no changes to the facility as described in the application for license,
b. A novable' graphite plug was installed in an access port :j replacing an existing stationary graphite plug. -Three 'I

.small fuel disks were added to the top polyethylene I disk in the core. The total amount of fuel material 1 added was 59.62-gm. The fuel addition changed the j amount of U-235 in the core from 670.24 gm to 672.93 j gm. j The reactivity change associated with the graphite plug i installation was measured and found to be -0.09% A k/k. l g The reactivity change associated with the fuel addition  !

was measured and found to be +0.10% ak/k. The net change in the excess reactivity of the reactor was <

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+0.01% Ak/k. .;

c. No new or untried experiments or tests were performed j during the reporting period.

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6. -Summary of' Safety Evaluations. l i

The addition of 3 small fuel disks to the core was calcu-lated to produce a reactivity change of not greater than j L

+0.12% Ak/k. Thas, the expected-excess. reactivity of the j reactor after the fuel addition was estimated to be less than 0.45% Ak/k, which would not exceed .the technical y specification of +0.65% Ak/k.

l The installation of the movable graphite plug was expected i to' result in a' reactivity change of -0.13% Ak/k. The Reac- 1 tor Safety Cemmittee found that no unresolved safety issues i existed for either change and-authorized procedures to.in- ,

stall the graphite plug rirst and'then perform the fuel i

addition.

l 7. - No radioactive effluents were released.or discharged to the  ;

environment during 1989.

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, 8. No person using the facility received'a whole body exposure f of. greater than.50 millirem during 1989; f

l , 9. Neutron and beta / gamma radiation surveys performed on the i ', exterior walls of the faci?'<y indicated that maximum com-bined contact radiation le, s were less than 2 mrem /hr.

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