ML20041G200
| ML20041G200 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 02/01/1982 |
| From: | Auterino L POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | |
| Shared Package | |
| ML20041G194 | List: |
| References | |
| NUDOCS 8203190385 | |
| Download: ML20041G200 (6) | |
Text
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OPERATING DATA REPORT DOCKET NO. 50-286 DATE February 1, 1982 COMPLETED BY L.
Auterino TELEPHONE (0141 7lo-8200 OPERATING STATUS
- 1. Unit Name:
Indian Point No. 3 Nuclear ?cwer Pl ant
- 2. Reporting Period: January, 1982.
- 3. Licensed Thermal Power (MWt):
3025
- 4. Nameplate Rating (Gross MWe):
1013 965
- 5. Design Electrical Rating (Net MWe):
926
- 6. Maximum Dependable Capacity (Gross MWe):
891 T. Maximum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.Give Reasons:
- 3 s
- 9. Power Level To Which Restricted. lf Any (Net MWe):
- 10. Reasons For Restrictions,if Any:
This Month Yr..to.Date Cumulative' 744 744 47545
- 11. Hours In Reporting Period
- 12. Number Of Hours Reactor Was Critical 736.4 736.4 32842.6 0
0
- 43. Reactor Reserve Shutdown Hours 0
727.7 727.7 31671.4
- 14. Hours Generator On-Line
/
-iS. Unit Reserse Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWH) 2,055,809 2,055,809 81,083,371
- 17. Gross Electrical Energy Generated (MWH) 609.630 609.630 25 405.760 IS. Net Electrical Energy Generated (MWH)
"94 470 "94 470
'a 111 977
- 19. Unit Service Factor 97.9 97.8
.66.6
- 20. Unit Availability Factor 97.8 97.8 66.6
- 21. Unit Capacity Factor (Using MDC Nets 88 2 88.2 57.4
- 22. Unit Capacity Factor (Using DER Net) 91 4 91 4 52 0
- 23. Unit Forced Outsge Rate 22 22 14 7
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and.9urstion of Each):
Pefuelina out v.n
- twch lor 2 25, if Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. L* nits in Test Status (Prior to Commercial Operationi:
Forecast Achieved INITIA L CP.s flCALITY INITIA L ELECTRICITY COMMERCIA L OPER ATION 8203190385 820208 PDR ADOCK 05000286 PDR (9/77)
R
AVEllAGE DAILY UNIT POWER 1.EVEL
+
DOCKET NO.
Co-?E I fl0 l allt l'O I ilL UNIT No.3 DATE 2/1/82 L-Auterino-COMPLETED BY TELEPl!ONE 914-739-82fo 1
i MONTil January 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVERACE DAILY POWER LEVEL (MWe Net)
(MWe-Net) g' 836 37 825 837 18 826 2
827 838 39 3
694 20 830 4
831 231 21 828 831 22 6
830 826 23 7
831-806 24 8
829 823 23 9
765 832 26 10 728 831 27 33 778 733 32 28 830 733 13 29 i
826 30 732 34 824 732 g3 3,
827 16 INSTRUCTIONS i
l On this format, list the average daily unit power levelin MWe Net for each day in the reputimg month. Compute :o the nearest whole megawatt.
(9/77) l l
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MONTIILY I & C CATEGORY I REPORT January 1982 Month
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DATE W.R.
EQUIPMENT MALFUNCTION CORRECTIVE ACTION 12-20-82 IC-1-942-2 3 PIA-1053 32 small gas No output from transmitter Replaced faulty pneumatic decay tank pressure relay 1-14-81 IC-1-989-3C Valve 891C 33 Accumulatoi Solenoid grounded cleared ground gas valve 4-15-81 IC-1-1050-3C Steam Generator second-Improper reading RTD wire resoldered at RTD ary temperature 5-12-81 IC-1-ll62-2 LT-437B Steam Generator Failed while calibrating Replaced amplifier in 33 Level Transmitter transmitter 5-20-81 IC-1-ll65-2 R2 Area Monitor Pegged high Repaired connector on input cable 5-12-81 IC-1-ll71-2 LT-437D Steam Generator 7 t Output does not respond Replaced amplifier in Wide Range Ievel properly to input Transmitter Transmitter 5-22-81 IC-1-ll73-3B R7 Area Monitor Erroneous high reading Replaced alarm circuit board 12-11-81 IC-1-1510-2 Boric Acid IIcat Trace Thermostat not working Reconnected thermocouple Circuit 39 for Boric test wire Acid Transfer Pump 32 12-28-81 IC-1-1523-2 R15 Area Monitor Recorder not functioning Corrected improper nating Recorder of connector
MOllTIILY llAltfTEllAllCE REPCitT January 1982 Honth
- DATE, W.11.
R EQUIPf1Ettr 11AIEUtiCTIOti CORRECTIVE ACTIOtt 1-19 l-2469 Pressurizer backup heaters Circuit Breaker opened Reset Breaker Group #33 1-19 l-2572 BFD-77/BFD-78 Aux. Boiler IIandwheels separated from opera-Resecured handwheels to Opcrators feed pump recirculation tors valves to the CST l-19 1-2573
- 34 Service Water Pump Vacuum breaker inoperable Disassemble / Cleaned /Reasse,mble o
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e
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DOCKET NO.
50-286 UNITSIIUTDOWNS AND POWER REDUCTIONS UNIT NAME Tndian Point No. 3 r
DATE Fohru,ry 1; lon2 COMPLETED fly L.
Autcrino REPORT MONTil Jamrarv 1982 TELEPflONE (914) 739-8200 i
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}Yh Licensee E-r, gm.
Cause & Corrective No.
Date g
3g
,s5 Event 3,7 p' '
Action to H
yE E
3 ;p3 Repori #
in V Prevent Recurrence c
o 3
O b
01 820104 F
16.3 A
3 SD 7ALVOp-F A voltage spike on No. 32 instrument bus, which was generated by a short circuit on a weld channel and contain-ment pressurization system solenoid valve, caused the activation of the dropped rod circuitry. The dropped rod indication aute natically initiated a turbine runback. During the runback, the unit tripped on steam / feed flow mismatch coincident with a low level in No. 32 steam generator. The sole-noid coil was replaced and startup was commenced.
l I
2 3
4 F: Forced Reason:
t Method:
i Exhibit. Inst ructions S: Scheduled A Equipment Failure (Explain) i 1-Manual for Preparation of Data l
H Maintenance or Test 8
2-Manual Scram.
Entry Sheets for Licensee
'C Refueling 3 Automatic Scram.
Event Repor (LER) File (NUREG-D-Regulatory Restriction l
4 Other (Explain).
0161)
E-Operator Training & License Examination F-Administrative S
G-Operational Error (Explain)
Exhibit, Same Source t'J/77)
Il-Other (Explain) t
a.
SUMMARY
OF OPERATING EXPERIENCE Indian Point Unit 3 was synchronized to the bus for a total of 727.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> producing a gross generation of 609,630 MWe for the reporting period.
One trip and two load reductions were experienced during this period.
On January 4, at 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> the plant experienced a turbine runback and subsequently a unit trip on a steam flow-feed flow mismatch coincident with low level in No. 32 Steam Generator. A voltage spike on No. 32 instrument bus, which was generated by a short circuit on a weld channel and containment press-urization system solenoid valve caused the activation of the dropped rod circuitry.
This initiated the runback which resulted in the trip.
The solenoid coil was replaced and plant startup was commenced.. On January 5, at 1220 hours0.0141 days <br />0.339 hours <br />0.00202 weeks <br />4.6421e-4 months <br /> the generator was sychronized to the bus and commenced power escalation consistent with maintaining flux difference within target band.
On January 12, at 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br /> commenced load reduction after experiencing an intermittent spike on a reactor protection channel. An investigation led to replacir.y the resistance temperature converter associated with No. 34 RCS loop hot leg. Lepairs were completed and at 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> the unit was returned to full load.
On January 26, at 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br /> commenced load reduction to allow the removal of #32 condensate pump from service for repairs.
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