ML20041F200
| ML20041F200 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 03/01/1982 |
| From: | Peterson D CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | |
| Shared Package | |
| ML20041F199 | List: |
| References | |
| NUDOCS 8203160284 | |
| Download: ML20041F200 (4) | |
Text
v AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-255 UNIT Palisades DATE 3/1/82 COMPLETED BY D. Peterson TELEPflONE 116) 764-8913 t
MONTil FEBRUARY 1982
,/ '
DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL
~
~
(M We-Net)
(MWe-Net) 1 506 0
E7 2
714
.18 0
e 3
735
, 39 g
114 4
20 0
O 5
2t.
n 0
6 22 -
n 0
^
7 23 n t' 8
0
' /
24 a
9 25 0
10 0
26 0
11 0
27 0
/
^
12 n
28 0
7 13 0
79 14 0
30 f>
15 n
3, I
n
/
/
INSTRUCTIONS On this format. list the aserage daily unit power levelin MWe. Net for each day in the reportine month. Compute to the nearest whole megawatt.
(9/77)
.c a
B203160284 820308 PDR ADOCK 05000255 R
i
~ I; g
y 3
g E
_)
,.I UNITSilUTDk)WNS AND POWER REDUCTIONS '
DOCKET NO..
50-255 UNIT NAME Palisades
~
DATE 1/1/RP REPORT MONTil FEBRUARY COMPLETED BY D VanDenBerg -
s TELEPilONE (616) 764-8913 s
.e I
s
,1
.m
- 3. Jab, E
=
c
~.
5E E
.s y Licensee
,E-t
$"L Cause & Corrective \\
y"-
DJ3C o
g-i
- $ E 4,
.5 g oc
- E, vent,
=?
- 9. ?
- Action to p
-s -
gi;5 g Report a in U ec c=
ac g
PrnentRecinrence
.e s
a 2
4 5
820204 F
595.9 sA 3
Cooling Tower Pump Tri,p.
N
,..s N
~
A
\\
s u
'\\
7 4
-+,p
- .t 1
x 3
m.,,
1 I
2 3
4 F: Forced Reason:
Method:
Exhibit G-Instructions S: Scheduled A-Eqaipment Failure (Explain) 1-Manual for Preparation of Data B Maintenance of Test 2-Manual Scram.
Entry Sheets for Licensee C Refueling 3 Automatic Scram.
Event Report iLER) File (NURI G-D-Regulatory Restriction 4-Other ( Explain )
0161)
E-Operator Training & License Examination F-Administrative 5
G-Operational Error (Explain)
Exhibit 1 - Same Source l'8/77) 1101her (Explain)
. _ _.. _... -... - _ _ =
- - - ~ _ - -
(
t t
OPER ATING DATA REPORT j
r DOCKET NO.
50-255 DATE 1/1/82 N
13
~
EL
)
i OPER ATING STATUS a
a
- 1. Unit Name:
Palisados Notes
- 2. Reporting Period:
820201 - 870228
- 3. LianscJ Thermal Power (MW ):
2530 811.7
- 4. Nameplate Rating (Gross MWe).
y 805
- 5. Design Electrical Rating (Net MWe).
I
- 6. Masimum Dependable Capacity (Gross MWe): *675
- 7. Masimum Dependable Capacity iNet MWe):
- 635
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.Gise Reasons:
- 9. Power Lesel To Which Restricted,1f Any (Net MWe):
- 10. Reawns For Restrictions,if Any:
i t
This Month Yr.-to Date Cumulatise
- 11. Hours in Reporting Period 672 1.416
_ 89.391 r
- 12. Number Of Houn Reactor Was Critical 76.1 724.1 49,447.3
- 13. Reactor Resene Shutdown Hours 76.I
- 14. Hours Generator On Line
_ _ 568.3 46.772.7'
- 15. Unit Resene Shutdown Hours
- 16. Gross Thermal Energy Generated (MWH) 168,384 1,116,336 92,523,600 342,810 28,570,760 l
p 52,920 320,262 26.833,195
[
?
- 17. Gron Electrical Energy Generated (MWH) 1S. Net Electrical Energy Generated (MWH) 49,671 11.3 40.1 52.3 l
- 19. Unit Senic-Factor
- 20. Unit Asailability Factor 11.3 40.1 52.3 11.6 35.6 47.3 l
- 21. Unit Cr Factor (Using MDC Net) 9.2 28.1 37.3 g
- 22. Umt Cap..u, netor (Using DER Net)
- 23. Unit Forced Outage Rate 88.7 59.8 33.7 l
l~4
- 24. Shutdowns Scheduled Oser Nest 6 Months tT; oe.Date and Duration of Each):
f f
(
4' a
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
3/3/82
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achiesed 4
INITI A L CRITICA LITY j
INITI A L ELECTRICITY 7
t'OMM ERCI AL OPER ATION
.i i
j
~
- Based on condenser back pressure (4/77)
\\
4
SUMMARY
OF OPERATING EXPERIENCE FOR FEBRUARY 1982 The Plant tripped February 4 when a cooling tower pump tripped on low lubrication flow. Approximately eight hours later a hydrogen explosion occurred in the exciter of the main generator. The Plant was shutdown for repairs the rest of the reporting period.
1 t
r, e
-en.
- - --