ML20040H482

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Supplementary Deficiency Rept Re Shutdown Cooling Sys Flow Control Valve Coupling Failure.Valve 2FV-0306 Will Be Changed from Remote to local-manual Operation for First Fuel Cycle
ML20040H482
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 02/04/1982
From: Papay L
SOUTHERN CALIFORNIA EDISON CO.
To: Engelken R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
10CFR-050.55E, 10CFR-50.55E, NUDOCS 8202180297
Download: ML20040H482 (2)


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or Southern Calitbrnia Edison Company g5 RO. SON 800 2244 WALNUT GROVE AVENUE ROSEMEAD, CALIFORNIA 91770 g pg,g uce passeosus as,.s73.Mpe February 4, 1982 Mr.

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Dear Mr. Eng'elken:

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Subject:

Docket No. 50-361 6

/;Nb San Onofre Nuclear Generating Station, Unit By letter to your office dated January 21, 1982 we transmitted a report regarding a failure of a valve coupling which we had previously reported to you as a potentially significant deficiency in accordance with 10CFR50 55(e).

Further developments have added to the corrective action we are taking regarding the reported condition.

Con-sequently, attached are twenty-five (25) copies of a supple-mental report entitled " SUPPLEMENTAL REPORT ON SHUTDOWN COOLING SYSTEM FLOW CONTROL VALVE COUPLING FAILURE, San Onofre Nuclear Generating Station, Unito 2 and 3."-

If you have any questions regarding this report, we would be happy to discuss them at your convenience.

1 Very truly yours, l

l Enclosures cc:

Victor Stello (NRC, Director I&E) l A. E. Chaffee (NRC, San Onofre Units 2 and 3) in l

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SUPPLEMENTARY REPORT ON SHUTDOWN COOLING SYSTEM FLOW CONTROL VALVE COUPLING FAILURE San Onofre Nuclear Generating Station, Units 2 and 3 INfRODUCTION By letter dated January 21, 1982, Southern California Edison trar.smitted a report regarding the failure of the coupitng which connects the valve s tem to the pneumatic valve operator on shudown cooling system (SDCS) flow control valve FV-0306 installed in San Onofre Unit 2.

That report recorded the results of investigation o f causes, analysis o f safety implications, and corrective action taken or to be taken.

This supplementary report provides additional information on corrective action which has been developed as a result of testing by the valve manufacturer.

CORRECf1VE ACTION SONGS-2 Shutdown Cooling Flow Control Valve 2FV-0306 will be changed from remote to local-manual operation for the first fuel cycle.

Specific modifications being made to 2FV-03J6 to ensure the actuator-to-valve coupling will meet specified service requirements are as follows:

1-A coupling larger than the one that f ailed (3" rather than 2") and made of AISI 4140 heat treated steel will be used.

2-Inside corner s tress concentration in the coupling, associated with use of a square broach, will be reduced by chamfering the corners of the broach.

3-The penumatic actuator will be disabled by removing the spring and spring housing.

4-rhe engagement clutch will be secured in the manual override position by installing a cover to preclude inadvertent disengagement.

5-A permanent, durable tag will be attached to the handsheel specifying the rim pull load lim t.

Ad ditionally, the "Open" "Close" direction will be clearly indicated on the handwheel.

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