ML20040F431

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Responds to 811207 Request for Addl Info Re Station Electric Distribution Sys Voltage Adequacy.Voltage Analysis Performed to Determine Transient Effects.Verification Test Results Encl
ML20040F431
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 02/04/1982
From: Gallagher J
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Stolz J
Office of Nuclear Reactor Regulation
References
NUDOCS 8202090188
Download: ML20040F431 (4)


Text

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s PHILADELPHIA ELECTRIC COMPANY 2301 M ARKET STREET P.O. BOX 8699 PHILADELPHI A. PA.19101 JOSEPH W. GALLAGHER sosetnic enoo."evIo oseantuswr (215)841 5003 February 4, 1982 Docket Nos. 50-277 30-278 i

Mr. John F.

Stolz, Chief Operating Reactors Branch #4 Division of Licensing U.S.

Nuclear Regulatory Commission Washington, DC 20555

Dear Mr. Stolz:

4 Your letter of December 7, 1981 requested additional information with regard to adequacy of station electric distribution system voltages for Peach Bottom 2 & 3.

These requests are restated below and are followed by our responses.

1.

Verify that the voltage transient caused by starting of the RHR motors will not prevent proper operation of other Class i

1E equipment connected to the distribution system, at all voltage levels of operation.

RESPONSE

A test was conducted at Peach Bottom to determine the effects of an RHR motor starting transient on ther Class IE equipment.

This test was conducted by isolating a 4 kV bus from the startup sources and supplying it via a diesel generator.

Instrumentation was provided to monitor contacts of several 82020901EE 820204

-PDR ADOCK 05000277 bse p-PDR

4 d

Mr. John F.

Stolz, Chief Page 2 different size 480V contactors and several different types of 120V relays.

The RHR pump was started on the 4 kV bus and produced a starting voltage transient of 60% nominal at the different voltage levels.

All the contactors and relays stayed in their picked-up condition without interruption during the starting transient.

It is expected that the same results would be obtained from a starting transient of this magnitude when operating on the startup sources.

The results of this test indicate that a voltage transient of this magnitude should not prevent proper operation of any 480V or 120V equipment connected to the distribution system at the time.

The use of a new transient analysis program has shown that the worst case for an RHR motor starting transient produces a voltage dip to 71.8% nominal on the 4 kV buses.

A previous program, which used a more conservative approach, indicated a worst case motor starting voltage drop to 59.4% nominal.

The worst case is for one unit at power, an accident in the other unit, the grid operating at 95%, and the loss of an off-site startup source just prior to the accident.

The worst voltage transient occurs during the start of the second pair of RHR pumps.

Since the voltage transient test which produced a dip to 60%

nominal indicated that there would be no mis-operation of relays or contactors, the new calculated dip of 71.8% nominal is considered acceptable.

2.

Perform a voltage analysis to determine the transient effects, if any, on engineered safety features performance during startup of a large, non-Class IE, motor.

RESPONSE

A transient analysis was performed to determine the transient effects on engineered safety features performance during the start of a 4500 (horsepower) condensate pump.

The case analyzed was with an accident in one unit and the other unit at power.

Only one startup source was available, the transformer had increased to its full boost tap position.

When the station buses transferred to the startup source, the cooling tower load was automatically shed and it was assumed that two condensate pumps were lost in the transfer.

Since two condensate pumps may be needed shortly after an accident, this case represents the i

i

Mr. John F. Stolz, Chief Page 3 i

start of the second pump.

The 230 kV grid was assumed to be operating at 95%.

The results obtained are shown below.

1 220-08 Line 218.5 kV 4

2SU Bus 12.7 kV 4 kV Buses 3.9 JkV 460V MCCs 439 V These results are within the acceptable limits that were provided previously.

3.

Submit results of voltage analysis verification tests in regard to questions 1 and 2.

RESPONSE

Two sets of tests were conducted at Peach Bottom to verify the results of the voltage analyses.

The first set of tests was run to verify steady state conditions and the second set of tests was run to verify transient conditions.

The steady state tests were run with Unit 2 at Power and the 13.2/4 kV Emergency Auxiliary Transformer carrying approximately 54% Load.

The calculated and measured voltages are shown below.

Calculated Measured i

Line 220-08 238 kV 238 kV 2 SU Bus 13.79 kV 13.98 kV 4 kV Buses 4.28 kV 4.23 kV 460 V MCC 468 V 462 V The transient tests were run by starting a 2000 hp RHR pump on the 4 kV bus.

The calculated and measured voltages are shown below.

Calculated Maanured Line 220-08 238 kV 238 kV 4 kV Bus 3.94 kV 3.87 kV 460 V MCC 431 V 425 V l

4 4

y Mr. John F.

Stolz, chief-Page 4 Since the calculated voltages were found to.be within 2% of the measured voltages, it~1s considered that the results of the tests have verified the transient and steady state analyses.

s If there are any questions or'if we can provide any additional information, please do not hesitate to contact us.

Very truly yours, i

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