ML20040A147

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Monthly Operating Rept for Dec 1981
ML20040A147
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 01/05/1982
From: Norris H
CAROLINA POWER & LIGHT CO.
To:
Shared Package
ML20040A143 List:
References
NUDOCS 8201200403
Download: ML20040A147 (5)


Text

tinB osure to Serial: RSEP/82-31 Page 1 of 5 .

OPERATIt:0 DATA REPORT DOCEPT !!O: 50-261 DA'l E :T 0105 COMPLETED LY: 11 Rav !? orris TELLPlioi;E: 803-383-4524 OPERATJNG STAT 11S llo t e n .

1. Unit f;ame: 11 . B. Robinnon Unit Two
2. Reporting Period: 811201, 00007 811231, 2400 There are presently 113 spent fuel ansemblies stored in the spent fuei
3. Licenced Ther mal Power (II.!t ): 2300 pool.
4. !?anoplat e Rat ing (Gross I?.le):]l9
5. Imign Elect rical Rat ing (!!c t t r..'e ) : 700 6.11ax inun Dependable Capacit y (Gros <. f r.ie): 700
7. !!axiuum Dependable capacit y (! et !!We ) : G5 C. IfReanonr.

Change: Occur in Capacity !;atingn (Iten.1;ua.ber 3 through 7) Since Last Re p o r t- , Cive

?;o chan;*e.

9. Power Level t o Which Kest rict ed, If Any (t et FNe): %535 (80% Reactor Power)
10. Reasonn For Rentrictions, If Any: Althouch the_ unit is not restricted by any outside

_ agenc;; the power level is presently reduced due to steam generator considerationn.

This !! ant h Yr.-to-Date Cumulative

11. llaurn in Iteport ing Pi riod 744 12 i oebc . o f 8760 94,926
..,u.

. Ecat. l oi Nas Cr it icoi 671.43 tohu.14 / 2 34 5. t. 2

13. React or 1:eserve Shut down llours 0 ~ 107.42 10S '> . 3 0 14 !!ours Generator On-Line 632.56 63'J6.49
15. Unit Rererve Shutdown Ilourn 70555.31 o~" 0 23.20
16. Gronn Thermal Energy Generated (!!Ull) 1,039,737~~ 11,883,00J 143,095,3/4 -
17. Gros. Elect rical Energy Generat ed (!C11) ~~T3T7+TtI~ ~ 3,73),76T 7 COT 5,970-
18. !!ct 1: leet :1 cal 1:nergy Generat ed (1:WH) 3UFii67i-~ 3,50T'7 F 437Clo,251-l 's . Unit Service Factor 65.0 T 20 Unit Availability Tactor 73.01 /4.32-

~ ~lI'I.02 73.01 74.3s-~ -

21. lin it Ca pac i t y Fa ct or (th.ing MDC !!et ) 62.M
22. Unit Capaci t y Fact or (l'c J un bl:R !!et) 60.14 69.10
23. Unit forced Outage Rate 59.50 57.13 65.64 14.97~~ 21.23 14.59
24. Shut dowtu; Scheduleil over !Jo:t 6 !!anths (Type, Date, and Duration or Each)':

refueling /mr.lutenance outage _in late winter.

25. If Shut Down At 1:nd of Report Period, Estinatel Date f Startup:
26. Uaits In Tent Stato:. (P: ac e to Ccmcrcial Gperat 'on): Forecast Achicved INITJAL CRITICALITY A -- --

INITIAL ELECTRICITY -- --

COMMERCI AL OPl: RATION -- --

1 F2D12OO403 820114 8 PDR ADOCK 05000261 1 -

R PDR ~

, . I

Page 2 of 5 AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-261 UNIT _ II. B. Robinson T DATE 820105 CO5!PLETED By 11. Ray Norris TELEPilONE 803-383-4524 MONT1: __ December DAY /,yEg A GE DAILY POWER LEytt DAY AVERACE D.\lLY POWER LEVEL (5t h Net)

IMWe Neti I -6 97 2 -20 18 550 3 __

-20 39 556 4 _

362 20 561 5 424 21 Sig 6 29 22 462 216 7

s 345 24 553 403 9

10 408 26 560 g3 404 27 548 ,

12 ___

522 2S 547 13 559 -

29 451 14 561 30 557 15 560 31 559 16 528 INS 1 RUCTIONS Onocatest the this formst,tist the whole mepwstt. symge daily unit power levet in MWe Set for each d:y in the reporting mo (9/7TI

. . ._ -. _. _ _ _ . . _ __ _ _.m _ _ . _ _ . _ - . ____m_. . . - _ _ _

Enclosure to Serial: RSEP/81-31 Page 3 of 5 UNITS!!UTDOWNS AND POWER REDUCTIONS Dg O.

Robtnson Unit

. DATE 9W" CO.\t."LETED I:Y H. Rav Norris

, REPORTMONTl! December TEl.LPl!ONE 803-383-4524

- = E

, ,$? E= $ .Y E Licensee ,5% '

No. Date g 3g 5 j g& Event ft Cause & Currective

7 c- 3 Action tu 8-f5 5 di e Report
80 5' Prevent Recurrence

% g -

v ,

O 12-01 811201 F 54.73 A 1 81-26 MB HTEXCH S/G Tube Leak (Continuation) 12-02 811203 F 16.32 A 1 --

HH VALVEX "B" WRV Malfunction 12-03 811206 F 11.01 A Mi 1 --

VALVEX, "B" WRV Repaired 12-04 811206 F 3.11 A 3 EA

~ --

INSTRU Rx trip due to low S/G level and steam flow - feed flow mismatch 12-05 811207 F 7.15 A 3 - -

BB INSTRU Grounded limit switch "B" MSIV shut,

, resulting in low S/G 1evel. -

'12-06 811216 F 19.12 A l' -

HA PUMPXX "B" EH Pump Seal Leak 12-07 811207 F --

A 4 --

HH VALVEX Load reduction due to "B" feedwater reg. valve (HiaP across valve) 12-08 811221 F -

A 4 -

SH VALVEX Load reduction due to "B" FWRV drain line leak; 12-09 811228 F --

A 4 --

HH PUMPXX Load reduction due to "A" main feed pump recirc. line leak I . 2 3 4 F: Forced Reason:

S: Ssl:edu!cd Method:

A Equipment Fai ure(Exp!:In) t-Manual Exhibit G Instructions Itataintenance of Test , for Preparatin of Data 2 Manu21 Scrarn. Entry Sheets for !.iecnsee C Rciueling .

D Regula:ory Restri;; tion 3 Autornati: Scram. Event Repin t (I.I.'R) life (NUREC.

4 Other (Explain) 016 )

L43perator Tr:,ining & License Examinsaion F Aduu:mtra:ive -

G Operati.:nal in cur (Explain) 5 (9/77) 1104her (Explain) Exhibit I Same Source

. i' -

OPERATING DATA REPORT

  • Corrected Copy
  • DOCF,ET NO: 50-261 DATE: 811203 COMPLETED DY: !!. Ray Norris TELEP110NE: 803-383-/A24 OPERATING STATUS Notes:
1. Unit Name: 11. B. Robinson Unit Tw There are presently 113 spent fuel
2. Reporting Period: 811101,0000/811135,M O assemblics stored in the spent fuel
3. Licensed Thermal Power (MN): 2300
  • 1
4. Nameplate Rating (Gross N.Jc):~739
5. Design Electrical Rating (Net FMe): 700
6. M1ximum Dependable Capacity (Cross FMe): 700
7. Maximum Dependable capacity (Net FNe):_665 l 8. If Changen Occur in Capacity Ratings (Item Number 3 through 7) Since Last Report, Cive Reasons: No change.
9. Power Level to Which Restricted, If Any (Net FMe): %325 (50% Reactor Pcwr)
10. Reasons For Restrictions, If Any: Although the unit is not restricteil by any oufaIde~

agency, the power IcVel is presently reduced due to steam generator considerations.

l This Month Yr.-to-Date Cumulative l

11. I!vut s Jn br.c.rring Pc:-1:;d 720 8016 94,182
12. Number of Ilours Reactor Was Critical D 7 F ~ 7 908./1 71673.99' l13.ReactorReserveShutdownllours 0 *107.42 *1085.30
14. Ilours Generator On-Line 163.13 5763.93 69922.75
15. Unit Reserve Shutdown llours 0.00 0.00 23.20
16. Cross Thermal Energy Cencrated ()Mll) 182,326 10,843,264 142,055,638
17. Cross Electrical Energy Cencrated (FMll) 55,381 _3,404,745 45,743,512
18. Net Electrical Energy Generated (lMll) 43,006 3,193,905 43,310,357
19. Unit Service Factor 22.65 71.90 74.24
20. Unit Availability Factor 22.65 71.90 74.26
21. Unit Capacity Factor (Using MDC Net) 8.98 59.92 69.15
22. Unit Capacity Factor (Using DER Net) 8.53 56.92 65.69
23. Unit Forced Outage Rate 77.3a 21.92 14.59
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, arid Duration of Each):

Refueling / Maintenance Outage in late winter.

25. If Shut Down At End of Report Period, Estimated Date of Startup: 12-1-81
26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY -- --

INITIAL ELECTRICITY -- --

COMMERCIAL OPEIMTION ,

(9/77) og .

p. ,

Page 5 of 5

-m l 1

OPERATING DATA REPORT

  • Corrected Copy DOCKET No: 50-261 DATE: 811103 )

COMPLETED BY: M. Watford TELEPHONE: 803-383-4524 OPERATING STATUS Notes:

1. Unit Name: __II. B,_Rshinson Unit Tun There are presently 113 spent fuel
2. Reporting Period: 811001, 0000/811031, 2400 ssemblies stored in the spent fue]
3. Licensed Thermal Power (MWt): 2300 pool.
4. Naueplate Rating (Groes MUe): 739
5. Design Electrical Rating (Net MWe): 700
6. Maximum Dependable Capacity (Gross MWe): 700
7. Maximum Dependable Capacity (Net MWe): 665
8. If Changes Occur in Capacity Ratings (Item Number 3 through 7) Since Last Report, Give Reasons: No change.
9. Power Level to Which Restricted, If Any (Net MWe): 4325 (50% Reactor Powori
10. Reacons For Restrictions, If Any: Although the unit is not restricted by any outside agency, the power level is presently reduced due to steam generator considerations.

This Month Yr.-to-Date Cumulative

11. Ilours in Reporting Period 745 7296 93.462
12. Number of Ilours Reactor Was Critical 745 5737.96 71.503.24 l 13. Reactor Reserve Shutdown Hours * .00 *107.42 _ *1085.30
14. Ilours Generator On-Line 735.80 5600.80 69.759.62
15. Unit Reserve Shutdown llours 0.00 0.00 23.20
16. Gross Thermal Energy Generated (MWil) 843,881 10,660,938 141.873.312
17. Gross Electrical Energy Generated (MWil) 25.',864 3,349,364 45.688.131
18. Net Electrical Energy Generated (MWil) 232,179 3,150,899 43.267.351
19. Unit Service Factor f8.77

! 76.77 74.64

20. Unit Availability Factor 98.77 76.77 74.66
21. Unit Capacity Factor (Using MDC Net) 46.86 64.94 69.62
22. Unit Capacity Factor (Using DER Net) 44.52 61.70 66.13
23. Unit Forced Outage Rate 1.23 15.87 14.03
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

Two outages are planned within the next six months: one in early November nna n refueling / maintenance outage in late winter.

25. If Shut Down At End of Report Period, Estimated Date of Startup: on line.
26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY -- --

INITIAL ELECTRICITY -- --

COMMERCIAL OPERATION -- --

(9/77) eg l