ML20039G736
| ML20039G736 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 01/11/1982 |
| From: | Clayton F ALABAMA POWER CO. |
| To: | NRC |
| Shared Package | |
| ML20039G737 | List: |
| References | |
| NUDOCS 8201190067 | |
| Download: ML20039G736 (3) | |
Text
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
e g
M:lling Addr:m Alabama Power Campany 600 Nortn 18th Street Post Office Box 2641 Birmingham. Alabama 35291 Te'eohone 205 783-6081 F. L C W'on, Jr.
Senio... Dresident Alabama Power Flintric.
+ng it'e southen elecinc system January 11, 1982 Docket No. 50-348 4?
A a
RECE!tign "
Director, Office cf Management
. b g
8 /0g O Ir.fornation and Program Control I
g U. S. Nuclear Regulatory Co= mission Washington, D.C.
20555 g
p
Dear Sir:
s
/f RE: Joseph M. Farley Nuclear Plant Menthly Operating Data Report Unit No. 1 Attached are two (2) copies of th'e December, 1981 Monthly Operating Report for Joseph M. Farley Nuclear Plant, Unit 1, as required by Section 6.9.1.6 of the Appendix A Technical Spccifications. As requested by letter f rom Mr. John F. Stolz to }k. Alan R. Barton, dated October 21, 1977, a " Narrative Su= mary of Operating Experience" is included in the attached repert.
If you have any questions, please advise.
Yours very truly,
'l s
y / <
i s
.3 a
< : c. i
<. 1, -,
F. L'." Clayton, Jr.
j
~
i FLCJr/KD1:bhj Attachments cc:
Mr. Ted Cintula (1 copy)
Director, IE (10 copies)
Director, RII (1 copy) s, 'I
$%8Te8fS$8@H R
,g c.
JOSEPH ?!. FARLEY NUC. EAR PLANT UNil' 1 NARRATIVE SLWL\\RY OY OPERATIONS DECEMBER, 1981 The unit continued to be shutdown through the month of December for repair of the main generator and Cycle 3 - Cycle 4 refueling operations.
The following safety-related maintenance was performed in the month of December:
- 1. Performed miscellaneous maintenance on diesel generators.
- 2. Performed various design changes required by NUREG-0737 and NUREG-0588.
STEAM GENERATOR TUBE PLUGGING Past experience at FNP indicates the majority of k'estinghouse steam generator tube leaks occur on the steam generator inner row tubes. Therefore, a management decision was made to plug all the inner row tubes of the three Unit 1 steam generators to prevent unplanned outages in th2 future.
Date of Plugging: 12/15/81 All S/G IC inner row tubes were plugged with the exception of the following inner row tubes which were previously plugged.
Row Column 1
27 1
38 1
39 Date of Plugging: 12/16/81 All S/G 1B inner row tubes were plugged with the exception of the following inner row tubes which were previously plugged.
Row Column 1
8 1
11 1
19 1
29 1
51 Date of Plugging: 12/17/81 All 94 S/G 1A inner row tubes were plugged.
I