ML20039G264
| ML20039G264 | |
| Person / Time | |
|---|---|
| Site: | Beaver Valley |
| Issue date: | 08/04/1981 |
| From: | Timko D DUQUESNE LIGHT CO. |
| To: | |
| Shared Package | |
| ML20039G263 | List: |
| References | |
| NUDOCS 8201150442 | |
| Download: ML20039G264 (6) | |
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OPERATING DATA REPORT DOCKET NO. 50-134 DATE
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1 COMPLETED BY D. R.
Tinko TELEPil0NE..L..? -^M-9308 OPERATING STA1US
- 1. Unit Namer Beaver Valley Power Station, Unit #1 N05 I'
- 2. Ripotting Period:
- 3. Licensed The inai Power (MW ):
2660 4
923
- 4. Nameplate Rating (Gross MWe):
852
- 5. Design Electrical Rating (Net MWe):
845
- 6. Sfaxinurt Depencable Capacity (Gross MWe):
810
- 7. Muimum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Irems Number 3 Through 7) Since Last Report.Give Reasons:
- 9. Power Level to which Restricted. If Any (Net MWe):
None
- 10. Reasons For Restuctions.If Any:.
N/A
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This Month Yr to.Date Cumulative 744 5,087 4 fi,031 II. Hours In Reporting Period 417.4 3,024.el 17.551.28
- 12. Numbe: Of Hours Reactor was Critical 0
0 4.482.8
- 13. Reactor Reserve Sh*:tdown Hours
- 14. Houn Generater On.Line 415.57 2,968. 91 t.
16.676.16
- 15. Unit Reserve Shutdown Hour:,
0 o
.o l,000, 0 6. O')
_7.322,017.4/ 35,429.910.62
- 16. Gross Tnerreal Energy Generated (MWH) 2,361,600 10.988,940 L
- 17. Gross Electrical Energy Generated (MWH)
- 18. Net Electrical Energy Generated (MWH) 317.551 2,176,347 10,037,852 t
55.y 58.4
.$ / 3
- 19. Unit Serse Factor 33.
8.4 37.5 l
- 20. Unit Availability Factor
- 21. Unit Capacity Factor SUsing MDC Net) 52.7 52.8 30.1
- 22. Unit Capacity Factor (U ing DER Net) 50.1 50.2 28.6 41.6
- 23. Unit Forced Outage Rate 44 l 45.2 l
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Eacht:
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p r. f n e l i n o Ouraoe/Januarv 2/13 Weeks
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units In Test Status (Prior to Commercial Operationi:
Forecast Achieved INITIA L CRITICA LITY N/A N/A INITIAL ELECTRICITY N/A N/A COMMERCIAL OPERATION N/A N/A (9/77)
R201150442 810810 PDR ADOCX 05000334 R
5,
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AVERAGE DAILY UNIT POWER LEVEL
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50-334
^
DOCKET NO.
UNIT BVPS Unic #1 8/4/81 r
DATE D. R. Ticko COMPLETED BY TELEPHONE 412-643-5308 J -' ' '
July, 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL
, l' (MWe-Net)
(MVe-Net) 788
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0 g7 g
791
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0 2
18 3
19 783 0
4 20 775 0
5 21 787 o
6 22 779 0
7 23
^ 774 0
8 24 774 0
9 25 0
782 10 26 791 0
Il 27 787 0
,=
12 28 774 0
13 29 783 0
14 30 15 31 16
':-779 INSTRUCTIONS On this forrnat. list the average d.riy unit power leselin Mn'e. Net for each day in the reporting inonth.Connpute to the nearest whole megawait.
(4,I771 y
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i UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-334 UNIT NAME BVPS. Unit #1 i-DATE.
" # ' 1 REPORT MONTH July,1981 COMPLETED BY D.
R. Timko TELEPHONE' 412-643-5308 l
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jYh Licensee
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Cause A Correceive Da's k
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4 2i5 Event 37
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Assi.m to j0 3:
E jig Report *.
40 Prevens Recurrence 6
i 7
810719 F
328.43 A
3 CB Vessel The plant was being taken off line to repair a blown rupture disk on thi i
pressurizer relief tank. When transferring f rom ~inain feed valves to bypass feed regulating valves, at 15% power, slow response of B bypass. feed regulating valve resultec.
in'a high steam generator level reactor trip. Replaced blown rupture disk.
b 4
1 2
3 4
F: Forced Reason:
Method:
Exhibit G. instructions S: Schedu?cd A Equipment Failure (Explain)
' l-Manual for Pseparaiom ol' Data 8 Maintenance cites 2 Manual Sesaan.
Entr> Shecis for Licensee C. Refueling-
. 3-Automatic Scram.
Event Repose Ill:RI File (NUREG D-Regulatory Restriction 4 Other IExplain) 01611-110pection Training & License Examination F Admmisstative i
G-OWrational Es tor IExplain t Estubis I Same' Source -
l't/77)
Il-Other (thplain i
i' DUQUESNE' LIGHT.CUNTANY' Beaver Valley' Power Station y
NARRATIVE
SUMMARY
OF MONTHLi OPERATING EXPERIENCE - JULY,-1981 j
July 1 Station in Operational Mode 1 at nominal full power. At 1125 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.280625e-4 months <br /> through on July 16, one of the two rupture discs on the Pressurizer Relief l
July 16 Tank (PRT) ruptured due to problems maintaining level and pressure within the tank.
July 17 Station in Operational Mode l'at nominal full power. At 0139 hours0.00161 days <br />0.0386 hours <br />2.29828e-4 weeks <br />5.28895e-5 months <br />, a reactor trip occurred due to high water 1cvel in the IB steam
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generator after the IB feedwater bypass flow regulating valve control-system did not adjust the feedwater flow quickly enough to stablize
-l the water level. At 0815 hours0.00943 days <br />0.226 hours <br />0.00135 weeks <br />3.101075e-4 months <br />, boration of the Reactor Coolant System-(RCS) to the cold shutdown boron concentration was begun. At 1053 hours0.0122 days <br />0.293 hours <br />0.00174 weeks <br />4.006665e-4 months <br />, 1
began cooldown of the RCS to 500F (pressure approximately 1800 PSIG) to permit replacement of. the PRT rupture disc. These. conditions were reached at 1249 hours0.0145 days <br />0.347 hours <br />0.00207 weeks <br />4.752445e-4 months <br /> and a maintenance team entered the containment i
to replace the PRT rupture disc. The installation of the rupture disc and the adjustment to the valve packing for Pressurizer Power-Operated l
Relief Valve (PORV) block valve [MOV-RC-535] were completed by 0030 i
hours on July 18.
Heat-up of the RCS was initiated at 0215 hours0.00249 days <br />0.0597 hours <br />3.554894e-4 weeks <br />8.18075e-5 months <br />. At 1318 hours0.0153 days <br />0.366 hours <br />0.00218 weeks <br />5.01499e-4 months <br />, the 1A containment air recirculation fan tripped due to high vibration warnings and the containment internal temperature began increasing. By 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br />,-the temperature was approaching the maximum allowable temperature and'cooldown of the RCS to Mode 5 conditions was connenced.
July 19 Station in Operational Mode 3 with the RCS pressure and temperature at approximately 1600 PSIG and 470F. The Station entered Mode 4 at 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br /> and Mode 5 an 1533 hours0.0177 days <br />0.426 hours <br />0.00253 weeks <br />5.833065e-4 months <br />. Containment vacuum was broken at 1559 hours0.018 days <br />0.433 hours <br />0.00258 weeks <br />5.931995e-4 months <br />.
p July 20 Station in Operational Mode 5 with the RCS pressuie and temperature th rough at approximately 60 PSIG and 170F. Maintenance crews were repairing July 28 the IB containment air -recirculation fan and moving the damaged motor l
from the 1A fan from the containment to the controlled area machine l
shop. Repairs to the IB fan'were completed by mid-afternoon on July 21.
l Final repairs and reassembly of the safety injection to the 1C RCS cold leg line check valve [SI-25] were completed at 0045 hours5.208333e-4 days <br />0.0125 hours <br />7.440476e-5 weeks <br />1.71225e-5 months <br /> on July 22 and station start-up was begun. At 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br />, with the station in operational Mode 5 e.nd start-up in progress, the station manegement-l received a report indicating potential problems with the pilot operator l
system of the main pressurizer relief valves.
Immediate action to l
inspect the valves was initiated and minor modifications were performed.
l In addition, repairs were made to two pressurizer power-operated relief valves prior to start-up.
At 1436 hours0.0166 days <br />0.399 hours <br />0.00237 weeks <br />5.46398e-4 months <br /> on July 28, operations personnel began drawing the containment' vacuum and, at 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />, began l
pressurizing the RCS.
I July 29 Station in Operational Mode 5 with the reactor coolant system pressure and temperature at approximately 326 PSIG and 158F. A reactor coolant pump (RCP) was started and RCS heat-up to Mode 4 was commenced. The station entered Mode 4 at 0516 ours and Mode 3 at 1917 hours0.0222 days <br />0.533 hours <br />0.00317 weeks <br />7.294185e-4 months <br /> with RCS I
heat-up to 547F in progress.
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. l DUQUESNE LIGHT COMPANY Beaver Valley Power Station NARRATIVE SLSDiARY OF MONfHLY OPERKf1NG EXPERIENCE - JULY, 1981 (continued)
July 30 Station in Operational Mode 5 with the reactor coolant system pressure and temperature at coolant system pressure and temperature at approximately 1400 PSIG and 460F with start-up in progress.
RCS temperature of 547 F was reached at 0330 hours0.00382 days <br />0.0917 hours <br />5.456349e-4 weeks <br />1.25565e-4 months <br /> and reactor coolant boron dilution from cold shutdown to start-up boron concentration was begun at 0645 hours0.00747 days <br />0.179 hours <br />0.00107 weeks <br />2.454225e-4 months <br />.
The reactor was critical at 1615 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.145075e-4 months <br />, the main unit generator was synchronized at 1805 hours0.0209 days <br />0.501 hours <br />0.00298 weeks <br />6.868025e-4 months <br /> and the station reached 100% power level at 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br />.
July 31 Station in Operational Mode 1 at nominal full power.
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DUQUESNE LIGHT COMPANY Beaver Valley Power Station MAJOR SAFETY-RELATED MAINTENANCE - July, 1981 1.
Replaced one of two rupture discs on the pressurizer relief tank.
2.
Repaired electric-pneumatic transducer for pressurizer spray valve [PCV-KC-455A].
3.
Replaced valve packing on pressurizer power-operated relief valves
[PCV-RC-455C and 455D).
4.
Replaced valve trim in pressurizer power-operated relief valve block valves [MOV-RC-535 and 537].
5.
Replaced the fan blade of the 1B containment air recirculation fan.
6.
Modified pressurizer pilot-operated relief valves [RV-RC-551A, 551B and 551C] to insure proper pressure sensing to the pilot operator system.
7.
Replaced the inboard seals on the IB main feedwater pump.
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