ML20039A219

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IE Insp Repts 50-259/81-28,50-260/81-28 & 50-296/81-28 on 810826-0925.Noncompliance Noted:Failure to Establish Fire Watch,To Have Special Work Permit & to Follow Procedures.App C & Details Withheld (Ref 10CFR2.790)
ML20039A219
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 10/29/1981
From: Cantrell F, Chase J, Paulk G, Sullivan R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20039A199 List:
References
TASK-1.C.5, TASK-2.E.4.1, TASK-2.E.4.2, TASK-2.K.3.13, TASK-2.K.3.27, TASK-TM 50-259-81-28, 50-260-81-28, 50-296-81-28, NUDOCS 8112160378
Download: ML20039A219 (13)


See also: IR 05000259/1981028

Text

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MATERIAL TRANSMITTED liEREWITH

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SAFEGUARDS INFORMATION

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CONTAINS 2.790@ UNITE] STATES

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NUCLEAR REGULATORY COMMISSION

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REGION 11

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101 MARIETTA ST

N.W., SUITE 3100

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ATLANTA, GEORGIA 30303

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0CT 3 01981

Report Nos. 50-259-81-28, 50-260/81-28 and 50-296/81-28

Licensee: Tennessee Valley Authority

500A Chestnut Street

Chattanooga, Tennessee 37401

Facility Name: Browns Ferry Nuclear Plant

Docket Nos. 50-259, 50-260 and 50-296

License Nos. DPR-33, DPR-52, and DPR-66

Inspection at Browns Ferry Site near Athens, Alabama

Inspectors:

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g R. F. Sul ivan

Date Signed

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f',- J. W. Chase

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G. L. Paulk

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Approved by:

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F. Cantrell,"Section Chief, Division of

Date Signed-

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Resident and Reactor Project Inspection

SUMMARY

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Inspection on August 26 to September 25, 1981

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Areas Inspected

This routine inspection involved 320 resident inspector-hours in the areas of

operational safety, reportable occurrences, plant physical protection, main -

tenance, surveillance testing, reactor trips, licensee action on previous

inspection findings, TMI action items, Unit I refueling, review of plant

operations, flooding of the residual heat removal service water pump room and an

emergency drill.

Resul ts

Of the 12 areas inspected, no violations or-deviations were identified in 9

areas. Six violations were found in 3 areas:

(failure to establish fire watch;

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MATERfAL TRANSMITTED HEREWml

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NS 2.7S0@ SAFEGUARDS INFORMATION

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MATERIA!. TRANSMITTED HEREWITH

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CONTAINS 2.790(d) SAFE 3UARDS INE0RVATl0N

failure in area of the security; failure to have special work permit (SWP);

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' failure to follow procedure paragraph 5; food found -in storage areas paragraph 7;

failure to take prompt corrective action). Two deviations were identified in two

areas:

(RHRSW pump test paragraph 9; and the failure of implementation of TVA's

response to inspection report 81-03 paragraph 3).

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MATERIAL. TRANSMITTED HEREWITH -

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CONTAINS 2.790 d) SAFEGUARDS Inf0MMTl0N

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DETAILS I

1.

Persons Contacted

Licensee Employees

H. L. Abercrombie, Power Plant Superintendent

J. R. Bynum, Assistant Power Plant Superintendent

J. L. Harness, Assistant Power Plant Superintendent

R. T. Smith, Quality Assurance Supervisor

R. G. Hetke, Engineering and Test- Unit Supervisor

D. C. Hims, Engineering and iest Unit Supervisor

R. G. Cockrell, Reactor Engineering Unit Supervisor

J. B. Studdard, Operation Section Supervisor

A. L. Burnette, Assistant Operations Supervisor

R. Hunkapillar, Assistant Operations Supervisor

T. L. Chinn, Plant Compliance Supervisor

M. W. Haney, Mechanical Maintenance Section Supervisor

J. A. Teague, Electrical Maintenance Section Supervisor

J. K. Pittman, Instrument Maintenance Section Supervisor

J. E. Swindell, Outage Director

B. Howard, Plant Health Physicist

R. E. Jackson, Chief Public Safety

R. Cole, QA Site Representative Office of Power

Other licensee employees contacted included senior reactor operators,

reactor operators, auxiliary operators, craftsman, technician, public safety

officers, QA personnel and engineering personnel.

  • Attended exit interview

2.

Exit Interview

Management Interview was conducted on August 28, Srptember 4,11,18 and

October 2, 1981, with the Power Plant Superintendent and/or his Assistant

Power Plant Superintendents and other members of his staff. The inspectors

summarized the scope and findings of their inspection activities.

The

licensee was infonned of 6 apparent violations and 2 deviations identified

during the report period.

3.

Licensee Action on Previous Inspection Findings

(Closed) Violation (296/81-03-05) Welding perfomed on safety related

system in which the individual welds could not be traced to a specific

welder.

The inspector reviewed Division Procedure N74M2 and confimed that

the weld data sheet was revised to include QC verification of welder certi-

fication.

In addition, the inspector reviewed several work plans in

,n~ ogress and noted that the welder had been verified as qualified by QC

prior to welding.

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(Closed) Violation 296/81-03-03) Personnel in high radiation area with no

dose rate instrument. The inspector discussed this incident with.various

personnel on site and found that they are aware of the requirement for

having a dose rate instrument with them in a high radiation areas.

(Closed) Violation 296/81-03-04) Personnel in radiation area without proper

Special Work Permit (SWP).

The inspector reviewed the corrective action

taken by the licensee and found it to be satisfactory. The inspector agrees

with the licensee that this incident was due to an error in judgement.on the

part-of the health physics technician.

(Closed) Violation (259/81-03-01, 260/81-03-01 and 296/81-03-02) Removal of

contaminated material from a regulated area without having the material

cleared by health physics. The inspector reviewed the licensee's response

to this item with regards to the retraining of the foreman involved and

found it to have been accomplished. The licensee stated in the response to

this item that an Outage Safety Awareness Bulletin would be used to brief

all outage personnel involved in the transportation of material from the

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plant. The inspector and the licensee could find no Outage Safety Awareness

Bulletin which discussed this item. The Assistant Plant Superintendent was

informed on August 28, 1981 that this was an apparent deviation from a

commitment.

(first example) (259/81-28-01, 260/81-28-01 and 296/81-28-01).

On August 31, 1981, an Outage Safety Awareness Bulletin was issued which

satisfied the licensee's commitment.

(Closed) Violation (296/81-03-01) Failure to follow procedure which

resulted in breaching of secondary containment door. The inspector reviewed

the licensee's response and found it to be adequate in regards to the new

interlock system. A new secondary containment door interlock system has

been installed since this incident and appears to prevent similar problem of

this nature, however; the licensee also committed to issuing a Outage Safety

Awareness Bulletin to discuss the importance of observing information signs

posted in various areas of the plant.

The inspector and the licensee could

find no Bulletin which addressed this subject. This was identified to the

Assistant Plant Superintendent as an apparent deviation from a commitment

(second example) (259/81-28-01, 260/81-28-01 and 296/81-28-01) on

September 14, 1981 an Outage Safety Awareness Bulletin was issued which

satisfied the licensee's commitment.

(Closed) Violation (259/81-06-01, 260/81-06-01 and 96/81-1b 01) Failure to

maintain secondary containment.

Open (259/80-02-03) Doorwatch to be sta-

tioned in secondary containment entry way to insure that secondary contain-

ment is not violated.

In June, 1981, the licensee installed a new secondary

containment door interlock system which is designed to prevent the opening

of two doors to the same airlock at the same time thereby losing secondary

containment. The new door interlock system is working satisfactorily.

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'(Closed) Violation (260/80-15-01) Failure to follow procedure. The in-

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spector reviewed the corrective action performed by the licensee and had no

questions.

(Closed) Deviation (259/80-43-01) Failure to revise administrative pro-

cedures on firewatches by date committed to. The inspector performed an in

office review ~of the licensee's response. Since this item was identified

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the inspector have noted no similar occurrences.

(Closed) . Violation (259/80-40-01) Failure to maintain adequate records.

The inspector monitored the recording of scram discharge header water levels

frequently after this event and found no futher instances of questionable,

recordings.

In January,1981, the manual system was upgraded to alarm in

the control . room, thereby _ voiding the necessity for 30 minutes level checks-

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by the auxiliary unit operator.

(Closed) Violation (260/80-29-01) No independent fire inspection performed

within three years. The inspector reviewed the corrective action taken to

prevent exceeding the three year audit requirement and found it to be

adequate at the time of the occurrence. Since then, the Technical Specifi-

cations have been changed to place the requirement for the fire audit under

the cognizance of the Nuclear Safety Review Board vice under a surveillance

requirement.

(Closed) Violation (260/80-29-02) Failure to follow procedure for core

verification. The inspector reviewed the corrective action taken by the

licensee and found it to be adequate. Since this event, no further problems

of this nature have been identified.

4.

Unresolved Items

There were no new unresolved items identified during this report period.

5.

Operational Safety

The inspectors kept informed on a daily bases of the overall plant status

and any significant safety matters related to plant operations.

Daily

discussions were held each morning with plant management and various member

of the plant operating staff.

The inspectors made frequent visits to the control room that each was

visited ~at least daily when an inspector was on site.

Observation included

instrument readings, setpoints and recordings; status of operating systems;

status and-alignments of emergency standby systems; purpose of temporary

tags on equipment controls and switches; annunciator alarms; adherence'to

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procedures; adherence to limiting . conditions for operations; temporary

alterations in effect; daily journals and data sheet entries; and control

room manning.

This inspection activity also included numerous informal

discussions with operators and their supervisors.

General plant tours.were conducted on at least a weekly bases. Portions of

the turbine building, each reactor building and outside areas were visited.

Observations included valve positions and system alignment; snubber and

hanger conditions; instrument readings; housekeeping; radiation area

controls; tag controls on equipment; work activities in progress; vital area

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controls;. personnel badging, personnel search and escort. Informal discus-

sion were held with selected plant personnel in their functional area during

these tours.

On August 22, 1981 at 3:20 a.m. a fire was discovered in the Unit 1 Reactor

Building underneath the tours on the 519 foot level. . The fire was extin-

guished by the fire brigade using a water hose and dry chemicals. The fire

was attributed to weid slag which smoldered in combustable material and did

not erupt into flames until af ter all craft personnel had left the area for

lunch.

The inspector investigated the cause of the fire and identified the fol-

lowing items which helped promote the occurrence of the fire:

(a) Poor housekeeping in the area of welding as combustable materials were

left around which was the main cause of the fire.

(b) The fire permit required two fire watches but only one was provided.

The single' fire watch informed his superior that he could not watch the

three areas where welding was occuring adequately, but; he was not

provided additional help.

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(c) Oxygen and acetalyne lines were not secured at the bottles during the

lunch break. The fire burned through the oxygen and acetalyne line

which then helped promote the spread of the fire.

TVA procedures

currently-require the securing of gas lines at their source only on

shift turnover. TVA has been asked to evaluate this requirement . in

light of this fire.

Prior to the fire, the single fire watch was required to observe three

different welding operations; bay 3, bay 11 and bay 16.

because of the

locations of the welding activities, the fire watch could only observe one

welding operation at a time. Technical Specification 3.11.H requires that a

continuous- fire watch shall be stationed in the immediate vicinity where

work involving open flame, welding or burning-is in progress on August 28,

1981, the assistant plant superintendent was was informed that having only

one fire watch for the three different welding operations in which the fire-

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watch could cnly . observe one operation was an apparent violation , of

Technical Specification 3.11.H. (259/81-28-02)

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While making a tour of Unit 1 reactor building on September 8,.1981, the in-

spector observed-a maintenance worker on the east. scram discharge header

(SDH). The inspector questioned the. foreman in charge of the job as to the

requirements of the SWP since the SDH area was posted as a high radiation

area.

The worker had no dose rate meter with him _ as observed by the

inspector.

.The inspector reviewed SWP 01-1-15285 which the workers

(maintenance man and foreman) used to sign in on for the work in the

vicinity of the east-SDH. The SWP was written specifically for the west SDH

only and required use of a dose - rate meter.

The workers signed in on an-

incorrect SWP and did not-use a does rate meter. No SWP was issued for work

in'the vicinity of the east SDH. The inspector immediately notified plant

staff. . Plant management was informed by the inspector on September 11,1981

that failure to have a _high radiation area controls by issuance of a SWP and

use of'a-dose rate meter was an apparent violation of -technical specifi-

cation 6.3.d.1 which requires entrance to a high radiation ' area be

controlled by issuance of a SWP and dose rate meter. (259/81-28-04) During

a tour of the Unit 2 reactor building on September 10, 1981, . the inspector

noted that weld permit no. 1748 fire prevention checkoff lists and certifi-

cation was not certified prior to welding in the vicinity of torus.griders 7

and 12. Plant management was informed that failure to provide fire preven-

tion certification prior to welding was an apparent violation of technical specification 6.3.A.10, failure to follow procedure as it relates to fire

protection and prevention (259/81-289-05).

Standard Practice 14.1 imple-

ments weld permit procedures of the DPM (Safety and Hazard'Contro! Manual -

procedure F 22).

6.

TMI Action Items

The following TMI action items were reviewed by the inspectors during this

report period. These items were due for implementation on July 1,1981.

a.

II.E.4.1.

Dedicatad Hydrogen Penetrations: The ' action item requires

the liensee to provide separate containment penetrations for the

containment atmosphere dilution system - to ensure single-failure

criteria. TVA's response dated July 16, 1981, states that some modifi-

cations to the system will be necessary to meet single-failure

criteria.

As of yet the final design has .not been approved. The

inspectors will continue to track this item.

b.

II.E.4.2.7. Closure of Containment Purge Valves on High Radiation:

The Browns Ferry primary containment isolation logic had the capability

of automatically isolating -'the containment purge valves when high

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radiation to sensed in the containment exhaust ducting. This item is-

considered closed.

c.

II.K.3.13. -Separation of High Pressure Coolant Injection (HPCI) and

Reactor Core Isolation Cooling (RCIC) Initiation Levels. TVA concurs

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with the Boiling Water. Reactor -(BWR) Owners' group recommendation that

the separation of HPCI and RCIC level setpoints' for auto start has no

substantial benefit so will not be performed. TVA is going to modify

the RCIC system to allow for auto restart to'the system. The schedule

for this modification is:

Unit 1 - 3/83 outage

Unit 2 - 3/82 outage

Unit 3 - 9/81 outage

The inspector will continue to track the modification progress.

d.

II.K.3.27. Common Reference Level: TVA's study of the proposed change

finds that the current vessel level indications are not confusing,

therefore, TVA does not plan on providing a common reference level.

This item will remain open for tracking purposes.

e.

I.C.5.

Feedback of Operating Experience. This item was previously

reviewed (IE Report 259, 260, 296/81-14) by the inspector and left open

for further verification of implementation by the licensee. A revised

division . procedure, DPM No. N72A39 was issued on July 28, 1981 to

-reflect the requirements of NUREG-0737. This in turn was implemented

at plant level by issurance of Standard - Practice 21.17, Review,

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Reporting, and Feedback of _ Operating Experience Items, September 9,

1981.

In addition provisions have been made for an annual audit of

this program by the Office of Power Quality Assurance staff. This item

is considered closed.

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In the above area, no violations or deviations were observed.

7.

Review of Plant Operations

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During this report period, the inspector conducted an inspection of the

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licensee's storage areas. ' This inspection consisted of:

a.

Verifying material and space parts are being received, inspected by

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qualified personnel and stored in accordance with licensee procedures.

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b.

Verifying non conforming items are marked / tagged,

c.

Verifying preventive maintenance on stored item was being performed.

d.

Verifying housekeeping and environmental requirements in store room

area was being met.

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Verified limited shelf-life items were controlled in accordance with

procedures.

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In addition the inspector verified traceability on selected safety related

item.

During this inspection the inspector identified food and drink being stored-

in the power stores main storage area and warehouse 3.

This is contrary to

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ANSI.N45.2.2-1972 which states that storage of food and drink in any storage

area will not be permitted.. On September 18, 1981,- the Plant Superintendent

was informed that this was an apparent violation of 10 CFR 50 Appendix B

Criteria XIII which require measures to control storage of material.

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' food and drink was immediately removed by the licensee from the warehouse

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storage. a rea s.

(259/81-28-06, 260/81-28-03 and 296/81-28-03)

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Unit 1 Refueling

The inspectors reviewed documentation and observed fuel handling operations

during the Unit I refueling outage. Upon completion of fuel loading quality

assurance verification of fuel assembly orientation and location was accom-

plished with satisfactory results. In addition, the inspector verified core

map position and orientation through video recordings taken after Unit 'l

fuel reload was completed. No discrepancies were noted.

9.

Surveillance Testing Observation

The inspectors observed the performance of the below listed surveillance

procedures.

The inspection consisted of a review of the procedure for

technical adeauacy, conformance to technical specifications, verification of

test instrument calibration, observation on the conduct of the test, removal

from service and return to service of the system and review of test data.

a.

SI 4.2.B.3, Instrumentation that Initiates or Controls CSCS Equipment

(Reactor Low Water Level)

b.

Mechanical Maintenance Instruction 19, Pumping Station Flood Protec-

tion, RHRSW pump, and Unwatering Pump Test (RHRSW pump rooms "A"

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"B")

c.

SI 3.3.1. A, Primary plant hydro

One deviation and one violation was noted during the observation and

procedural review of item b.

The inspector observed the conduct of MMI-19

on September 14, 1981. During the procedural reviews it was determined that

the approved procedural test requirements differed from the Final Safety

Analysis Report commitments.

Specifically, FSAR answer to question 2.6-5

states that each RHR service water pump will have operability demonstrated

during the flood test procedure. MMI-19' requires only eight of the twelve

RHRSW pumps to be checked for operability. In addition, the FSAR commits to

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a -flood test to the 18 inch level vice the' MMI-19 test requirements of 6

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inches. The two above mentioned discrepancies between FSAR commitments and

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actual procedural requirements is an apparent deviation.

Plant management

was informed of the apparent- deviation, on September 18,

1981.

(259/81-28-07, 260/81-28-04, 296/81-28-04)

A review of records indicated that the annual RHRSW pump operability test,

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compartment sump pump test, and the compartment leak rate tests were not

completed in 1978 or 1980. The compartment leak rate test for 1979 was

documented as invalid for compartments "C"

and "D"

and no record of re-

-schedule and satisfactory completion of the invalid portion of the test was

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available for review.

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The pump operability test, sump pump test, and leak rate test are required

to be completed annually in accordance with Mechanical Maintenance

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Instruction 19. This is an apparent violation of technical specification

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6.3.A as an example of failure to follow procedures. Plant management was

informed of the apparent violation (259/81-28-08, 260/81-28-05 and

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296/81-28-05) on October 2, 1981.

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10. Maintenance Observation

The inspectors observed the below listed maintenance activities for

procedure adequacy, adherence to procedure, and proper performance of the

maintenance.

a.

Repair / Installation of residual heat removal service water pump

discharge air relief valve.

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b.

Torus modification for Unit 1

c.

LPCI MG set installation for Unit 1

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No violations or deviations were identified in the above area. For further

discussion on item "a", refer to paragraph 12.

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11.

Reportable Occurrences

The below listed licensee event reports (LERs) were reviewed to determine if

the information provided met NRC reporting requirements. The determination

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included adequacy of event description and corrective action taken or

planned, existence of potential generic problems and the relative safety

significance of each event. Additional in plant reviews and discussion with

plant personnel as appropriate were conducted ~ for those indicated by an

. asterisk.

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LER'NO.

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Event

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'*259/81-43

7-25-81

Secondary containment 30-day

. report

  • 259/81-33

6-14-81

Primary containment leak rate -

  • 259/81-32

6/9/81

Reactor pressure switches out of

limits

259/81-41

7/22/81

Turbine building vent monitor

inoperable

260/81-36

7/7/81

- Smoke detector alarm

260/81-42

-8/3/81

Suppression chamber high level-

switches

296/81-33

7/6/81

3C diesel generator start relay

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  • 296/81-38

8/2/81

Valve 3-FCV-71-3 on RCIP. inoperable

In the above area no violations or deviations were identified.

12. -Flooding of Residual Heat Removal Service Water (RHRSW) Pump Room

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Onl August 22, 1981, the "A" RHRSW pump room was flooded to a level of 6

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feet which resulted:in the 3 RHRSW pumps in this room being made-inoperablec

(LER 259/81-47) The cause was attributed to failure of the air _ vacuum' val _ve

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associated with RHRSW pump ' A2 to properly seal after the pump _ was placed

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into operation. Water leakage past the valve exceeded the_ capacity of the

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two sump-pumps located in the room. The three RHRSW pumps were not damaged

although water was found.in-the pump oil.

Maintenance' tar performed on

transmitters which had been flooded to return them to operacie condition.

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The inspector reviewed the details of the flooding incident which included

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the history of maintenance on the air vacuum valves.

Their findings

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included the following:

a.

The air vacuum valves in service on the 12 RHRSW pumps were made by two

different manufactors, 6 by Valve and Primer Corporati.on (APCO)'and 6

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by Crispin Manufacturing. Both are float type valves where the float

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rises to seat against a rubber sealing material. The main difference-

is that the APC0' valves have floats with. guide tubes on the upper and

lower ends. '.The Crispin valve has a float weighted on one end and no

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. guide tubes.

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b.

Three of-the APC0 valves had the upper guide bar missing including the

valve ' assigned to pump A2.

The bar, about 3 inches in length, had

broken off at both ends.

From examination of the break surface, TVA

concluded that the bars had been missing for a long period of time.

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c.

Inspection verified that floats in valve with the~ upper guide bar

missing could come free from the lower guide and be subject to force

which _ caused varying ~ degrees ' of deformation.

Float seating was

adversely affected.

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d.

The maintenance record card for the valve associated with pump A2

revealed that the rubber valve seat was replaced on May 15, 1981 and

again on July 7,1981 to correct valve leakage. Valve maintenance over

the years has been performed by " skill of the trades" method without

the benefit of written procedures or manuals. There was no evidence

that personnel recognized during maintenance that the guide bar was

missing on some valves or if .they did that such a condition was

identified as a defective component.

e.

The practice that has been in existence is to rotate the ' float, with

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v .rbal concurrence of the vendor, on occasions where the top of the

-float is deformed and the bottom is not damaged and thus makes a better

sealing surface. Although the float is not symetrical TVA stated that

the vendor advised that it would function either way.

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f.

Attached to the side of the large air vacuum valve is a small air

relief valve to vent small releases of air during pump operation after

the large valve has seated. On some of the small valves the vents were

plugged and on others the vents were covered with insulation. The

determental affect of having these small valves inoperable was not yet

determined.

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The failed-valve from pump A2 has been sent to TVA metallurgical staff

for evaluation of the broken on missing guide bar and of a small

hairline crack observed at the base of the valve. A report of their

findings is planned.

h.

Another problem identified by TVA was that the flood switches in the

"A" room did not appear to function properly. A wiring error was found

which prevented the system from alarming at the 2 inch level. An alarm

that did come in during the room flooding was apparently initialed at

the 18 inch level when the transmitter for the level sensor was

flooded. There was no evidence that the switches had been tested since

they were installed in 1973.

The wiring error was corrected and an

annual test program was established.

The above findings revealed that there has been a history of air vacuum

valves failures with repeated float and seal damage occurring and of missing

upper guide- bars without adequate problem identification er corrective

action taking place until the recent flooding incident of August 22.

Another adverse finding was that the vents for some of the small

.r relief

valves had been plugged or covered with insulation.

Plant mana gen ant was

informed on October 2,

1981 that these adverse findings represented an

apparent violation (259/81-28-09, 260/81-28-06 and 296/81-28-06) of 10 CFR 50, Appendix B, Criterion XVI for failure to promptly identify and take

corrective action on conditions adverse to quality.

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-13.- - Reactor Trips

The inspector reviewed activities associated with the below list'ed _ reactor

trips during this report pe ri od.-

The review included determination of

cause, safety significance, ~ performance of personnel and systems, and

corrective action. The inspectors examined instrument recordings, computer

. printouts, ~ operations journal entries, scram reports and had discussions

~

with operations, maintenance and engineering support personnel as appro-

,

!

priate.

On August 22, 1981, Unit 3 tripped at 1:24 a.m. from 85% power due to main

steam -isolation valve (MSIV) closure during as surveillance test of main

steam tunnel high temperature switches.

Th'e problem was attributed to

faulty test circuitry which introduced a second extraneous'high temperature

signal which satisfied the logic to close the MSIVs.

Three main steam

relief valves were operated to control reactor pressure. No emergency core-

cooling systems were initiated. Required systems performed satisfactorily.

On August 23,1981, Unit 2 tripped at 2:01 a.m.

from 82% power during a

surveillance test of APRMs when one channel was placed in the standby

,

condition while the previous channel tested had not been returned to operate

-

which satisfied the - trip logic.

No emergency core cooling systems were

initiated. Plant safety systems operated satisfactorily.

On August 30, 1981, Unit 3 tripped at 1:49 p.m. from 97% power due to a

power load unbalance.

The cause was attributed to false operation of a

breaker failure relay in the 500 kV system which caused a voltage surge. No

relief valves were initiated nor were any emergency core cooling systems

initiated. Required systems performed satisfactorily.

On September 7, 1981, Unit 2 tripped at 12:02 p.m. from 90% power due to a

power load unbalance. A generator breaker underwent spurious opening which

produced the unbalance. The .cause of breaker operation was 'not determined.

RCIC was manually initiated but only operated for 1 minute. Required safety

systems performed satisfactorily.

On September 15,1981, Unit 2 tripped at 8:44 a.m. from 96% power due to

turbine trip which was caused by the loss of stator cooling. Stator cooling

pump "A" tripped due to a faulty overload relay and pump "B" was out of

service for seal maintenance. Both pumps were repaired before returning the

unit to the system.

HPCI and RCIC were manually initiated to control

reactor water level. Required safety systems performed satisfactorily.

'

Within the areas inspected no violations or deviations were identified.

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14. ' Emergency Drill

An emergency drill:to test the_ Brown Ferry radiological emergency plan was

conducted on September 9,

1981.-

The : drill ' involved wide- participation

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'

. including local, state and federal . agencies. The NRC emergency response

' team was dispatched from Region II for on . site observation and participation

'in the excercise. Details of the drill were reported in IE Report 259, 260,

and 296/81-24.

'

The three' resident inspectors reported to the- site after receiving telephone-

notification and instructions-from Region II. On September 11, 1981 one oft

the= inspectors attended the public meeting in Decatur, Alabama. Where -the

results of' the drill were discussed 'by members of the participating

agencies.

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