ML20035D933

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SALP Rept 50-285/93-99 for 910801-930130
ML20035D933
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 01/30/1993
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20035D934 List:
References
50-285-93-99, NUDOCS 9304140129
Download: ML20035D933 (22)


See also: IR 05000285/1993099

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INITIAL SALP REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION IV

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NUMBER

50-285/93-99

Omaha Public Power District

Fort Calhoun Station

August 1,1991, through January 30,1993

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TABLE OF CONTENTS

Page

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INTRODUCTION . . . . . . . . . . . . . . . . . . . . . .

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II.

SUMMARY OF RESULTS . . . . . . . . . . . . . . . . . . .

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III. CRITERIA . . . . . . . . . . . . . . . . . . . . . . . .

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IV.

PERFORMANCE ANALYSIS . . . . . . . . . . . . . , . . . .

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A.

Plant Operations . . . . . . . . . . . . . . . . .

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B.

Radiological Controls

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C.

Maintenance / Surveillance . . . . . . . . .

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D.

Emergency Preparedness . . . . . . . . . .

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E.

Security . . . . . . . . . . . . . . . .

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F.

Engineering / Technical Support

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G.

Safety Assessment / Quality Verification . . . . . .

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V.

SUPPORTING DATA AND SUMMARIES

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A.

Major Licensee Activities

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B.

Direct Inspection and Review Activities

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INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data on a

periodic basis and to evaluate licensee performance based upon this

information. The program is supplemental to normal regulatory processes used

to ensure compliance with NRC rules and regulations.

It is intended to be

sufficiently diagnostic to provide a rational basis for allocating NRC

resources and to provide meaningful feedback to licensee management regarding

the NRC's assessment of their facility's performance in each functional area.

An NRC SALP Board, composed of the staff members listed below, met on

February 26, 1993, to review the observations and data on performaace and to

assess licensee performance in accordance with NRC Manual Chapter 0516,

" Systematic Assessment of Licensee Performance."

This report is the NRC's assessment of the licensee's safety performance at

the Fort Calhoun Station for the period August 1, 1991, through January 30,

1993.

The SALP Board for Fort Calhoun was composed of:

Chairman

L. J. Callan, Director, Division of Radiation Safety and Safeguards (DRSS),

Region IV

Members

M. Virgilio, Assistant Director for Region IV & V Reactors, NRR

T. Gwynn, Deputy Director, Division of Reactor Projects (DRP), Region IV

A. Howell, Deputy Director, Division of Reactor Safety (DRS), Region IV

P. Harrell, Chief, Technical Support Staff, DRP, Region IV

R. Mullikin, Senior Resident Inspector, Fort Calhoun Station, DRP

S. Bloom, Project Manager, Fort Calhoun Station, NRR

The following personnel also participated in or observed the SALP Board

meeting:

C. Skinner, Intern, Technical Support Staff, DRP, Region IV

G. Hubbard, Acting Director, Project Directorate IV-1, NRR

L. Constable, Chief, Plant Support Section, DRS, Region IV

R. Vickery, Reactor Inspector, DRS, Region IV

D. Powers, Chief, Maintenance / Surveillance Section, DRS, Region IV

I. Barnes, Technical Assistant, DRS, Region IV

P. Baranowsky, Region IV Coordinator, Office of the Executive Director

of Operations

J. Pellet, Chief, Operations Section, DRS, Region IV

R. Azua, Resident Inspector, Fort Calhoun Station

B. Murray, Chief, Facilities Inspection Program Section, DRSS, Region IV

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SUMMARY OF RESULTS

Overview

Overall, licensee performance was good.

It was apparent that management's

priority was the safe operation of the facility. This was apparent both in

the conservative operability determinations made and the heightened awareness

of shutdown risks.

Performance in the Plant Operations functional area was

very good.

Significant improvements were noted in the quality of emergency

and abnormal operating procedures as well as the guidance provided to

operations personnel.

In addition, the number of licensed operators was

increased to an appropriate level. During an actual event that challenged the

operations staff and emergency response organization, the response was

excellent. However, the plant perturbations caused by personnel errors and

the loss of shutdown cooling indicated a need for increased management

attention in these areas.

Performance in the Radiological Controls area declined. Weaknesses in the

radiological protection program were identified due to two uptake events.

Overall, the radiation protection department had a good performance level.

Excellent performances were noted in the ALARA program, radioactive waste

effluents management, radiological environmental monitoring, transportation of

radioactive materials and wastes, training, and audits and surveillances.

Performance in the Maintenance / Surveillance area was good. However, oversight

of surveillance activities during refueling outages and nonsafety-related

maintenance activities that could impact safety-related systems may need

increased management attention.

Performance in the Emergency Preparedness area increased to an excellent level

as indicated by the response to an actual ALERT and during exercises, drills,

and walkthroughs with operating crews.

Performance in the Security functional

area was maintained at an excellent level.

Performance in the Engineering / Technical Support area was superior.

Examples

of the licensee's superior performance were the resolution of engineering

issues and the identification of design issues and the communication of these

issues to the NRC staff.

In addition, the systems engineering program was

notable.

Performance in the Safety Assessment / Quality Verification area was maintained

at a superior level.

Licensee management provided notable oversight of the

safe operation of the facility, except for the incident involving unauthorized

sampling of a liquid waste system.

Rating Last Period

Rating This Period

Functional Area

(05/01/90 to 07/31/91)

(08/01/91 to 01/30/93)

Plant Operations

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Radiological Controls

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Maintenance / Surveillance

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Emergency Preparedness

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Rating Last Period

Rating This Period

.Functional Area

(05/01/90 to 07/31/91)

(08/01/91 to 01/30/93)

Security

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Engineering / Technical

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Support

Safety Assessment /

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Quality Verification

  • I Improving Trend - Licensee performance was determined to be improving

during this assessment period.

Continuation of the trend may result in a

change in the performance rating.

III. CRITERIA

The evaluation criteria, category definitions, and SALP process methodology

that were used, as applicable, to assess each functional area are described in

detail in NRC Manual Chapter 0516, dated September 28, 1990.

This chapter is

available in the Public Document Room files. Therefore, these criteria are

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not repeated here, but will be presented in detail at the public meeting to be

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held with licensee management.

IV.

PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

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This functional area consists primarily of the control and execution of

activities directly related to operating the plant.

Evaluation of this functional area was based on routine inspections performed

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by the resident inspectors and six inspections performed by region-based

personnel.

In addition, the results from an Augmented Inspection Team were

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included in this assessment.

The previous SALP report (NRC Inspection Report 50-285/91-99) recommended that

management continue with the efforts that were already in progress for

increasing the number of licensed, on-shift operators and upgrading the

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emergency operating procedures.

In addition, it was recommended that

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operations management become more proactive in providing guidance and

direction to operations personnel.

During this assessment period, the licensee increased the number of licensed,

on-shift operators to an appropriate staffing level. Operations management

was proactive in its approach to providing guidance and direction to

operations personnel and, as a result, a previous concern with onshift

communications was appropriately addressed. The inspectors noted that the

licensee provided shift briefings before nonroutine activities and used the

simulator to provide operators with the expected plant response to potential

plant transients.

For example, a condition occurred in the plant that

resulted in the potential for the loss of a dc bus. The licensee used the

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. simulator to demonstrate how the plant would respond if the dc bus was lost in

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order to prepare operations personnel in the event that the plant transient

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occurred.

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It was noted, during the conduct of routine, day-to-day plant operations, that

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the operations staff maintained an excellent awareness of plant status and

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limiting conditions for operation in effect.

Excellent coordination and

communication between operations personnel and other groups was observed.

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Plant housekeeping was generally maintained at an excellent level, with some

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exceptions. Management personnel routinely toured all plant operating spaces.

The response by the on-shift operations staff to the July 3-4, 1992, stuck

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open pressurizer code safety valve, loss-of-coolant event demonstrated an

outstanding level of performance by the licensed operators for off-normal

events. The excellent response by the licensed operators ensured that this

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event did not result in a threat to the public.

Another on-shift licensee

crew was challenged by a similar, but less severe event on August 22, 1992,

and also responded very well.

Although overall operations personnel performance was excellent, there were

plant perturbations caused by personnel error.

An operator trainee caused the

generation of a containment isolation actuation signal during a surveillance

test when an override switch was not fully engaged. An operator trainee also

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caused an automatic start of Diesel Generator 2 after failing to synchronize

Emergency Diesel 1 to the bus during surveillance testing.

During the

refueling outage, an operator failed to put a reactor trip channel for low

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flow in bypass before shutting down a reactor coolant pump and, as a

consequence, a reactor trip signal was initiated. An operator inadvertently

started Emergency Diesel Generator 2 during the performance of a . surveillance

test by pushing the local start button instead of the alarm acknowledge button

at the local panel. Overpressurization of the steam generator blowdown system

occurred because of an oversight by licensed operators during the development

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of a equipment tagout. These events indicated a lack of attention to details

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by the operations staff.

The events initiated by operator trainees occurred

relatively early in this assessment period and the licensee has taken

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appropriate actions to address this issue.

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The Fort Calhoun Station experienced three automatic reactor trips during this

assessment period. One trip was due to personnel error when a level sensor

for a main steam reheater was incorrectly returned to service. This was the

first automatic trip since July 1986. The other two trips were due to

equipment malfunctions. The first resulted from the malfunction of a

nonsafety-related inverter and the second resulted from the f ailure of the

power supply for the electrohydraulic control system for the main turbine.

Operator training effectiveness and the relationship between the operations

and training organizations continued to improve during this assessment period.

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Operations management involvement in the operator licensing examination

process was evident.

This cooperative relationship resulted in a beneficial

teamwork approach to resolving training issues. The 100 percent pass rate on

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two sets of initial license examinations and on the requalification

examination demonstrated the licensee's commitment to improving licensed

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operator training.

The licensee made significant improvements in the content of the emergency and

abnormal operating procedures.

The procedures were well organized, logical,

and provided effective transitions to other procedures and attachments. The

Augmented Inspection Team credited the upgrade of the emergency operating

procedures as a contributing factor to the successful response to the

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July 3-4, 1992, stuck open pressurizer code safety valve, loss-of-coolant

event. The operators' knowledge and skills and the labeling of plant

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equipment were considered strengths. Good measures for configuration control,

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maintenance of the procedures, and training on the procedures were noted.

The operations staff's performance during the refueling outage was good. The

licensee implemented measures to reduce shutdown risk, which included the

installation of a temporary diesel generator, the policy to always have three

electrical sources available at all times, and to restrict midloop operations

to less than 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Despite these measures, a 7-minute loss of shutdown

cooling occurred because of the shutdown of the cooling pump. The electrical

system was in an abnormal lineup during the performance of a surveillance test

and an overloaded breaker caused the bus that powered the shutdown cooling

flow control valve controller and flow indication to be lost. Operators

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secured the running low pressure safety injection pump to prevent a possible

runout condition due to the flow control valve failing open.

The cause of the

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electrical system being in an abnormal lineup during surveillance testing was

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a lack of oversight by the licensee.

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At the beginning of the refueling outage, the licensee failed to implement

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adequate controls designed to preclude foreign materials from entering the

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refueling and spent fuel pool exclusion areas. After this concern was

identified by the NRC, it was immediately resolved by the licensee in a

satisfactory manner.

Fuel movement was performed efficiently and without an

incident. However, a weakness was noted in the use of visual and audio aids

to assist the refueling crew inside containment.

It was also noted that the

refueling crew did not always check the path of the refueling machine trolley

and bridge and formal guidance was needed concerning the control of suspended

irradiated fuel assemblies.

Licensee management generally made conservative equipment and component

operability decisions. When it became apparent in September 1991 that a

potential common-mode failure existed with the emergency station batteries

because of case cracking, the licensee shut down the plant and replaced the

batteries.

However, the licensee had prior indication in July 1991 that a

battery common-mode failure potential was present and failed to take actions

to address battery operability.

To reduce shutdown risk during the

replacement of the batteries, the licensee used the initial group of removed

batteries as a backup while new batteries were being installed.

The backup

batteries could have been manually connected to a dc bus if needed. An

example of conservative decisionmaking occurred when the licensee suspended

plant heatup from the refueling outage after cracked cam followers were

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discovered on 4160-volt breaker switches.

The critical switches were replaced

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before heatup continued.

In summary, overall performance in the area of plant operations was good.

The

licensee appropriately addressed all of the weaknesses that were identified in

the previous SALP report. The operating staff's performance was excellent,

both in day-to-day operations and response to events. The personnel errors

that resulted in plant perturbations demonstrated a lack of attention to

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details. Management involvement in plant operations was also excellent.

Management generally made conservative decisions in regard to safe plant

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operation, with the exception of battery operability. Operator training

effectiveness was apparent by the 100 percent pass rate on both initial and

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requalification examinations. The emergency and abnormal operating procedures

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showed significant improvement. The performance of the operations staff

during the refueling outage was good. However, a lack of oversight by the

licensee resulted in a loss of shutdown cooling.

2.

Performance Rating

The licensee is considered to be in Performance Category 2 in this functional

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area.

3.

Recommendations

a.

NRC Actions

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Review the licensee's outage management controls program during the next

scheduled refueling outage.

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b.

Licensee Actions

Improve controls over outage management and address the occasional lack of

attention by operations personnel.

B.

Radiological Controls

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Analysis

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This functional area consists primarily of activities related to radiation

protection, radioactive waste management, radiological effluent control and

monitoring, radiological environmental monitoring, and transportation of

radioactive materials.

This area was inspected four times by region-based radiation specialist

inspectors and on a continuing basis by the resident inspectors.

Excellent

performance was noted in this functional area during the previous assessment

period and no specific concerns or recommendations were identified.

During this assessment period, several violations were identified relating to

two uptake incidents that occurred during February and April 1992. The

violations involved improper implementation of the radiation protection

program, which included the failure to follow radiation protection procedures,

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. poor communications among radiation protection department personnel, and the

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lack of supervisory oversight. The violations were related to the specific

events and did not indicate a significant breakdown in the overall radiation

protection program.

The licensee's investigation and assessment of the uptake incidents were

excellent. The root cause analysis of each uptake incident was very good.

The investigation identified some minor weaknesses in the radiation protection

program that contributed to the violations. The corrective actions for the

uptake incidents and other events involving radiation protection were prompt,

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comprehensive, and conservative. The licensee's performance was excellent

regarding the difficult evaluation of transuranic radioactive radionuclides

involved in one of the uptake incidents.

Management provided excellent support for the radiation protection program.

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In general, radiation protection supervisory oversight of the day-to-day

activities was very good.

Radiological protection personnel were found to be

knowledgeable of their responsibilities and performed their duties in a

professional manner. Their efforts in support of plant activities during the

1992 refueling outage, following the loss-of-coolant event on July 3-4, 1992,

and activities related to the testing and removal of the pressurizer code

safety valves were excellent. A very good radiological occurrence report

program was implemented.

An excellent planning and preparation program was established for the 1992

refueling outage. An excellent inventory of radiation protection supplies and

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equipment was maintained for refueling outage activities.

Excellent

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coordination existed between the radiation protection department and other

departments.

External and internal radiation exposure controls were

implemented effectively.

High radiation and very high radiation areas were

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properly posted and controlled.

An excellent as-low-as-reasonably-achievable (ALARA) program was implemented.

The radiological protection department was proactive in the area of ALARA

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briefings, which were conducted prior to the performance of complex

maintenance and operational activities and/or when the potential for high

radiation exposure was present. The ALARA prejob briefings were thorough and

emphasized good radiological protection practices.

The ALARA suggestion

program was very good. The ALARA program looked for ways to reduce person-rem

exposures and personnel contamination events. The person-rem exposures for

1992 were about at the established goal, whereas the personnel contamination

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events exceeded the goal.

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An excellent liquid and gaseous radioactive waste effluent program was

maintained. Quantities of radionuclides released in liquid and gaseous waste

effluents, and radiation doses to the environment calculated from the effluent

releases, were within the Technical Specification and Offsite Dose Calculation

Manual limits. Semiannual radioactive effluent release reports were submitted

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in a timely manner and contained all of the required information presented in

the required format. One abnormal radiological gaseous release occurred

during this assessment period.

Changes to the Offsite Dose Calculation Manual

and process control program were documented properly. A good program was

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. established for testing the air cleaning systems.

It was noted that several

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of the effluent radiation monitors were out of service for extended periods of

time and, in some cases, the licensee's efforts to return the monitors to

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service have not been fully successful.

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An excellent radiological environmental monitoring program was maintained.

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The program was well managed and included very good implementing procedures.

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The environmental sampling stations and equipment were well maintained and

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calibrated. The environmental thermoluminescent dosimeter program was well

maintained and the thermoluminescent dosimeter results compared very well with

the NRC's thermoluminescent dosimeter results at collocated sites. Annual

radiological environmental operating reports were timely and contained the

required information.

Excellent solid radwaste and radioactive materials transportation programs

were maintained.

Excellent procedures for the preparation and shipment of

radioactive waste and other radioactive materials were in.glemented.

The

licensee properly characterized, classified, and prepared radioactive waste

for shipment and burial.

Radioactive materials and waste shipments were made

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without incident or problems.

Staffing was maintained at appropriate levels in the chemistry, radwaste, and

radiological services departments. Two supervisor positions had been open in

the radiation protection departments since mid-1992.

The various departments

experienced a very low turnover of technical personnel. The radiation

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protection staff was sufficient and appropriately supplemented with contract

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radiation protection technicians during outages.

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Excellent training and qualification programs were established and

implemented for personnel in this functional area. The radiological controls

area personnel were well trained and qualified.

Training instructors were

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well qualified.

Excellent coordination existed between the training

department and the various contributing departments that received training in

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this functional area. An excellent radiological training program was

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established for radiation workers.

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Excellent audits and surveillances were performed in the radiological controls

area.

The audits and surveillance identified several findings that were

reflective of an aggressive audit program. Corrective actions for the

findings were timely and technically sound.

The audit teams included

technical experts to review the specific program areas.

In summary, several violations were identified that involved the two uptake

events which occurred in early 1992. A thorough investigation was performed

by the licensee regarding the events and some weaknesses in the radiation

protection program were identified.

In general, the radiation protection

department maintained a good performance level. An excellent ALARA program

was maintained.

Excellent performances were noted in the areas of radioactive

waste effluents management, radiological environmental monitoring,

transportation of radioactive materials and wastes, training, and audits and

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surveillance.

Effluent monitors have been out of service for extended

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periods. Management provided strong support for the radiological controls

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2.

Performance Rating

The licensee is considered to be in Performance Category 2 in this functional

area.

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3.

Recommendations

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a.

NRC Actions

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Review in-plant implementation of the licensee's radiological protection

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program.

b.

Licensee Actions

Address filling of the vacant positions in the radiological protection

department, resolve the rerformance of effluent monitors, and resolve the

causes for the high numbers of contaminations.

C.

Maintenance / Surveillance

1.

Analysis

This functional area consists of activities associated with the preventive and

corrective maintenance of plant structures, systems, and components. This

area also includes the conduct of surveillance testing, and inservice testing

and inspection activities.

NRC inspection efforts consisted of routine inspections by the resident

inspectors and six inspections performed by region-based inspectors.

In the

last SALP report, no recommendations were made for overall program

improvement.

The maintenance program has undergone a number of improvements, which resulted

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in overall good physical appearance of the plant and in the good performance

of maintenance activities. The licensee continuously upgraded the preventive

maintenance program and optimized the program's approach. The maintenance

training program included a notable range of courses designed to familiarize

the maintenance staff with vital plant systems. As a result, the licensee

maintained a stable and well-qualified maintenance work force.

In addition, a

strong calibration program was developed and calibration scheduling was

effectively controlled to ensure compliance with program frequencies.

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Calibration procedures were exceptionally well written, detailed, and

comprehensive.

The inservice inspection program and implementing procedures were well written

and consistent with requirements of Section XI in the ASME Code. The repair

and replacement program provided appropriate instructions for controlling

repair and replacement activities and performing any required preservice and

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inservice inspection program examinations.

Observation of inservice

inspection program examinations and review of personnel certification records

indic<.ted that the nondestructive examinations were properly performed by

qualified personnel using qualified procedures.

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The f ort Calhoun Station experienced a reactor trip during this assessment

period that was directly related to the performance of a nonsafety-related

maintenance activity.

Reviews of the nonsafety-related activity did not

address the potential deleterious effects these activities could have on

safety-related activities. As a result, actions needed to eliminate the

potential were overlooked. Other maintenance errors identified during this

assessment period were found to have minor safety significance with no

programmatic concerns identified. The licensee took prompt actions to correct

identified maintenance deficiencies.

The implementation of the maintenance program by the licensee was very good.

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Maintenance activities were performed in accordance with approved procedures

and were well coordinated.

Preplanning of maintenance activities and

attention to detail by maintenance personnel were notable strengths, with very

good communication between maintenance personnel in the field and other

organizations. Management oversight of maintenance activities was excellent

throughout this assessment period, with supervisory personnel presence noted

during complex activities and periodically during the performance of more

routine efforts.

The systems engineering organization was actively involved in maintenance and

surveillance activities.

The oversight provided by the engineers helped to

ensure that the maintenance and surveillance programs were implemented in a

very good manner.

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The licensee's implementation of the surveillance program was noteworthy, with

one exception.

Because of a lack of oversight by the outage control center

during the performance of surveillance activities during the refueling outage,

shutdown cooling was lost due to an overloaded electrical bus.

Surveillance

tests were scheduled and performed as required by the Technical

Specifications.

Personnel adherence to surveillance procedures was excellent.

The Type B and C local leak rate test results were good.

Coordination among

surveillance, systems engineering, and operations personnel during testing

activities was very good.

In summarc performance in this functional area was good. The licensee has

been proa.tive and has taken actions to continually improve the maintenance

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program.

Procedural compliance was very good. Management oversight of this

functional area was notable. A loss of shutdown cooling resulted from the

lack of oversight during the performance of surveillance testing.

Plant

perturbations resulted from nonsafety-related maintenance activities.

2.

Performance Ratina

The licensee is considered to be in Performance Category 2 in this functional

area.

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Recommendations

a.

NRC Actions

None

b.

Licensee Actions

Perform an assessment of the effect that nonsafety-related maintenance

activities could have on safety-related systems and provide an appropriate

level of oversight of surveillance testing during refueling outages.

D.

Emergency Preparedness

1.

Analysis

This functional area includes activities related to the establishment and

implementation of the emergency plan and implementing procedures, onsite and

offsite plan development and coordination, support and training of emergency

response organizations, licensee performance during exercises and actual

events that test the emergency plans, and interactions with onsite and offsite

emergency response organizations during planned exarcises and actual events.

Evaluation of this functional area was based on the results of two inspections

conducted by regional emergency preparedness analysts and observations by the

resident inspectors.

The previous SALP report noted that management attention and aggressive

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actions should be taken to improve overall performance.

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During this assessment period, there were five actual emergency declarations.

Four of the declarations were classified as Notification of Unusual Events,

resulting from entering a Technical Specification shutdown action statement.

In all four of the cases, the licensee made timely classifications and offsite

notifications. On July 3,1992, an Alert was declared because of a

loss-of-coolant event. During this event, emergency response facilities were

activated and response personnel successfully implemented major portions of

the emergency plan and implementing procedures.

The Augmented Inspection Team

noted that the licensee's overall response during this event was excellent.

In addition to the effective response to actual classified events, the

licensee's emergency response organization demonstrated improved performance

during emergency drills and the 1992 emergency exercise. During the exercise

and drills, NRC evaluators and observers noted efficient and effective

implementation of the emergency plan and implementing procedures.

Implementation of abnormal and emergency operating procedures by the

operations staff was very good.

Emergency command and control was excellent

and technical assessment and mitigation efforts were strong.

During the

exercise, operational support personnel performed well as d improvements were

noted in the exercise of radiological controls during emergencies. The

exercise scenario was run using the control room simulator in the dynamic mode

to enhance challenge and realism. One minor exercise weakness was identified

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during the 1992 exercise involving the failure to make prompt emergency

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classification of conditions corresponding to a Site Area Emergency.

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Emergency training drills exceeded requirements in both number and scope.

For

example, a casualty control drill, not required by the NRC, was held to

provide enhanced training for maintenance personnel assigned to the Operations

Support Center staff.

The licensee's exercise and drill critiques were

effective in identifying areas in need of corrective action.

The operational status inspection found that changes to the emergency plan

were generally reviewed and submitted to NRC in an appropriate manner.

Emergency facilities, equipment, and supplies had been maintained in a state

of operational readiness. An appropriate level of staffing had been

maintained for the emergency response organization and an excellent program

had been implemented to train and maintain the proficiency of these response

personnel. Comprehensive and effective audits of the emergency preparedness

program had been performed.

The licensee maintained a cooperative and supportive working relationship with

offsite response organizations. The Federal Emergency Management Agency did

not evaluate the 1992 exercise; however, they did evaluate an unannounced /off-

hours drill and a medical drill involving offsite agencies. No deficiencies

were identified during the drills.

In walkthroughs conducted with shift crews during the operational status

inspection, the three teams evaluated demonstrated excellent proficiency in

implementing the emergency plan and implementing procedures in response to a

rapidly escalating scenario. All simulated events were properly classified.

Timely and accurate notifications were made to offsite authorities.

Dose

assessments and protective action recommendations were based on plant

conditions and were appropriate.

In summary, licensee management and staff continued to improve the emergency

preparedness program.

Efforts produced excellent results in key emergency

preparedness areas. The excellent training provided to emergency response

organization personnel was evident during exercises, drills, and walkthroughs

with operating crews. The performance of the emergency response personnel

during the Alert was excellent. The emergency preparedness program has been

effectively managed.

2.

performance Rating

The licensee is considered to be in Performance Category 1 in this functional

area.

3.

Recommendations

None

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.E .

Security

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1.

Analysis

This functional area includes activities that ensure security of the plant,

including all aspects of access control, security background checks, and

protection of safeguards information.

Evaluation of this functional area was based on the results of two inspections

performed by region-based physical security specialist inspectors and routine

observations by the resident inspectors.

In addition to the normal regional

inspections, a special Operational Safeguards Response Evaluation was also

performed during this assessment period.

l

The previous SALP report noted a strong and effective security program. No

specific recommendations were included in the previous report.

During this assessment period, one repeat Severity Level III violation was

identified involving the protection of safeguards information.

The licensee

took effective corrective actions, with substantial programmatic changes made

with respect to the handling of safeguards information. Overall, the

enforcement history was good during this assessment period.

Management continued to provide strong support to ensure that an effective

security program was maintained. Management was actively involved in

day-to-day activities and provided excellent oversight of the implementation

of the security program.

Quality assurance audits of the security program were thorough, performance

oriented, and comprehensive. The audits of the self-screening contractors

were very comprehensive and identified several problems with contractor

programs. The security organization provided timely, effective, and

technically correct responses to the audit findings and recommendations.

<

The testing and maintenance program was effective in ensuring that security

systems were maintained operational. Testing personnel were well trained and

allowed to use their initiative when testing the security systems.

The licensee submitted four Physical Security Plan revisions pursuant to

10 CFR Part 50.54(p) that involved significant changes to their program.

The

changes were in compliance with the requirements of Part 50.54(p).

The licensee had an appropriate number of security force personnel assigned to

normal shifts. During the 1992 refueling outage, prior planning by the

security management staff resulted in a significant reduction in overtime

hours, when compared to previous outages.

The security training program was very effectively administered and

implemented. Training records were well maintained.

Excellent training

facilities and training aids were maintained and used. A new weapons training

range was constructed and effectively used.

In preparation for the

Operational Safeguards Response Evaluation inspection, tactical training was

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emphasized and the excellent results indicated the effectiveness of the

training. During this evaluation, the security force demonstrated the ability

'

to bring sufficient response assets to bear quickly and effectively against

simulated armed intruders. The Operational Safeguards Response Evaluation

pointed out that there exists a strong security management team that was

involved in and supportive of the security program. The security forces

demonstrated an effective contingency response capability and a strong

defensive strategy. Another positive element of the response capability was

the command, control, and communications.

The overall results of the

Operational Safeguards Response Evaluation inspection was evidence of a well-

motivated and well-trained security force.

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In summary, the licensee had maintained an excellent security program. The

security organization was appropriately staffed with well trained officers.

The security management staff was proactive, professional, and received

excellent management support from plant and corporate management. The results

of the Operational Safeguards Response Evaluation were indicative of a strong

security program.

1

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2.

P_ftrformance Ratinq

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The licensee is considered to be in Performance Category 1 in this functional

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area.

3.

Recommendations

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None

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F.

Engineering / Technical Support

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1.

Anal ysis

This functional area consists of technical and engineering support for all

plant activities.

It includes all licensee activities associated with the

design of plant modifications; engineering and technical support for

operations, outages, maintenance, testing, surveillance, and procurement

activities; training; and configuration management.

NRC inspection efforts consisted of routine inspections by the resident

inspectors and seven region-based inspections.

The inspection effort included

team inspections to assess the motor-operated valve progrcm, as specified in

Generic Letter 89-10, " Safety-Related, Motor-0perated Valve Testing and

Surveillance," and engineering and technical support functions.

The previous SALP report did not address any recommendations.

Enforcement

history during this assessment period was excellent.

The licensee's engineering organization continued to be proactive in the

identification and resolution of engineering issues.

For example, the

licensee reviewed information supplied by the NRC concerning a potential

safety issue at another facility. This resulted in the discovery that

backleakage could occur through the safety injection and refueling water tank

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discharge check valves during the recirculation phase. This could have

allowed radioactive water to enter the tank, which is vented to atmosphere.

The licensee's prompt evaluation of this concern allowed the valves to be

replaced during the 1992 refueling outage.

The systems engineering program generally continued to function well. One

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example was the discovery that a personnel access lock equalizing valve had

never been leak rate tested.

Systems engineering was also involved in the

discovery that cam followers on certain safety-related switches were

susceptible to cracking.

The system engineer's performance in day-to-day

activities was excellent.

They were observed to be actively involved in all

activities associated with their system. The system engineers' performance

with regard to surveillances and maintenance was excellent.

However, the

,

systems engineering organization was responsible for inappropriately taking

reactor coolant drain tank samples, resulting in the loss of containment

integrity. This sampling was performed without the use of an approved

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procedure.

In addition, in response to a problem that involved battery case

cracking, a root cause analysis indicated that a potential common-mode failure

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existed. This root cause analysis did not receive timely attention and action

by plant management.

The licensee's design basis reconstitution program continued tc identify items

that were outside the plant's design basis.

The identification of design

issues and the communication of these issues to the NRC staff was considered

superior.

The engineering organization's response to plant events and other complex

activities was superior.

The engineering organization performed well during

the refueling outage with support for the reactor vessel thermal shield

inspection and repair, reactor vessel inservice inspection, steam generator

eddy current testing, ultrason4 testing of de off-loaded fuel, emergency

battery replacements, and the u.;tallation of a temporary diesel generator.

However, in response to the loss of shutdown cooling, engineering provided

incorrect procedural guidance to limit the 480-volt bus loading. The result

was a subsequent loss of three 480-volt busses.

This was considered an

isolated occurrence.

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The licensee's initial efforts in developing a program in accordance with its

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commitments to Generic letter 89-10 was generally good. Some weaknesses were

identified in the licensee's program, but these weaknesses were typical of

those found throughout industry, and no operability concerns were identified.

The licensee maintained a competent nuclear engineering staff with notable

in-house computing and reload safety analysis capabilities.

The licensee's

nuclear engineering staff was assertive in maintaining cognizance of fuel

performance and potential adverse impacts, as evidenced by the requirement

that all proposed changes to fuel assembly design be reviewed and approved by

the licensee prior to implementation in the reload batch. The licensee's fuel

examination activities and first-time application of a fuel assembly

reconstitution process were successful and performed without encountering any

significant problems.

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3he licensee developed and implemented an effective program to control design

changes, modifications, and temporary modifications in accordance with the

Technical Specifications, Updated Safety Analysis Report, and regulatory

requirements.

The licensee's process for the performance of safety

evaluations was considered to be exceptional.

For example, the number of

active temporary modifications was relatively few and those that were in

effect were properly implemented.

The implementation of plant modifications was considered good. The

modifications to the electrical power system for the electrohydraulic control

system were implemented in a timely manner and should improve the reliability

of the facility. The licensee's analysis for the revision to the high

pressurizer pressure reactor trip and pressurizer power-operated relief valve

setpoints following the loss-of-coolant event provided an appropriate basis.

The prompt implementation of the modification to readjust these setpoints was

found to be commendable.

The licensee's calculations and evaluations related

to the electrical distribution system were noteworthy.

The replacement of two

safety injection and refueling water tank valves was properly implemented.

Engineering management's oversight of the engineering organization's

involvement with safety issues continued to be superior. Design Engineering

interfaced well with their site contacts and system engineering.

Communication between the engineering departments and the rest of the plant

organization was very good.

The staffing levels were considered to be

consistent with the workload. The design basis documents and user friendly

procedures were found to be a positive influence on design engineering job

performance. The licensee had identified several strategic engineering

initiatives.

For example, the licensee initiated actions to enhance steam

generator reliability, plant reliability,- and outage planning and control.

These initiatives were commendable.

The system engineer training program was a strength in the development of an

effective system engineering program. The system engineer's coordination of

activities related to their assigned systems was viewed as superior.

The

system engineers had developed very good credibility and working relationships

throughout the licensee's organization.

There was a strong sense of ownership

of systems by the system engineers.

The training department's performance in operator training was very good.

This was evident in the 100 percent pass rate on two sets of initial licensee

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examinations and the requalification examination.

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In summary, the licensee's overall performance in this functional area was

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superior. The licensee's engineering organization continued to be proactive

in the resolution of engineering issues.

The systems engineering program was

notable.

Some engineering problems were considered isolated cases and not

indicative of a programmatic problem. The identification of design issues and

the communication of these issues to the NRC staff was considered superior.

Engineering made significant efforts to resolve ongoing issues.

Engineering

management's oversight of the engineering organization's involvement with

safety issues continued to be excellent. The licensee maintained a competent

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nuclear engineering staff with notable capabilities.

The licensee developed

and implemented excellent programs for design changes, modifications, and

temporary modifications.

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2.

Performance Rating

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The licensee is considered to be in Performance Category 1 in this functional

area.

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3.

Recommendations

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None

G.

Safety Assessment /0uality verification

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1.

Analysis

This functional area includes licensee activities associated with the

implementation of licensee safety policies; licensee activities related to

<

amendment, exemption, and relief requests; responses to generic letters and

bulletins; the resolution of safety issues and performance of safety

evaluations; safety committee and self-assessment activities; licensee

activities related to the identification and resolution of equipment and

programmatic problems; and licensee activities associated with quality

verification functions.

,

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NRC inspection efforts in this area consisted of the core inspection program,

regional initiative inspections, and NRR program reviews. The previous SALP

report did not identify any recommendations in this functional area.

The licensee's commitment to safety was evident during the refueling outage.

]

A control center was formed as the central coordinating body for the outage,

which had the overall, day-to-day responsibility for outage activities.

Two

assistant plant managers were appointed as outage managers. The outage

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control center assumed responsibility for as much of the routine control room

outage activities as possible.

However, equipment taken out of service

continued to require control room approval.

A definite focus on reducing

shutdown risks was prevalent, as exemplified by the installation of a

temporary diesel generator as an additional power supply.

The outage control

center performed excellently throughout the outage, except for one instance

where a surveillance test of the safety injection pumps was performed a day

earlier than scheduled.

As a result, shutdown cooling was lost for

approximately 7 minutes. This event was considered an indication of a

programmatic weakness with outage planning and control.

Overall, the

performance of the licensee during the refueling outage was very good.

The Nuclear Safety Review Group was effective in carrying out its charter, as

evidenced by the group's involvement in major events and issues. A notable

characteristic of the Nuclear Safety Review Group was its timeliness in

addressing issues and issuing findings or recommendations. The Quality

Assurance organization initiated a functional area trending program, which

identified weaknesses or concerns. The issues identified by this process were

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resolved in a timely manner. A good working interface was found between the

Nuclear Safety Review Group and Quality Assurance.

These groups provided good

support to the Safety Audit and Review Committee. The Quality Assurance and

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Nuclear Safety Review Groups' overview of engineering activities were

considered a strength.

The onsite and offsite committees were effective in the identification of

issues. The onsite Plant Review Committee was proactive in assessing the

adequacy of proposed corrective actions.

The nuclear planning organization

was engaged in a process of identifying strategic issues, such as steam

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cenerator reliability, or issues with long-term or future implications, such

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as the installation of a third permanent offsite power source. The majority

of these strategic issues are safety-related.

Quality control personnel were

noted in the plant on numerous occasions.

Excellent communication and

coordination was apparent between the quality control inspectors and plant

personnel.

The licensee has expended significant resources in the upgrade of all plant

safety-related and nonsafety-related procedures. As a result of these

efforts, the procedures provide concise and effective instructions for the

performance of tasks.

The quality of plant procedures was generally excellent

based on the licensee execution of the procedures. On occasion, minor

inconsistencies were noted in the procedures, but personnel involved backed

out of the procedures and obtained clarification before recommencing the

ongoing evolution.

The licensee has been proactive in the identification and correction of

problem areas. The licensee continued to exert a strong effort toward the

identification of problems related to safety and conditions adverse to

quality. An assessment of the licensee's corrective actions in response to

'7

inspection findings and licensee event reports revealed that the actions were

thorough, proper, and timely,

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A review of recent changes revealed innovative enhancements to the programs

for root cause analysis and the investigation of human performance related to

specific events. Human performance evaluation had evolved to the point where

investigations were performed by a team staffed by members from nonrelated

disciplines. All root cause analyses were performed by the system engineering

group.

The actions resulting in the violation of containment integrity was an example

where licensee management failed to exercise control over certain plant

activities. The incident, where a liquid sample was taken from a drain valve

(WD-1060) that was located between two containment isolation valves, was

significant due to the number of occurrences and the nonquestioning attitude

of those plant personnel that were aware of the activity. The sampling was

allowed to be done without the use of an approved procedure, nor was the

evolution approved for performance by the operations staff.

During this assessment period, the NRR staff reviewed a large number of

license amendments and safety analyses performed by and for the licensee.

Generally, the licensee's submittals demonstrated a clear and concise

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understanding of the NRC guidance and concern and positively showed a

management that was extremely involved in the licensing process.

The

submittals were generally technically competent, unambiguous, and complete.

However, in some cases, additional information was required to complete the

review. Occasionally, technical staff's responses to questions were

inconsistent with prior submittals or the NRC staff had to explain the

question. On several submittals, the licensee's review process failed to

detect mistakes involving either the technical information or the writeup

explaining the information. The licensing department initiated an additional

level of review, but a subsequent submittal showed that the review process

still needed improvement.

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During a 10 CFR Part 50.59 package review, the NRC staff found that the

licensee's evaluations were well prepared and well documented.

Multidiscipline issues were addressed and included a review by engineers from

various discipline groups. The affected sections of the Updated Safety

Analysis Report were clearly identified and the safety evaluations addressed

the potential safety concerns, including the Part 50.59 issues related to

unreviewed safety questions.

The review also found that a screening criteria

and Part 50.59 reportability analysis existed if needed to process temporary

modifications.

There have been four waivers of compliance issued to the licensee during this

assessment period.

The waivers dealt with the opening of the outer personnel

air lock door, to perform repairs, and the performance of a steam generator

inservice inspection following a loss-of-coolant event. The waivers requested

by the licensee were thorough and complete.

'

Licensee management has provided an excellent level of oversight for the safe

operation of the facility. Management and the licensee's staff demonstrated

their capabilities when challenged by abnormal and emergency situations.

Through management's and the staff's participation in industry working groups,

they have effected changes in the facility operation based on their awareness

of problem areas that are being identified at other facilities. Management's

strong oversight of plant operations is due, in part, to their familiarity

with the operation of the facility since all personnel in the line management

function, up to and including the Senior Vice President, are former plant

managers.

Overall, licensee management provided notable oversight of the safe operation

of the facility, except for the incident involving unauthorized sampling of a

liquid waste system. The licensee's independent oversight organizations were

actively involved in ensuring that facility operations were performed in a

safe manner.

Licensee submittals made by the licensee were technically

competent, unambiguous, and complete; however, some submittals required NRC

staff assistance or were not consistent. The licensee's root cause analysis,

Part 50.59 program, human performance evaluation system, and corrective action

programs were excellent.

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2.

Performance Rating

The licensee is considered to be in Performance Category 1 in this functional

area.

3.

Recommendations

None

V.

SUPPORTING DATA AND SUMMARIES

A.

Major Licensee Activities

1.

Major Outages

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September 1991 - Replacement of station batteries

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February 1992 - Refueling outage

July 1992

- Loss-of-coolant event

August 1992

- Premature lifting of a pressurizer code safety valve

2.

License Amendments

Eleven license amendments were issued during this assessment period.

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B.

Direct inspection and Review Activities

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NRC inspection activity during the assessment period included 40 inspections.

Approximately 4500 direct inspection hours were expended, which did not

include operator licensing examinations or contractor hours.

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