ML20031C629
| ML20031C629 | |
| Person / Time | |
|---|---|
| Site: | Big Rock Point File:Consumers Energy icon.png |
| Issue date: | 06/08/1979 |
| From: | Himebauch N CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | |
| Shared Package | |
| ML20031C626 | List: |
| References | |
| NUDOCS 8110070367 | |
| Download: ML20031C629 (4) | |
Text
_ - _ - _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ _
OPERATING DATA REPORT DOCKET NO.
50-155 l
DATE 6/8/79 COMPLETED BY NHimebauch TELEPHONE fLIFs47-6537 X A80 OPERATING STATUS Notes
- 1. Unit Name:
Bic Rock Point Plent NeaQ Q ruh MSV 1970 vessel internals have been
- 2. Reporting Period:
2h0 removed to facilitate
- 3. Licensed Thermal Power (MWt):
75 CRD Housing Leakage and
- 4. Nameplate Rating (Gross MWe):
72 vessel hardware vibration
- 5. Design Electrical Rating (Net MWe):
67 repairs.
- 6. Maximum Dependable Capacity (Gross MWe):
63
- 7. Maximum Dependable Capacity (Net MWe):
- 8. If Changes Occur 4 7.apacity Ratings (Items Numt,er 3 Through 7) Since L.ast Report.Give Reasons:
- 9. Power Level To Which Restritted.If Any (Net MWe):
67 Drvout Time
- 10. Reasons For Restrictions.If Any:
(
This Month Yr to Date Cumulative 7hh 0 7699.0 1hl.786.0
- 11. Hours In Reporting Period 0.0 778.1 98,goh,g
- 12. Number Of Hours Reactor Was Critical 0
0 0
- 13. Reactor Reserve Shutdown Hours U*U 773 7 96,710 7
- 14. Hours Generator On-Line 0.0
- 15. Unit Reserve Shutdown Hours 0.0 136,006.4 17,656,416.9
- 16. Gross Themial Energy Generated (MWH) 0.0 42,010.0 5,657.062.0
- 17. Gross Electrical Energy Generated (MWH) 0.0 39,335 1 5,353,996.4
- 18. Net Electrical Energy Generated (MWH) 0.0 21.4 68.2
- 19. Urit Service Factor 0.0 21.4 60.2
- 20. Unit Availability Factor 11 2 55 5 n.n
- 21. Unit Capacity Factor (Using MDC Net) 1>*1
>d.4 00
- 22. Unit Capacity Factor (Using DER Net)
>c.2 ly.g
- 23. Unit Forced Outage Rate 100,;
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Fachl:
Sent-her 1_ 147Q
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units In Test Status (P ior to Commercial Operation):
Forecast Achieved INITIA L CRITICALITY INITIAL ELEGRICITY COMMERCIAL OPERATION k
O PDR
s UNITSHUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-155 UNIT NAME Bic Rock Point DATE 6/8/70 REPORT MONTH liay 1979 COMPLETED BY NHimebauch TELEPHONE 616-5h7-6537 x 180 "E
e r.
.5 ui 5"
Licensee E*
E _e E
g.5 X g ".,
Cause & Corrective No.
Date g
3g
,, g 5 Event uT N0 o.b Action to
$E 5
j di y Report
- Prevent Recurrence i
S SHUTDOWN CONTINUED FROM APRIL 197 >
3 5/1/T9 -
F Thb.0 A
3 Reactor tripped on high pressure due
',o 5/31/79 79-018 CA ZZZZZ fact turbine bypass valve failed to c aen RA ZZZZZ on h/17/79 - subsequently discovered, during testing, a CRD housing leak an 1 vibrating hardware in the reactor ves Jel.
(These comments previously reported o 1 April report)
I 2
3 4
F: Forced Reason:
Method:
Exhibit G. instructions S: Scheduled A Equipment Failure (Explain)
- 1. Manual for Preparation uI Data B Maintenance of Test
- 2. Manual Scram.
Entry Sheets for Licensee C-Refueling 3.Autunutic Scram.
Event Report (LER) File (NUREG-D-Regularory Restriction 4Deher (Explain) ul6II E-Operator Training & Ucense Examination F Administrative 5
G-Operational Error (E xplain)
Exhibit I - Same Source (9/77)
Il-O her(Explain)
s A\\ ERAGE DAILY UNIT PO'YER LEVEL
+
DOCKET NO.
50-155 UNIT Big Rock Point J m 8, 1979 DATE lulimebauch COMPLETED BY TELEPHONE 616-Sh7-6537 x 180 MONTH May 1979 DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe-Net)
(Mwe. Net)
I I7 2
18 3
39 4
20 f
5 21 22 W
6
)~
I.
7 23 I
C 8
24 d
F 9
23 N
10 26 v
i!
O 27 o
t i2
,8
~
L 13 29 14 33 15 3
I6 INSTRUCTIONS On this format list the average dady urut power level in MWe Net for each day in the reporting month. Compute to the nearest whole rnegawatt.
(4/77) s
May 1979 Refueling Information Request 1.
Tacility name:
Big Rock Point Plant Scheduled date for next refueling shutdown:
2.
In Progress Scheduled date for restart following shutdown:
3.
September 1979 Will refueling or res.umption of operation thereaf ter require a technical 4.
specification change or other license amendment?
NO If yes, explain.
i If no, has the reload fuel design and core configuration been reviewed 1
by Plant Safety Review Committee to determine whet M
If no review has taken place, when is it scheduled?
I Scheduled date(s) for submittal of proposed licensing action and 5.
supporting information:
4 N/A Important licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance ana-1 6.
lysis methods, significant changes in fuel design, new operating procedures:
N/A 1
170
- spent fuel storage pool core 0
7.
Number of fuel asse$blies in; Present licensed spent fuel storage capacity:
193 8.
Size of any increase in licensed storage capacity that has been requested or f-is planned (in number of fuel assemblies):
2kB Projected date of the last refueling that can be discharged to spent fuci 9.
pool assuming the present licensed capacity:
1983
- - - - -... _ _, _. _, _.. _, _.... -, _. -. _ _ _... - _..., _... _ _ _,.. _ _, _ _ _ _ _ _ _, _. _ _ _ _ _. ~..