ML20030C357

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Interim Deficiency Rept Re GE Motor Control Ctrs That Contain Varglas Wire Tire Matl Which May Unravel & Cause Loss of Support,Initially Reported 810624.GE Corrective Action Plan Not Yet Received
ML20030C357
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 07/21/1981
From: Van Brunt E
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To: Faulkenberry B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
10CFR-050.55E, 10CFR-50.55E, ANPP-18455-JEC, NUDOCS 8108260016
Download: ML20030C357 (3)


Text

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i 50.55(e) Report

,t Docket Nos. 50-528/529/530

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PHOENIX, ARIZON A 85036

p. o. sox 21666 ANPP-18455-JEC/BSK[h',D';,Q July 21, 1981 4

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U. S. Nuclear Regulatory Commission co7 2 ?T Region V r"

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Walnut Creek Plaza - Suite 202

.h s 1990 North California Boulevard S

Q Walnut Creek, California 94596 ep p Attention:

Mr. B. H. Faulkenberry, Chief g.

g Reactor Construction and y

j[e Engineering Support Branch y

Subject:

Interim Report A 50.55(e) Potentially Reportable Deficiency! Relating to GE Motor Control Centers That Contain "Varglas" Wire Tie Material Which May Unravel and Cause a Loss of Support File: 81-019-026 D.4.33.2

Reference:

Telephone Conversation between J. Eckhardt and B. S. Kaplan on June 24, 1981 (DER 81-18)

Dear Sir:

I j

The NRC was notified of a potentially reportable deficiency in the referenced telephone conversation. At that time, it was estimated that a determination of reportability would be made within thirty (30) days.

Due to the extensive investigation and evaluation required, an Interim Report is attached.

It is now expected that this informa-tion will be finalized by December 15, 1981, at which time a complete report will be submitted.

Very truly yours, i

CLM

/1 til E. E. Van Brunt, Jr.

APS Vice President Nuclear Projects ANPP Project Director EEVBJr/JEC:skc 3

Attachment f/

8108260016 810721 PDR ADOCK 05000528 S

PDR sl-131

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U. S. Nuclear Regulatory Commission Attention:

Mr. B. II. Faulkenberry, Chief ANPP-18455-JEC/BSK July 21, 1981 Page 2 cc: Victor Stello, Jr., Director i

U. S. Nuclear Regulatory Commission

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Office of Inspection and Enforcement Washington, D. C.

20555 A. C. Gehr Snell & Wilmer R. L. Robb D. B. Fasnacht W. E. Ide A. C. Rogers J. M. Allen B. S. Kaplan J. A. Brand W.11. Wilson W. G. Bingham W. J. Stubblefield R. L. Patterson R. W. Welcher D. R. llawkinson Ms. Patricia Lee Hourihan 6413 South 26th Street Phoenix, Arizona 85040 Mr. M. A. Kiffer General Electric Company 5320 North 16th Street Phoenix, Arizona 85016 1

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INTERIM REPORT i

POTENTIAL REPORTABLE DEFICIENCY j

ARIZONA PUBLIC SERVICE COMPANY (APS)

PVNGS UNITS NO. 1 AND 2 l

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Potential Problem During a Bechtel witnessed test of a General Electric Class IE Motor Control Center at Mebane, North Carolina, a test failure was documented on March 27, 1981, which was caused by a piece of "Varglas" wire tie material becoming lodged between N.O. contacts of Relay FX

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(Points 7 and 8 on Drawing 221B5925). This prevented relay contacts from closing when the relay was energized.

A follow-up surveillance was completed for the related GE equipment delivered to the jobsite. This activity found that the "Varglas" wire ties were loose on wiring bundles and found in the bottom of the MCC panels. The following Nonconforma..ce Reports have been issued to identify these conditions as follows:

NCR MCC Tag Numbers E-J-1094 1E-PRA-M31 and 1E-PHB-M32 E-J-1095 2E-PHA-M31 and 2E-PHB-M32 E-A-106 2E-NHN-M20 (Non-Class IE)

I II.

Approach To and Status Of Proposed Resolution-Bechtel has contacted GE regarding these conditions, but has not yet received their evaluation and corrective action plan.

III.

Projected Completion of Corrective Action and Submittal of the Final Report Y

l The evaluation, resolution and Final Report are forecast to be completed by December 15, 1981.

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