ML20029D126

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Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-245/93-16, 50-336/93-11 & 50-423/93-13
ML20029D126
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 04/26/1994
From: Lanning W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Opeka J
NORTHEAST NUCLEAR ENERGY CO.
References
NUDOCS 9405040063
Download: ML20029D126 (3)


See also: IR 05000245/1993016

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APR 2 s 19y

Docket Nos. 50-245; 50-336; 50-423

,

Mr. John F. Opeka

Executive Vice President - Nuclear

Northeast Nuclear Energy Company

P. O. Box 270

Hartford, Connecticut 06141-0270

Dear Mr. Opeka:

SUBJECT:

COMBINED INSPECTION REPORTS 50-245/93-16; 50-336/93-11;

50-423/93-13

This letter refers to your September 10, 1993, correspondence, in response to our July 22,-

1993 letter.

In your response to the Notice of Violation regarding failure to restore the reactor building

closed cooling water radiation monitor to service properly following surveillance testing, you -

noted an apparent miscommunication between the plant equipment operator and the control

room operations staff over the status of the radiation monitor and focused your corrective

action on the plant equipment operator's performance. We note that the correct status of the

radiation monitor was communicated to the control room staff and, on more than one

,

occasion, was properly indicated in the plant equipment operator's rounds logs which are

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reviewed periodically by shift supervisory personnel. We are concerned regarding the

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apparent performance deficiencies on the part of operations shift supervision revealed by this

event, and request that you inform us of the results or progress on the action stated in your

,

letter to make the team (shifts) more effective or of any other corrective actions which you

may have taken to address these deficiencies.

With respect to the other violations in our inspection report, thank you for informing us of

the corrective and preventive actions documented in your letter. These actions will be

examined during a future inspection of your licensed program.

.

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Your cooperation with us is appreciated.

Sincerely,

Wayne D. Lanning, Acting Director

Division of Reactor Projects

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Mr. John F. Opeka

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cc:

S. E. Scace, Vice President, Nuclear Operations Services

D. B. Miller, Senior Vice President, Millstone Station

H. F. Haynes, Nuclear Unit Director

G. H. Bouchard, Nuclear Unit Director

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F. R. Dacimo, Nuclear Unit Director

R. M. Kacich, Director, Nuclear Planning, Licensing and Budgeting

J. Solymossy, Director of Nuclear Quality and Assessment Services

Gerald Garfield, Esquire

Nicholas Reynolds, Esquire

K. Abraham, PAO (2)

Public Document Room (PDR)

Local Public Document Room (LPDR)

Nuclear Safety Information Center (NSIC)

State of Connecticut SLO Designee

NRC Resident Inslator

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APR ~* 61994

Mr. John F. Opeka

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bec:

. Region I Docket Room (with concurrences)

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bec (VIA E-MAIL)*

J. Stolz, NRR/PD I-4

V.' McCree, OEDO

G. Vissing, PM, NRR

V. Rooney, PM, NRR

D. Jaffe, PM, NRR

J. Anderson, NRR

M. Shannon, NRR/ILPB

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DEC-G9-1993 16:01

MILLSTONE RESIDENT OFFICE

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September 10, 1993

Docket No. 50-336

B14605

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Ret

10CFR2.201

U.S. Nuclear Regulatory Commission

Attention: Document Control Desk

Washington, DC 20555

Gentlemen:

Millstone Nuclear Power Station, Unit No. 2

Reply to a Notice of Violation

Combined Inspection Report _Nos. 50-245/93-16: 50-336/93-11; 50-423/93-13

In a letter dated July 22, 1993, m the NRC Staff transmitted to Northeast

Nuclear Energy Company (NNECO) Combined Inspection Report Nos. 50-245/93-16,

50-336/93-11, 50-423/93-13.

As discussed in that report, the NRC Staff cited

NNECO for three apparent violations of the Commission's regulations at

Millstone Unit No.

2.

Pursuant to 10CFR2.201, and in accordance with the

instructions contained in the inspection report, NNECO hereby provides, as an

attachment to this letter, the. required information in response to the Notices

of Violation.

Per a telephone conversation with Region I Staf f,

the due date to respond to

the Notices of Violation was extended to September 10, 1993.

This extension

was requested to allow Millstone Unit No. 2 personnel involved in response to

these Notices of Violation time to support operational events associated with

the unit and allow additional time to evaluate and respond to the recently-

issued NRC Staf f Systematic Assessment of 1,1 cense Performance report.

In the NRC Staff's July 22.

1993, letter, the Staff expressed concern

regarding'the apparent repetitive nature of the three cited violations. These

concerns centered on the lack of timely and comprehencive actions to prevent

recurrence, and the apparent ineffectiveness of NNECO's previous corrective

actions.

We share these concerns as evidenced by NNECO's recent decision to

task an Independent Review Team to evaluate performance issues at Millstone

Unit No. 2.

Additionally,

a Millstone Unit

No.

2 Performance Improvement Initiative

recently has been initiated to address a wide-range of unit performance

issues.

We believe that this initiative, coupled with IRT recommendation

implementation,

will help effect resolution to a number of

specific

performance issues that have recently occurred.

The Performance Improvement

Initiative is currently comprised of action plans that address the areas of

configuration control, attention to detail, management / supervisory oversight,

communications, personnel roles and responsibilities, resources, work control,

and accountability. We believe the action plans that have been developed will

immediately address those areas of concern identified. We will be prepared to

(1)

A.

R.

Blough letter to

J.

F.

Opeka, ' Millstone Combined Inspection

Report Nos. 50-245/93-16; 50-336/93-11: 50-423/93-13," dated July 22,

1993.

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MILLSTONE RESIDENT OFFICE-

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U.S. Nuclear Regulatory Costunission

B14605/Page 2

September 10, 1993

discuss this initiative and the results of the Independent Review Team's

effort more fully at the management meeting to be held September 24, 1993.

We trust that you find this information satisfactory and we remain available

to answer any questions you may have.

Very truly yours,

NORTHEAST NUCLEAR ENERGY COMPANY

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J. F. @ive Vice President

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Execut

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cc:

T. T. Martin, Region 1 Administrator

J. W. Andersen, NRC Acting Project Manager, Millstone Unit No. 1

G. S. Vissing, NRC Project Manager, Millstone Unit-No. 2

.'

V. L. Rooney, NRC Project Manager, Millstone Unit No. 3

D. H. Jaffe, NRC Project Manager, Millstone Station

P. D. Swetland, Senior Resident Inspector, Millstone Unit Nos. 1, 2,

and 3

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Docke_t No. 50-336

B14605

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Attachment 1

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Millstone Nuclear Power Station, Unit'No. 2

Reply to a Notice of Violation

Combined Inspection Report Nos. 50-245/93-16:

50-336/93-11; 50-423/93-13

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September 1993

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U.S. Nuclear Regulatory Commission

B1460S/ Attachment 1/Page 1

September 10, 1993

Millstone Nuclear Power Station, Unit No. 2

Reply to a Notice of Violation

Combined Inspection Report Nos. 50-245/93-16;

50-336/93-11; 50-423193-13

_ _ _ _

RESTATEMENT OF VIOLATION At

Millstone Unit 2 Technical Specification 6.8.1

requires that procedures

covering station activities shall be established and implemented.

Station

Administrative Control procedure (ACP) ACP-QA-3.02E, " Procedure Compliance,"

and Surveillance

Procedure

SP-2404AW,

"RBCCW

Liquid Radiation Monitor

(RM 6038) Calibration," were established pursuant to the above.

Procedure ACP-QA-3.02E requires, in part, that the intent and direction of

procedures shall be followed, and that deviation from procedures is not

permitted.

Surveillance Procedure SP-2404AW, "RBCCW Liquid Radiation Monitor

(RM 6038)

Calibration," Steps 4.7 and 6.8.8, require that operations personnel open and

shut, respectively, the isolation valves to the sample canister on monitor RM-

6038.

Technical Specification 3.3.3.9,

" Radiation

Liquid Effluent Monitoring

Instrumentation," Table

3.3-12,

Action

3,

applicable to reactor building

closed cooling water system radiation monitor RM-6038, requires, in part, that

with monitor RM-6038 inoperable greacer than 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, grab samples of service

water system effluent shall be collected and analyzed for gross radioactivity

once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Contrary to the above;

1.

During performance of Procedure SP-2404AW on May 3,

1993, the sample

canister

isolation

valves

on

monitor

RM-6038

were

closed

by

instrumentation and controls personnel vice operations personnel; and,

at the completion of the calibration, the sample canister isolation

valves were not reopened, rendering monitor P&6038 inoperable.

2.

From 7:57

p.m.,

on May 3,

1993, to 1:00 a.m.,

on May 6,

1993, monitor

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RM-6038 was inoperable, during which time grab samples of service water

system effluent were not collected and analyzed for gross radioactivity.

This is a Severity Level IV Violation (Supplement I)

1.

Reason for the Violation

The cause of the event was procedural noncompliance.

The radiation

monitor calibration procedure specifically required that the operations

department close and reopen the isolation valves to RM-6038.

In this

event, the Instrument and Control (I&C) technician closed ' the skid

isolation valves, failed to have Operations close the system isolation

valves, and failed to reopen the skid isolation valves upon completion

of the procedure.

2.

Corrective Steps Than Havo_Been Taken And The Results Achieved

The radiation monitor was immediately unisolated and returned to

service.

Chemistry analysis of the service water system verified that

DEC-09-1993 16:03

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U.S. Nuclear Regulatory Commission

B14605/ Attachment 1/Page 2

September 10, 1993

no gross radioactivity was present.

This event was reported to the NRC

on June 4, 1993, as LER 93-009.*

NNECO considers this event alone unacceptable.

Additionally,

as

discussed between the Millstone Unit No. 2 Director and the NRC Resident

the apparent misreading by the Plant Equipment Operators

Inspector,of the equipment and the resultant incorrect logging, is equally

(PEO's)

unacceptable.

We consider this second issue to be indicative of a lack of attention to

detail and a breakdown in communication.

We have interviewed the PEOs

who mistakenly recorded that flow was evident, when in fact, there was

none.

Our investigation has determined that the PEOs did make their

assigned rounds, but were not effective in verifying flow.

no flow condition had originally

The PEO who properly identified the

reported

the

situation

to

the

control

room

on

May

4,

1993.

Unfortunately, incomplete corrective action was taken by the control

On May 5, 1993, the same PEO realized that the

room staff in response.

situation was not corrected and notified the oncoming shift PEO of the

The oncoming shift PEO identified the problem and had the

lack of flow.

situation corrected.

Plant management is concerned about this lack of attention to detail

with respect to the PEOs ineffective flow verification,

and the

miscommunication between the PEO and control room over the inoperability

of the radiation monitor.

The individuals involved in this event were

counseled, a memo was issued to provide additional guidance to PEOs.

This memo stresses that the PEOs need to individually evaluate their own

'

performance in regard to both rounds and shift turnovers and ensure that

PEO shift turnovers ae performed consistently,

that appropriate

information is passed on to oncoming PEO's, and that problems are to be

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identified and investigated properly. Operations Department Instruction

2-OPS-6.15 was modified to strengthen the PEO job function,

and

specifically includes the requirements that shift turnovers must include

a comprehensive exchange of information.

Specifically, shift turnover

must include:

Status of various systems and equipment.

.

Reasons for any abnormal or out of specification readings noted on

.

rounds sheets.

Plant evolutions in progress.

.

Potentially hazardous activities or conditions reported during the

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previous shift.

Significant maintenance activities completed or carried over.

.

Equipment which is out of service or for which Trouble Reports or

.

Tags have been initiated.

The Operations Department has taken a pro-active approach to assure

these events do not recur.

Shift supervisors are being ' encouraged to

_

S. E. Scace letter to U.S. Nuclear Regulatory Comission, * License Event

(1)

Report 93-009-00,* dated June 4, 1993.

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U.S. Nuclear Regulatory Commission

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B14605/ Attachment 1/Page 3

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September 10, 1993

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develop plans to make the teams more effective, knowing full well that

they are being held accountable for safe and accurate job performance.

Items being considered include: 1) performing more frequent round

observations with their PE0; 2)

Shift Supervisor inspections prior to

4

pEO roundo and a comparison of subsequent discussions of findings and

issues.

NNECO believes the recurrence of these problems is due to incorrect or

ineffective root cause determination and, as a result, incorrect or

ineffective corrective actions have been taken.

corrective stens That Will Be Taken To Avoid Further Violationa_

3.

The I&C Technicians involved were disciplined and counseled on the

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importance of procedural compliance.

The calibration procedure for RM-6038 has been revised to include the

a

following:

Clarification of isolation valve restoration instructions.

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A verification and sign-off of normal process

flow during

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restoration.

A verification and sign-off of inlet and outlet valves open after

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restoration.

Additionally, all radiation monitor procedures have been reviewed and

revised,

as

required,

to

incorporate

the

above

changes,

where

appropriate.

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Dete When. Full compliance Will 3, Achieved

Full compliance was achieved on May 6, 1993, when the radiation monitor

isolation valves were opened.

5.

Generie :tumlications

The changes made to the Radiation Monitor procedures are applicable to

Millstone Unit No.

2.

The impact of the changes at the Haddam Neck

Plant and Millstone Unit Nos. 1 and 3 will be evaluated.

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DEC-09-1993 16:04

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B14605/ Attachment 1/Page 4

September 10, 1993

RESTAI _--I 0F VIOLATION B

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Unit 2 Technical Specification 4.0. 5.a - requires, in part, that

Millstone

inservice testing of valves shall be performed in accordance with Section XI-

of the ASME Boiler and Pressure vessel Code as required by 10CFR50,

Section 50.55a(g).

Surveillance

Procedure

SP-21131,

" Chemical

and Volume

Control . System

operational Readiness Test,* implements the requirements of the above for

2-CH-510 and 2-CH-511.

Procedure SP-21131, Step 7.5.4,

requires, in

valves

part, that if either valve does 2ot meet the acceptance criterion specified by

the procedure, the valves shall be inenediately declared inoperable; a plant

incident report shall be submitted: and the inservice' test coordinator or the

engineering department inservice inspection supervisor shall be notified as

soon as possible.

Contrary to the above, on May 25, 1993, valves 2-CH-510 and 2-CH-511 failed to

the ' f ailure mode test acceptance criterion of Procedure SP-21131, and

meet

were not declared inoperables a plant incident report was not submitted until-

June 3, 1993; and neither the inservice test coordinato.T nor the engineering

department inservice inspection supervisor were notified until June 3, 1993.

This is a Severity Level IV violation (supplement I)

1.

Reason For The Violation

The cause of this violation was the lack of understanding of Inservice

Test (IST) program requirements by the shift supervisor involved and his

lack of compliance with the-procedure guidance.

The procedure clearly

stated thats

a.

the valve was to be declared inoperable

b.

appropriate Technical Specification action must be taken

c.

a PIR was to be submitted

d.

the IST coordinator was to be notified

e.

a trouble report was to be sutenitted

f.

testing was to be continued or suspended as directed by the SS

only steps e and f were followed.

The shift supervisor believed these

actions were appropriate since he knew that engineering practice was to

recommend additional testing and that he believed it was within his

1

authority to retest the valves.

2.

corrective steps That save Been Taken And The Results Achieved

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The valve was declared inoperable, a PIR was initiated to document the

situation, and the IST coordinator was notified.

2.

corrective steps That will Be Taken To Avoid Further Violations

The shift supervisor received appropriate disciplinary action with

respect to the need for complete compliance with IST procedures and the

inappropriateness of his judgements.

In subsequent situations, with

similar IST requirements, the appropriate procedure guidance has. been

followed by this supervisor.

This event was reviewed with all Millstone Unit No. 2 shift supervisors.

i

In addition, a memo to all shift supervisors was distributed on

August 29, 1993, that clarifies expectations with respect to evaluating

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B14605/ Attachment 1/Page 5-

September 10, 1993

IST results.

This memo stressed the need.for IST procedure coenpliance,

how to address aborted test attempts, and the need for protqpt initiation

of PIRs.

The violation also discussed a Plant.Information Report (PIR) timeliness

issue.

The Millstone Unit No. 2 Directer has established, as a result

a task force to evaluate the PIR process with the

of separate concerns,

goal of producing a significant inprovement

in,

and consistency

throughout the process.

The PIR task force will shape and fona the

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process by which individuals perform the investigation, evaluation and

root cause of PIR's thereby ensuring that all investigations are timely

and meet established schedules. In addition, the task force will ensure

all investigations are in-depth and concise, that the appropriate

that

root causes and contributing causes are identified, that the corrective

actions and actions to prevent recurrence are appropriate and effective.

the task force will ensure that the issues learned are

Finally,

appropriately shared throughout the Northeast Utilities organization.

4.

Date M aa Full Compliance Will Be' Achieved

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Full compliance was achieved on June 3, 1993, when the actions specified

in the procedure were acconplished.

5.

^=^ric Immlications

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This violation will be evaluated at the Haddam Neck Plant and Millstone

Unit Nos. 1 and 3 for potential applicability.

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U.S. Nuclear Regulatory Commission

B14605/ Attachment 1/Page 6

September 10, 1993

RSSTATeM7MT OF VIOLATION C

Millstone Unit 2 Technical specification 6.8.1

requires that procedures

covering

station activities

be

established and

implemented.

Station

Administrative Control Procedures (ACP) ACP-QA-3.02E, ' Procedure Compliance,'

and

ACP-QA-2.06A,

" Station

Tagging,"

Chemistry

Procedure

CP-2806X,

" Containment Purge,' and Operatione Procedure OP-2383A, ' Process Radiation

Monitors Operation,' were established pursuant to the above.

Procedure ACP-QA-3.02E,

step

6.2, requires, in part, that the intent and

direction of procedures shall be followed, and that deviation from procedures

is not permitted.

Procedure ACP-QA-2.06A, Step 6.1.2.1, requires, in part, that the position of

valves be verified to be in the proper position when placing tags.

" Containment Purge," Step 5.2.10, and Operations

Chemistry Procedure CP-2806X," Process Radiation Monitors Operation,* Step 5.10, require

Procedure OP-2383A,

that operations personnel disconnect the temporary sample rig from connections

downstream of radiation monitor RM-8123 and restore normal valve positions

following collection of containment atmosphere samples.

Contrary to the above;

1993, valves 2-AC-122 and 2-AC-124 were not verified to be

On March 28,

1.

The

in the proper shut positions when tags were placed on the valves.

valves were actually open.

2.

On several occasions prior to March 28, 1993, following sampling of the

containment

atmosphere,

chemistry

personnel

conducted

activities

required to be performed by operations,

i.e.,

disconnecting the sample

rig and repositioning valves.

This is a Severity I,evel IV Violation (Supplement 1)

1.

Reason for the Violation

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The cauce of this event was personnel error:

Work Practice Procedures

not followed and Verification not performed.

Following CP 2383A,

' Process Radiation Monitors Operation," steps for RM-8123 containment

sampling would have restored the Radiation Monitor to a normal operating

Verifying the red tag required position for 2-AC-124 and

configuration.

2-AC-122 against the actual valve position would have ensured that the

valves were closed after the tags were rehung.

The chemistry personnel error was caused by the chemistry procedure not

clearly stating that Operations must perform the manipulation of the

valves.

Corrective steps That Have Been Taken And The Results Achieved

2.

When the day shift PEO reported the incorrect lineup on radiation

monitor RM-8123, he was directed to take the following actions:

Close

the inlet and outlet drain valves (2-AC-124 and 2-AC-122), disconnect

the sample tubing, and replace the pipe caps on 2-AC-124 and 2-AC-122.

These actions were completed.

shift briefings were conducted for the operating shifts shortly af ter

the incident occurred.

These briefingc discussed the incident and

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U.S. Nuclear Regulatory Comission

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B14605/ Attachment 1/Page 7

September 10, 1993

reviewed Operations Department roles and procedural requirements for

containment sampling using RM-8123 and PE-8162.

The PEO involved was counseled by his supervision regarding the

importance of procedure compliance during evolutions.

Verification

during tagging activities was also emphasized.

3.

Corrective Stepa__That Will Be Taken to Avoid Further Violation

Operator

training

will

be

conducted

to

incorporate

knowledge

requirements associated with containment air sampling into the classroom

I

portion of the Non-Licensed operator Initial Training (NLIT) Auxiliary

Building PE0 course.

In addition, additional training on containment

air sampling has also .been included in the Non-Licensed Operator

Continuing Training (NLCT) Auxiliary Building PEO cource. This training

is in progress and will be completed in October 1993.

Finally, in-plant

walk throughs will be performed as part of the next cycle of NLCT.

This

cycle of training will reemphasize which valves may be manipulated by

chemistry and which valves may be manipulated by operations. This cycle

of NLCT will be completed by January 1994.

The chemistry procedure concerning the operation of the valves (CP

2006X, ' Containment Purge") is being rewritten to include only Chemistry

Department personnel responsibilities.

In addition, the feasibility of a design change is being evaluated. The

modification involves installation of permanent connection points for

the RM-8123 and RM-8262 external sample equipment.

If implemented, the

)

modification will remove the requirement for Operations personnel to

maintain red tags and temporary sample hoses on the Radiation Monitor

inlet and outlet drain valves.

4.

Date when Full _ Compliance Will Be Achieved

Full coqpliance was achieved on March 28, 1993 when the PE0 notified the

control room of the

condition,

shut

the

isolation valves,

and

disconnected the rig.

The initial training enhancements have been made and will be given

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during the normal initial training modules.

NLCT will be completed by

January 1994.

The chemistry procedure revision will be completed by

f

September 30, 1993.

5.

Generic Implications

The corrective actions made and being proposed to training and

procedures are specific to Millstone Unit No. 2.

Plf nt and at

This violation will be evaluated at the Haddam Neck

A

Millstone Unit Nos. 1 and 3 for potential applicability.

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DEC-10-1993 11:17

MILLSTONE RESIDENT GFFICE

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FACSIMILE FROM MILLST0hE RESIDEE OFFICE

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'Ihank you for informing us of the corrective and preventive actions

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LEC-10-1993 11:18

MILLSTOE RESIDENT OFFICE

203 443 5893

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General Offices * Selden Street, Berlin. Connecticut

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P.O. BOX 270

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HARTFORD. CONNECTICUT 06141-0270

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June 7, 1993

Docket Nos. & ?di

50 #3E

50_423

B14486

Re:

10CFR2.201

U.S. Nuclear Regulatory Commission

Attention: Document control Desk

Washington, DC 20555

Gentlemen:

'

Millstone Nuclear Power Station, Unit Nos.1, 2, and 3

Reply to Notice of Violations

Combined insoection 50-245/93-10: 50-336/93-06t 50-423/93-07.

In a letter dated April 30, 1993,"' the NRC Staff transmitted its Notice of

Violation (NOV) relating to NRC Combined Inspection '..eport Nos. 50-245/93-10;

50-336/93-06; and 50-423/93-07. . The report discussed the results of safety

inspections conducted between March 3, 1993, and April 3, 1993.

Based on the

results

of the

Staff's

inspection,

three

violations were

identified.

Attachment 1 to this letter provides Northeast Nuclear Energy Company's

,

(NNECO) response to the first violation, on behalf of Millstone Unit No.1

pursuant to the provisions of 10CFR2.201.

Attachment 2 provides NNECO's

response to the second and third violations on behalf of Millstone Unit No. 2

pursuant to the provisions of 10CFR2.201.

In a telephone conference with the

NRC Staff on May 24, 1993, it was mutually agreed that this response would be

submitted within 30 days from May 6,1993, the date of receipt.

The NRC letter also involved a detailed review of the activities of groups

which contributed to the overall self-assessment functions at the Millstone

Station.

While NNECO does not dis)ute the inspection findings, we have

included a brief discussion relat'ng to

self-assessment activities

in

Attachment 3.

(1)

A.

R.

Blough letter to J.

F.

Opeka, " Millstone Combined Inspection

50-245/93-10; 50-336/93-06; 50-423/93-07,' dated April 30, 1993.

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DEC-10-1993 11819

t11LLSTONE RESIDENT OFFICE

203 443 5893

P.04

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U.S. Nuclear Regulatory Commission

B14486/Page 2

June 7, 1993

!

If you have any questions regarding information contained herein, please

contact us.

Very truly yours,

NORTHEAST NUCLEAR ENERGY COMPANY

FOR: J. F. Opeka

Executive Vice President

BY:

"#

W. D. Romberg

P'

Vice President

cc:

T. T. Martin, Region I Administrator

1

D. H. Jaffe, NRC Project Manager, Millstone Station

J. W. Andersen, NRC Project Manager, Millstone Unit No. 1

G. S. Vissing, NRC Project Manager, Millstone Unit No. 2

V. L. Rooney, NRC Project Manager, Millstone Unit No. 3

P. D. $ wetland, Senior Resident Inspector, Millstone Unit Nos.1, 2,

and 3

-

DEC-10-1993 lit 19

MILLSTGNE RESIDENT OFFICE

203 443 5893

P.05-

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Docket No. 50-245

B14486.

'

Attachment 1

,

'

Millstone Nuclear Power Station, Unit No.1

Reply to a Notice of Violation

combined Inspection 50-245/93-10; 50-336/93-06; 50-423/93-07

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June 1993

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DEC-10-1993 11:19"

MILLSTONE RESIDENT OFFICE

203 443 5893.

P.06

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1

- U.S. Nuclear Regulatory Commission

i

B14486/ Attachment 1/Page 1

!

June 7, 1993

4

Millstone Nuclear Power Station, Unit No.1

i

Reply to a Notice of Violation

Combined. Inspection 50-245/93-10; 50-336/93-06; 50-423/93-07

!

Restatement of Violation

i

i

During an NRC inspection conducted on March 3,1993, through April 3, h the

1993,.

i

violations of NRC requirements were identified.

In accordance wit

" General Statement of Policy and Procedure for NRC Enforcement Actions," 10CFR 2

j-

Part 2, Appendix C, the violation ~ is listed below:

,

A.

10CFR Part 50, Appendix B, criterion XVI (corrective Actions) requires,

!

in part, that measures shall be. established to assure that conditions

adverse to quality, such as failures, deficiencies, and deviations be

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!

promptly identified and corrected.

The measures shall assure that the

i

cause of the. condition is determined and corrective action is taken to

preclude recurrence.

.

'

Contrary to the above, since 1985, fourte= safety-related auxiliary

electrical contacts have failed to operate on demand, rendering Unit 1

l

equipment inoperable.

The cause of the failures was attributed to dried

i

grease / cleaner residue, a maintenance-related condition applicable to

4

many similar safety-related contacts.

The licensee did not develop

effective corrective actions to preclude recurrence of the subsequent

i

failures.

l

This is a Severity Level IV Violation.

(SupplementI)

1.

Reason for Violation (Violation A1

l

Plant Incident Report (PIR) investigations, relating to auxiliary contact

i

failures, identified the need to perform Preventative Maintenance (PM) of

3

the auxiliary contacts in order to improve component reliability.

This

action was not completed at the time of PIR close-out and no tracking

,

i-

commitment was established to ensure the completion of the PM activity,

l

which resulted in subsequent failures.

,

,

'

Although it would have been expected that this action would have been

completed, the PIR Administrative Control Procedure did not specifically

>

require action item tracking prior to close-out.

2.

Corrective

Steos That Have

Been Taken

and

the Results AcMeved

(Violation A)

j

-

.

An expedited program was established to identify, inspect, clean, and

lubricate the app,icable safety related auxiliary contac;s. This program

i

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DEC-10-1993. 11:20

MILLSTOtG RESIDENT OFFICE

203 443 5893

~P.07

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U.S. Nuclear Regulatory Comission

B14486/ Attachment 1/Page 2

June 7, 1993

4

was completed on April 28, 1993.

Note that this program did not reveal

any contact

abnormality sufficient to

inhibit the component from

performing its safety function.

3.

The Corrective Steps That Will Be Taken to Avoid Further Violations

(Violation A)

Since the time of the 1991 PIR, there have been numerous enhancements

made to the PIR process such that the PIR Administrative Control

Procedure (ACP-QA-10.01) now requires that comitments be established for

,

all corrective actions and/or actions to prevent recurrence identified in

the PIR that are incomplete at the time of PIR close-out.

The importance and significance of comitment tracking and follow-through

will be reinforced to all personnel involved with PIR investigations and

close-outs. This will be completed by July 30, 1993.

A periodic PM program will be established to clean and lubricate all the

safety-related contacts every other refuel outage. All nonsafety-related

auxiliary contacts will be cleaned and lubricated every third refuel

outage.

. This program will be in place by December 31, 1993, to be

implemented during the 1994 refuel outage.

4.

The Date When Full como11ance Will Be Achieved (Violation A)

An expedited program was established to identify, inspect, clean, and

lubricate

the applicable safety-related auxiliary contacts.

Full

compliance was achieved when this program was completed on April 28,

1993.

5.

Generic Implications (Violation Al

This issue will be identified to Engineering Management personnel at

Millstone Unit Nos. 2 and 3 and the Haddam Neck Plant.

Actions will be

taken as appropriate.

,

Additional Information (ViolationJO

The Staff expressed concern with the timeliness of corrective actions

established following the 1992 auxiliary contact failure.

An imediate

program to clean or replace the auxiliary contacts was not considered based on

the following:

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MILLSTONE RESIDENT OFFICE

203 443 5893

P.08

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4

U.S. Nuclear Regulatory Commission .

B14486/ Attachment 1/Page 3

June 7, 1993

NNECO was awaiting a response to a verbal request made to GE for

-

recommendations

to

improve

the

reliability

of

the

auxiliary

contacts.

Based on the number of auxiliary contacts. utilized, a failure rate

-

of two safety-related contacts per year was not deemed excessive.

Performance of Technical Specification surveillance would detect

-

contact failures.

Absent explicit te.a.hnical vendor information, . Millstone Unitf No.1

-

personnel elected not to implement actions which had the potential

to increase the failure rate.

It should be noted that when NNECO did receive accurate information from the

vendor, the issue was addressed aggressively and resolved.

The ' Staff also expressN concern for NNEC0's lack of consideration for the

potential of common mode failure.

This historical failure rate, as reviewed

by Probabilistic Risk Assessment, is consistent with their expectations, which

are established based on industry contact failure data.

However, the Staff's~

point- regarding sensitivity to common mode- failures is. well taken.

In this

regard, NNECO will

provide to Engineering and Plant -Operations. Review

Committee members by July 30, 1993, information regarding the potential for

,

common mode failures.

Additionally

since

1991,

the

Engineering

Department

is

assigned

the

responsibility for investigation of the majority of PIRs, allowing trends and

common mode failures to be more readily recognized.

Based upon NNECO's difficulty in determining appropriate PM requirements for

auxiliary contacts from the component vendor, a Nuclear Network Notification

(OE 5909) was transmitted on April 6,1993, to inform other plants of the

vendor recommendation to clean and lubricate the auxiliary contacts on a

three-to-five year basis,

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MILLSTONE RESIDENT OFFI

203-443 5893'

P.09

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()ocket No. 50-336

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B14486

,

.

1

2

4

4

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Attachment 2

Millstone Nuclear Power Station, Unit No. 2

l

Reply to Notice of Violations

-

Combined Inspection 50-245/93 10; 50-336/93-06; 50-423/93-07

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June 1993

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DEC-10-1993 11:21-

MILLST0tE RESIDENT. OFFICE

203 443 5893

P 10

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.

U.S. Nuclear Regulatory Commission

B14486/ Attachment 2/Page1

June 7, 1993

Millstone Nuclear Power Station, Unit No. 1

Reply to Notice of Violations

Combined Inspection 60-245/93-10; 50-336/93-063 60-423/93-07

Restatement of Violations

During an NRC inspection conducted on March 3,1993, through ' April 3,1993,

violations of NRC requirements were identified.

In accordance with the

" General Statement of Policy and Procedure for NRC Enforcement Actions," 10CFR Part 2, Appendix C, the violations are listed below:

B.

Millstone

Unit

2

Technical

Specification.

6.8.1.a.

requires

that

procedures be established, implemented, and maintained as recommended in

Appendix A

of

Regulatory

Guide 1.33,

Revision 2,

February

1978.

Regulatory Guide 1.33, Revision 2, February 1978.- Regulatory Guide 1.33

recommends procedures for administrative control of surveillance testing.

Surveillance Procedure SP-2401C, "RPS Turbine Loss of Load . Test," step

6.2.1

requires that certain reactor protection system (RPS)

trip

bistables be bypassed . prior to testing the turbine trip bistable.

Step 6.2.6 ~ requires alarms on the nuclear instrumentation linear ' power

range channel - drawer and the RPS- trip bistables to be reset prior to

removing the bypass keys installed in, step 6.2.1.

Contrary to the above,'on February 22, 1993, on one occasion, step 6.2.6

of SP-2401C was not performed prior to removing the bypass keys; and, on

two occasions, step 6.2.1 of SP-2401C was not performed prior to testing

the turbine. trip bistables.

This is a Severity Level IV Violation.

(SupplementI)

C.

Millstone Unit 2 Technical Specification 6.8.1.e requires that procedures

be

established,

implemented,

and

maintained- for - emergency

plan

implementation.

Emergency Plan Implementing Procedure ~4701-4, " Event

Classification," requires prompt NRC notification of any . event or

condition that results in an unplanned automatic actuation of any

engineered safety feature, including the reactor protection system (RPS).

Contrary to the above, on February 22, 1993, an unplanned automatic

!

actuation of the RPS system occurred due to excessive feeding of the

steam generators; the licensee did not report the event to the NRC until

March 11', 1993.

This is a Severity Level IV Violation.

(supplement 1)

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DEC-10-1993 11:22

MILLSTONE RESIDENT OFFICE

203 443 5893,

P.11

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U.S. Nuclear Regulatory Commission

!

B14486/ Attachment 2/Page 2

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June 7, 1993

,

1.

The Reason For the Violation (Violation B)

'

The reason for the violation results from a' failure to specifically

identify to the user which items were required to be reset prior to

removing the bypass keys.

The importance of this step had not

specifically been clearly stated previously.

i

2.

The Corrective Stoos Taken and The Results Achieved (Violation B).

4

3.

In response to the conditions which resulted in the Notice of Violation,

4

change #2 to Revision 6 of SP-2401C was written and approved.

This

change added a precaution which identifies the results of the failure to

i

reset the high voltage bistable as the- initiator of a power trip test

,

4

interlock (PTTI).

The actuation of the PTTI results in tripping the

'

affected channel,

i ..

The second portion of the change calls for resetting the high voltage.

.

. bistable ' and Level I bistable, rather than the general reference to

3

l

resetting alarms

and. bistables.

No previous problems with this

,

!

surveillance are known to have been experienced.

hith this change, no

l

future recurrence is anticipated.

![

3.

The Corrective Stoos That Will Be Taken to Avoid Further Violations

-

(Violation B)

i

The Instrument and Controls (I&C) Department Manager will discuss this

j

event,

the Notice of Violation,

and the lessons learned with I&C

department personnel.

This discussion is expected to occur' before

.

June 30, 1993.

i

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4.

Ihe_Date When Full Como11ance Will Be Achieved (Violation B)

SP-2401C was changed and approved on April 13, 1993, therefore, full

compliance has been achieved.

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5.

Generic Imolications (Violation B)

i

This event will be discussed with I&C Department personnel at Millstone

Unit Nos. I and 3 and the Haddam Neck Plant.

Actions will be taken as

-

appropriate.

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DEC-10-1993 11:22.

MILLSTONE RESIDEN 0;F CE

203 M3 5893

P.12

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U.S. Nuclear Regulatory Commission

B14486/ Attachment 2/Page 3

June 7, 1993

1.

The Reason For The Violation (Violation c)

In reviewing the personnel actions associated with this event, it appears

that during performance of the event recovery actions, therc was.a less-

than-sufficient level of review. More attention was given to the reasons

i

for the cooldown event than to the results of the cooldown event.

The

operating shift members, knowing the . reactor was tripped based upon

events which had occurred earlier in the morning, focused their attention

on the causes of the cooldown and the appropriate actions necessary to

respond to the changing plant conditions. Once the cause of the cooldown

'

was determined

their review refocused to the level- of attention which

,

was required to prevent recurrence. The actions required to specifically

1

identify the occurrence, or cause, of an automatic actuation of the

reactor protection system (RPS). appear not to have been taken.

Rather,

,

it appears that the actions were based .on the belief that the event was

'

understood and all parameters had been addressed.

Thus, the RPS

actuation was unreported for 18 days.

Personnel

involved

in,

or

present' during, .these

actuations

were

interviewed, with the results of these interviews accurately rep

CombinedInspectionReport.{esented-

i

in Section 2.4 of the April 30, 1993,

2.

The corrective Steos That Have- Been Taken And The Results Achieved

(Violation C)

A review of the events which occurred during February 22 and February 23,

1

1993, was performed upon our discovery of the cited failure to report an

automatic actuation of the RPS.

As a result of this review, an

additional two RPS actuations were identified.

NNECO has determined that

neither of these two actuations is reportable pursuant to 10CFR50.72 or

'

100FR50.73.

,

i

The NRC reporting requirements for the automatic actuation of the RPS

'

have

been discussed

extensively with

members

of the

unit

staff

responsible for the reporting of. these events.

Additionally, the

individual who was filling the role of On-Site Director -of Station

Emergency Operations (ODSED) has been counseled on his judgment during

,

this series of events.

Discussions pertaining to these events have been

extensive within the unit and have focused on the requirement to review

the control room journal as a necessary input for determining the

'

reportability of a specific event.

(2)

A. R. Blough to J. F. Opeka, " Millstone Combined Inspection 50-245/93-10;

50-336/93-06; 50-423/93-07, dated April 30, 1993.

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MILLSTONE RESIDENT OFFICE

203 443 5893

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U.S. Nuclear Regulatory Commission

B14486/ Attachment 2/Page 4

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June 7, 1993

3.

The Corrective Actions That Will Be Taken To Avoid Further Violations

>

(ViolationC)

The unit management will prepare and distribute a memorandum to Millstone

Unit No.

2 personnel .which will

further define expectations for

performance

in

the

lower

operational

modes

and

the ' operability

requirements of the RPS -while in Mode 3.

' This discussion will not be

limited

to

the Operations

personnel,

but

will

also

define

the

-

expectations for personnel performing surveillance testing.

Discussions

,

under this memorandum or an additional memorandum will be distributed to

the Unit Senior Operator Licensed personnel, as well as those personnel

,

who fulfill the role of ODSEO and Duty Officer, to highlight expectations

'

concerning the importance of timely event assessment and- classification

-

in accordance with existing Administrative Controls Procedures.

The caution statement, contained with E0P 2526, " Reactor Trip Recovery,"

will be reviewed to determine if it would be more appropriate as an

Action step.

The most appropriate location for this guidance, as either

a Caution or as an Action step, will be determined.

'

4.

The Date When Full Como11ance Will Be Achieved (Violation C1

The corrective actions, stated in section 3 will be completed by July 31,

1993, with the exception of any revision to E0P 2526 which, if required,

,

will be completed by December 31, 1993.

.

5.

Generic Imolications (Violation C1

This issue will be discussed with Engineering Department Management

)

personnel at Millstone Unit Nos. 2 and 3,

and the Haddam Neck Plant.

Actions will be taken as appropriate.

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DEC-10-1993 11:23

MILLSTOE RESIDENT OFFICE

203 443 5893

P.14

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Docket Nos. 50 245

I

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50-336

50-423

B14486

i

!

I

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s

Attachment 3

l

Millstone Nuclear Power Station, Unit Nos.1, 2, and 3

Reply to Notice of Violations

Combined Inspection 50-245/93-10; 50-336/93-06; 50-423/93-07

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June 1993

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MILLSTONE RESIDENT OFFICE

203 443 5893

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U.S. Nuclear Regulatory Commission

.

B14486/ Attachment 3/Page 1

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June 7, 1993

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Millstone Nuclear Power Station, Unit Nos. 1, t'and 3

Reply to Motice of Violations-

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Combined Inspection 50-245/93-10 50-336/93-06: 50-423/93-07

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self Assessment Groun Activities (Section 5.4)

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Backaround

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The combined ' inspection report" (Section 5.4) included a detailed review of

the activities of groups that contributed to the overall self-assessment -

function at the Millstone Station.

Several different types of assessment

activities were inspected and discussed. The inspection report concluded that

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the effectiveness of the self-assessment groups at Millstone Station varied.

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The NRC' Staff found that, .although the Quality Services Department (QSD)

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critically assessed plant and corporate performance and clearly. communicated

findings to management, chronic weaknesses in corrective action programs .and

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compliance with administrative procedures existed.

The NRC Staff indicated

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that this area of the report warranted NNECO's close attention.

Further, the

report invited our response if we either had questions or disputed the

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findings.

This - attachment provides a discussion of NNECO's 'self-assessment

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activities at Millstone Unit Nos. 1, 2, and 3.

Immediate Action

NNECO has taken and will continue to take actions to improve performance in

this area.

The inspection report discussed the Corrective Action Request

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(CAR) 93-01, which QSD issued to NNECO management on March 3, 1993, to elicit

action.

In response, the Millstone Station Vice President issued two separate

memoranda, dated April 30, 1993.

Millstone Station Vice President Neporandum to NNEC0 Department Heads:

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The first Millstone Station Vice President memorandum was sent to NNECO

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Department Heads and discussed causes and actions to prevent recurrence.

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Three general causes of ongoing procedure noncompliance were identified.

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These

were

ambiguous

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conflicting

procedure

content,

insufficient

familiarity with procedural requirements, and

>ersonnel error.

The cause

associated with an individual- QSD Surveillance finding typically fell within

one or more of these categories.

The recurring nature of deficiencies

identified by the QSD Surveillances indicated that the identification of

causal

factors was not sufficiently accurate to allow the appropriate

corrective actions to be implemented.

If the causal factors were not well

understood, then actions to prevent recurrence could not- be successful.

The

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(3)

A. R. Blough to J. F. Opeka, " Millstone Combined Inspection 50-245/93-10;

$0-336/93-06; 50-423/93-07, dated April 30, 1993.

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DEC-10-1993 11:25

MILLSTONE RESIDENT OFFICE

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U.S. Nuclear Regulatory Commission

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B14486/ Attachment 3/Page2

June 7, 1993

underlying

cause

of

recurring

procedure

noncompliance

was

inadequate

determination of the causal factors for QSD surveillance items.

One of the factors mentioned- above as contributing to certain procedure

noncompilance occurrences was .the existence of ambiguities or errors in some

procedures, especially Administrative Control

Procedures (ACPs).

In an

attempt to minimize the impact of this factor, a review was performed of

selected ACPs to identify problems that should - be corrected immediately.

These procedure changes are being expedited,

and will make procedure

compliance hss difficult.

It is recognized,

however,

that procedure

inadequa:, es still a potential causal factor for procedure noncompliances

identifiej by QSD Surveillances and other processes. The existin

effort will continue to implement long-term corrective measures. g ACP rewrite

To address the underlying cause of recurring deficiencies identified by. QSD

Surveillances,

station

personnel

were

instructed

to

improve

their

determination of the causal factors for these deficiencies.

This would be

done in two ways:

by processing and responding to each individual QSD

Surveillance finding in a more rigorous manner (described below), and by

evaluating trends in procedure noncompliance and work performance by analyzing

QSD Surveillance findings, Work Observation Program observations, and Plant -

Incident Report (PIR) data.

Following the identification of causal factors

and corrective / preventive' measures, follow-through is -required to assure

timely and effective completion of corrective / preventive actions.

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Processino of OSD Surveillance Findinos:

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Beginning May 10, 1993 all deficiencies identified by QSD Surveillances were

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required to be responded to in writing by the cognizant department.

These

responses would address the following: cause of the deficiencies, the generic

implications of the deficiency, immediate and/or long-term actions to correct

the deficient condition, and actions to prevent recurrence, including interim

measures, if appropriate.

Five working days before the response due date,

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each response i s required to be forwarded to the cognizant Unit Director for

review.

Responses not meeting the above requirements will be rejected and

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returned, with comments, to the submitting unit depart::ent head.

The Station

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Vice President will be costed on each response to QSD, ano will review quality

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and timeliness.

Following a brief period for everyone to understand the

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process, the adequacy of these responses will be tracked and trended, for

consideration in the annual performa":e appraisal of all personnel in the

response preparation and approval chain.

Millstone Station Work Observation Procram

The Work Observation Program was initiated in September 1992.

It was

identified as a strength by the Institute of Nuclear Power Operations (INPO)

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during a recent Millstone Station evaluation.

It functions as a management

and worker tool that:

1) Reinforces work practice expectations; 2

Evaluates

work practices; 3) Directs supervisory involvement; 4) Provides a) process to

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B14486/ Attachment 3/Page 3

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June 7, 1993

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promptly correct deficiencies; 5) Provides management information to-monitor

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corrective action effectiveness.

Observations are conducted by department

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heads and first line supervisors.

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Trendina of Work Observation Proaram Observations and Deficiencies Identified

by OSD Surveillances:

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The results of QSD Surveillances, the Work Observation Program, and PIRs.will'

be categorized and trended on a monthly basis.

This process is designed to.

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identify trends-in occurrences of siellar deficiencies.

A team composed of

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QSD, Nuclear Licensing, Unit ' representatives, and Program Services evaluate

the results and provide analysis and trend plots to De sartment Heads,

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-Directors, and the Station Vice President.

The conclusions w 11 be disetwed.

by Directors at the third department head-meeting of each month.. Action items

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will be assigned as necessary, .and controlled routings (CRs) issued for

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tracking.

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Millstone Station Vice President Memorandum to All Station Personnel:

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'The second Millstone Station Vice President memorandum was sent lto all

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Millstone Station personnel

to emphasize the. Station Vice President's

expectations for procedure compliance at Millstone-Station. A previous Notice

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of Violation and the recent CAR indicated that some station personnel were not

performing to' expectations regarding compliance with station ACPs.

The

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Station Vice' President's expectations are stated below.

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All personnel performing work at Millstone Station are expected to use

and comply with applicable procedures.

When questions relating to the

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adequacy or interpretation of procedures arise, the work must stop until

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the question is resolved by first-line supervision.

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First-line supervisors are exsected to assure that personnel Working

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under their direction have sufficient knowledge and understanding of the

procedures applicable to their work assignments.

They are also expected

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to assure that personnel adhere to the provisions of these procedures.

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Training, project briefings, and field observations should

be used to

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assure this expectation is understood and is being achieved.

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Department heads and Directors are expected to assure that the above

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expectations are met by direct observation by monitoring the Work

Observation Program and QSD Surveillances, and by other appropriate

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measures.

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The memorandum expressed that everyone should understand that the issue is

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performance of personnel to standards and expectations.

All personnel must

understand what is expected of them, examine their. own performance, and

recognize the need for improvement.

It was emphasized that the above

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expectations must be met.

Each individual is accountable for his/her ~ own

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MILLSTOtE RESIDENT OFFICE

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U.S. Nuclear Regulatory Commission

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B14486/ Attachment 3/Page 4

June 7, 1993

performance, and supervisors are also accountable for the performance of their

subordinates.

In addition to these two Station Vice President memoranda, additional short .

term and long-term actions have been initiated.

Short-Term Actions

A task force review of approximately 30 ACPs was conducted to identify

compliance problems related to the ACPs.

As a result of the task force

review, six procedures were identified as requiring a change.

The proposed

procedure changes were based on:

(1) procedure clarity; (2) procedures with

which personnel have compliance difficulty;

(3)hanges

work observation-or QSD

surveillance-identified problems.

Procedure

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are

currently

in

progress.

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In addition, two global issues were identified. ' Specifically, ACP training is

essentially a repeat of the procedure steps rather than focusing on process

training;

i.e., train personnel on what the process is and how they fit into

that process, and how She ACPs support that process.

The second global issue

is a lack of a matrix that ties the procedure requirements to a position.

Lona-Term Actions

A new work process improvement effort is currently in progress.

It is

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expected to result in:

1) Integrated work teams; 2) Improved work . scope

change process; 3) Fewer interface points; 4) Improved communications; and 5)

Streamlined documentation.

The Stop Think Act Review (STAR) Program is a Self-Check Program. The program

will be applied to all working groups at Millstone Station.

Booklets have

been printed and are ready for distribution. NNECO management is treating the

Self-Check Program as a philosophy, i.e., the program itself may require only

brief initial training, while its concepts will be incorporated into-training

presented by the training department in formal training.

This would include

new employee training, annual general employee training, technical staff

management training, technical training, and operator training. . Currently,

the training department has incorporated the process into certain sessions

including Millstone Unit No. 1 Operator Training.

Department heads and

supervisors will reinforce self-checking expectations in department meetings

and tailboard sessions.

By using the weekly station meeting, newsletters from the Station Vice

President, Millstone Target Vision, and posters and -booklet distribution,

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NNECO management plans to introduce the program to all Millstone workers,

including contractors.

The depth of training for initial presentation of the

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program is currently being detemined.

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DEC-10-1993 11:27

MILLSTONE RESIDENT OFFICE

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U.S. Nuclear Regulatory Commission-

B14486/ Attachment 3/Page 5

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June 7, 1993

Conclusion

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NNECO management recognizes the need to improve self-assessment corrective

action programs and compliance with administrative arocedures.

We have taken

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immediate action in the form of the two station Vice President memoranda to

explicitly communicate expectations.

. Additional short-term and long-term

actions are expected to reinforce these expectations. ' QSD and line management

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have recently seen improvement. The surveillance information and deficiencies:

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have become more clear and well focused, allowing corrective actions to be

more appropriately determined.

We are optimistic that the sum of these

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actions will continue- to be instrumental in strengthening this identified

weakness.

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DEC-09-1993 .16:01

MILLSTONE RESIDENT OFFICE

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P. 02 -

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' APPLICATION FOR A REPLY IErlER

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Licensee's Name:

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Subject:

Inspection N ' ME '9 b ' 5

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Combined Inspection

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(if more

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Fmydot Selection:

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Use this Standard I.etter:

Paragraph No.

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This letter refers to your 9'l 0 9b+ndence, in response to

our 9 2 L '9b letter. (Enter appropriate dates)

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Thank you for informing us of the corrective and preventive actions

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documented in your letter. These actions will be examined during a

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future inspection of your licensed program.

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Your cooperation with us is aporeciated.

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Sincerely,

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Use the standard letter, but insert the following text as Paragraph

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(Please number paragmphs).

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In your verponse to the Motice of Ylolation regarding failure to restore the

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reactor building closed cooling water radiation monitor to nervice properly

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following surveillance testings you noted an apparent miscommunication between

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.the plant equipment operator and the control room operacions statf over the

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status of the radiation monitor and focused your corrective action on the

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plant equipment operator's performance. We note that the correct status of.

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the radiation monitor was' communicated to the control room statf and, on more

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than one occasion, was properly indicated in the plant equipment operator's

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rounds logs which are reviewed periodically by shift supervisory personnel.

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We are concerned regarding the apparent performance deficiencies on the part

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of operations shift supervision revealed by this evente and request that you

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inform us of any corrective actions which you may have taken to address thess

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deficiencies.

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itegion I Form 13

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(Revised October,1992)

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