ML20028A424
| ML20028A424 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 11/04/1982 |
| From: | Hairston W ALABAMA POWER CO. |
| To: | |
| Shared Package | |
| ML20028A422 | List: |
| References | |
| NUDOCS 8211220124 | |
| Download: ML20028A424 (10) | |
Text
4 JOSEPH M. FARLEY NUCLEAR PLANT UNIT 2 NARRATIVE
SUMMARY
OF OPERATIONS October, 1982 In the month of October there was one unit shutdown on October 22, 1982, which initiated the Cycle I - Cycle II refueling.
The-following safety-related maintenance was performed in the month of October:
1.
Performed miscellaneous maintenance on diesel generators.
2.
Repacked 2E Service Water pump.
3.
Repacked #7 River Water pump.
4.
Performed annual inspection on Spent Fuel Pool Cask crane.
5.
Repaired leaking Spent Fuel Pool check valve V013 (Pen. #95).
l e
1m R
STEAM GENERATOR TUBE PLUGGING Based on industry experience and past experience at FNP, the majority of Westinghouse steam generator tube leaks occur on the steam generator inner row tubes. Therefore, a management decision was made to plug all the inner row tubes of the three l';it 2 steam generators to prevent unplanned outages in the future. Also, three additional tubes on Steam Generator 2A were plugged.
Dates of Plugging:
10/28/82 - 11/01/82 All (94) S/G 2A inner row tubes were plugged.
In addition, the three following tubes on S/G 2A were also plugged.
Row Column 28 10 29 11 30 12 All (94) S/G 2B inner row tubes were plugged.
All (94) S/G 2C inner row tubes were p' lugged.
OPERATING DATA REPORT DOCKET NO. 50-364 DATE 11/04/82 COMPLETED BY W.G.Hairston, III TELEPHONE (205)899-5156 OPERATING STATUS
- 1. Unit Name:
Joseph M. Farley - Unit 2 Notes
- 2. Reporting Period:
October, 1982
- 1) Cumulative data since
- 3. Licensed Thermal Power (MWt):
2652 7/30/81, date of commer-860 cial operation.
- 4. Nameplate Rating (Gross MWe):
- 5. Design Electrical Rating (Net MWe):
829
- 6. Maximum Dependable Capacity (Gross MWe):
854.7
- 7. Maximum Dependable Capacity (Net MWe):
813.7
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
N/A
- 9. Power Level To Which Restricted,If Any (Net MWe):
N/A
- 10. Reasons For Restrictions. If Any:
N/A This Month Yr.-to.Date Cumulative i1. Hours In Reporting Period 745 7,296 11,017
- 12. Number Of Hours Reactor Was Critical 528 6,346.2 10,032.4
- 13. Reactor Reserve Shutdown Hours 0
97.6 138.4
- 14. Hours Generator On.Line 527.7 6,254.2 9,920.7
- 15. Unit Reserve Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWH) 1.387,065 15,955,657 64,400,880
- 17. Gross Electrical Energy Generated (MWH) 441,252 5,102,520 8,173,898
- 18. Net Electrical Energy Generated (MWH) 417.138 4.832.614 7,753,334
- 19. Unit Service Factor 70.8 85.7 90.0
- 20. Unit Availability Factor 70.8 85.7 90.0
- 21. Unit Capacity Factor (Using MDC Net) 68.8 81.4 86.5 67.5 79.9 84.9
- 22. Unit Capacity Factor (Using DER Net)
- 23. Unit Forced Outage Rate 0.0 11.6 8.1
- 24. Shutdowns Scheduled Over Next 6 Months (Typc. Date,and Duration of Each1:
N/A
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
12/12/82
- 26. Units in Test Status 1 Prior to Commercial Operation):
Forecast Achiesed
)
INITIA L CRITICALITY 5/06/81 5/08/81 INITIA L ELECTRICITY 5/24/81 5/25/81 COMMFRCIAL OPERATION 8/01/81 7/30/81 (4/77 )
a DOCKE1NO.
50-364 s
UNIT J.M. Farley-Unit 2 11/04/82 i
DALE CO.stPLETE D 11Y W. G. Hairston, III i
1ELLfilONE (205)899-5156 October
.\\tCNill AVER AGE DA!Lh POWEli L EVEL DAY AVEllAGE D.\\ll.Y l'Oh Eit LEVEL '
DAY
(.'.the Net )
(.\\lWe Net) d 800 37 809 1
2 791 13 nna f
804 19 795 3
797 20 789 4
795 785 5
21 794 22 742 6
795 7 23 794 4 ]
g 796 25 '
9
, 796 26 10 796 '
gg 27 l2 794 23,
797 29 g3 14 806 30 809 33 15 806 16 I
e L'iSil UCllONS On t!nt formu.liu the moge daily umt powe-levelin htWe Net for each d:y in the reporimg monih. Compute to
, the neatne whule ne;r.mt.
1 j
0 (77) 1,
.,g
.r 3-6 8
s l
\\
UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-364 UNIT NAM E
.T. M. Farley-Unit 2 DATE 11/04/82 l
REPORT MONTil ocenhor _ 1982 COMPLETED BY L! r:. n if rs t on. III TELEPilONE (205) 899-5156 i
I i
I c
rs 3 so ~-
6 r
5 *4 liCCH5CC 54 8.4 2 _C E
9 c
Cause & Currective
~~u No.
Date g
3g
,3 g 5 Event
- s ?
3 Action to g
m-u Repor: #
v) U Eu Prevent Recurrence ggg g
O :::
a:
6 013 821022 S
217.3 C
1 NA NA NA Unit was taken off line for the i
Cycle I - Cycle II refueling outage.
l 1
l i
l l
i i
I i
2 3
4 F: Forced Reason:
Method:
Exhibit G Instructions S: Scheduled A-Equipment Failure (Explain)
I-Manual for Preparation of Data B Maintenance of Test 2 Manual Scram.
Entry Sheets for I.icensee C-Refueling 3 Automatic Scram.
Event Repini (1.ER) File (NUREG.
~
D Regulatmy Restriction 4 Other (Explain) 01611 E-Operator Training & license Examination F Adminisisative 5
G Opesatsunal Lesor (Explain) thlnbit 1 Same Sousee 19/77) ll Of hes (F aplain) i
.l
JOSEPH M. FARLEY NUCLEAR PLANT UNIT 2 NARRATIVE
SUMMARY
OF OPERATIONS October, 1982 In the month of October there was one unit shutdown on October 22, 1982, which initiated the Cycle I - Cycle II refueling.
The following safety-related maintenance was performed in the month of October:
1.
Performed miscellaneous maintenance on diesel generators.
2.
Repacked 2E Service Water pump.
3.
Repacked #7 River Water pump.
4.
Performed annual inspection on Spent Fuel Pool Cask crane.
5.
Repaired leaking Spent Fuel Pool check valve V013 (Pen. #95).
i l
i l
l
--n e-, -
n-----
-,n-,
--n-
--e
+ -,
4 STEAM GENERATOR TUBE PLUGGING Based on industry experience and past experience at FNP, the majority of Westinghouse steam generator tube leaks occur on the steam generator inner row tubes. Therefore, a management decision was made to plug all the inner row tubes of the three Unit 2 steam generators to prevent unplanned outages in the future. Also, titree additional tubes on Steam Generator 2A were plugged.
Dates of Plugging:
10/28/82 - 11/01/82 All (94) S/G 2A inner row tubes were plugged.
In addition, the three following tubes on S/G 2A were also plugged.
Row Column 28 10 29 11 30 12 All (94) S/G 2B inner row tubes were plugged.
All (94) S/G 2C inner row tubes were plugged.
i l
l 1
i
t OPERATING DATA REPORT DOCKET NO. 50-364 DATE 11/04/82 COMPLETED BY W.G.Hairston, III TELEPHONE (205)89f-5156 OPERATING STATUS
- 1. Unit Name:
J SePh M. Farley - Unit 2 Notes
- 2. Reporting Period:
October, 1982
- 1) Cumulative data since 2652 7/30/81, date of commer-
- 3. Licensed Thermal Power (MWt):
860 cial operation.
- 4. Nameplate Rating (Gross MWe):
- 5. Design Electrical Rating (Net MWe):
829
- 6. Maximum Dependable Capacity (Gross MWe):
854.7 813.7
- 7. Maximum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Items Nnmber 3 Through 7) Since Last Report. Give Reasons:
N/A
- 9. Power Level To Which Restricted. If Any (Net MWe):
N/A
- 10. Reasons For Restrictions,if Any:
N/A This Month Yr.-to-Date Cumulatise 745 7,296 11,017
- 11. Hours in Reporting Period
- 12. Number Of Hours Reactor Was Critical 528 6,346.2 10,032.4
- 13. Reactor Reserve Shutdown Hours 0
97.6 138.4
- 14. Ilours Generator On.Line 527.7 6,254.2 9,920.7 t
- 15. Unit Resene Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWH) 1.387,065 15,955,657 64,400,880 i
- 17. Gross Electrical Energy Generated (MWH) 441,252 5,102,520 8,173,898
- 18. Net Electrical Energy Generated (MWH) 417.138 4.832,614 7,753,334
- 19. Unit Senice Factor 70.8 85.7 90.0 70.8 85.7 90.0
- 20. Unit Asailability Factor i
- 21. Unit Capacity Facto IUsing MDC Net) 68.8 81.4 86.5 67.5 79.9 84.9
- 22. Unit Capacity Factor (Using DER Net)
- 23. Unit Forced Outage Rate 0.0 11.6 8.1
- 24. Shutdowns Scheduled Oser Next 6 Months (Type.Date and Duration of Eacht:
N/A 12/12/82
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
s'
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achiewd 5/06/81 5/08/81 INITI A L CRITICALITY INITIAL ELECTRICITY 5/24/81 5/25/81 COMMERCIAL OPEst ATION 8/01/81 7/30/81 (4/77 )
50-364 D00'El NO. _
UNIT J.M. Ferley-Unit 2 s,
11/04/82 DALE _
i W. G. Hairston, III CO.stPLETED BY T
1ELLPllONE (205)899-5156 October 3fCNill DAY AVERAGE DTil.Y l'Oh Eit LEVEL '
DAY AVERAGE D \\lLY POWI:!( L EVEL (MWe Net)
(.'.t h e-Ne t )
800 17 809 791 13 gn3 2
804 g9 795 3
789 797 20 4
785 _ _
~
795 y
742 794 22 6
< M 23 7
.s. g
- 4 794
]
796 25 '
9
. 796 '
26 10 796 n
it 794 23 12 -
797
- ,y 13
~ 806 30 g.g
- 809 3g g5 806 16 I
i i
i INSTTit1CilONS On this fornnt. list the asetsge daily unit power !cielin MWe Net for each d:y in the reposung inuaith.Coen
, the ficJtdt whoie si ;iwaii.
a e
(9/77)
- i O.,
.2 O
O e
4 0
i
. :~
e UNIT SilUTDOWNS AND POWER REDUCT10NS DOCKET NO. 50-364 UNI.' N AM E L M. Farlev-U11t 2 DATE 11/04/82 COMPLETED BY u c h irston. III l
REPORT MONTil ocenhor _ 1982 TELEPilONE (205) 89c-5156 l
I "i
Licensee Ev, fg
.! E 3
h Ek Cause & Correceive No.
Date R
ij g 2s5 Event u?
$q Action so 50
$E 5
j gg g Repor: #
Prevent Recurrence 6
013 821022 S
217.3 C
1 NA NA NA Unit was taken off line for the Cycle I - Cycle II refueling outage.
4 l
I 2
3 4
F: Forted Reason:
Method:
Exhibit G Instructions S: Scheduled A Equipment Failure (Explain) 1 Manual for Preparation of Dais il Maintenance or Test 2 Manual Scram.
Entry Sheets for Licensee C Refueling 3 Autonutic Scram.
Event Report (1.ER) File (NUREG.
D-Regulatiuy Resisiciion 4 Other (Explain) 0161i E-Operator Training & license Exainination F Administsative 5
G Opciational I.isos (linplam) lishibit I - Same Sousee 19/77) 11 Othes ll% plain)