ML20028A424

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Monthly Operating Rept for Oct 1982
ML20028A424
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 11/04/1982
From: Hairston W
ALABAMA POWER CO.
To:
Shared Package
ML20028A422 List:
References
NUDOCS 8211220124
Download: ML20028A424 (10)


Text

4 JOSEPH M. FARLEY NUCLEAR PLANT UNIT 2 NARRATIVE

SUMMARY

OF OPERATIONS October, 1982 In the month of October there was one unit shutdown on October 22, 1982, which initiated the Cycle I - Cycle II refueling.

The-following safety-related maintenance was performed in the month of October:

1.

Performed miscellaneous maintenance on diesel generators.

2.

Repacked 2E Service Water pump.

3.

Repacked #7 River Water pump.

4.

Performed annual inspection on Spent Fuel Pool Cask crane.

5.

Repaired leaking Spent Fuel Pool check valve V013 (Pen. #95).

l e

1m R

STEAM GENERATOR TUBE PLUGGING Based on industry experience and past experience at FNP, the majority of Westinghouse steam generator tube leaks occur on the steam generator inner row tubes. Therefore, a management decision was made to plug all the inner row tubes of the three l';it 2 steam generators to prevent unplanned outages in the future. Also, three additional tubes on Steam Generator 2A were plugged.

Dates of Plugging:

10/28/82 - 11/01/82 All (94) S/G 2A inner row tubes were plugged.

In addition, the three following tubes on S/G 2A were also plugged.

Row Column 28 10 29 11 30 12 All (94) S/G 2B inner row tubes were plugged.

All (94) S/G 2C inner row tubes were p' lugged.

OPERATING DATA REPORT DOCKET NO. 50-364 DATE 11/04/82 COMPLETED BY W.G.Hairston, III TELEPHONE (205)899-5156 OPERATING STATUS

1. Unit Name:

Joseph M. Farley - Unit 2 Notes

2. Reporting Period:

October, 1982

1) Cumulative data since
3. Licensed Thermal Power (MWt):

2652 7/30/81, date of commer-860 cial operation.

4. Nameplate Rating (Gross MWe):
5. Design Electrical Rating (Net MWe):

829

6. Maximum Dependable Capacity (Gross MWe):

854.7

7. Maximum Dependable Capacity (Net MWe):

813.7

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

N/A

9. Power Level To Which Restricted,If Any (Net MWe):

N/A

10. Reasons For Restrictions. If Any:

N/A This Month Yr.-to.Date Cumulative i1. Hours In Reporting Period 745 7,296 11,017

12. Number Of Hours Reactor Was Critical 528 6,346.2 10,032.4
13. Reactor Reserve Shutdown Hours 0

97.6 138.4

14. Hours Generator On.Line 527.7 6,254.2 9,920.7
15. Unit Reserve Shutdown Hours 0

0 0

16. Gross Thermal Energy Generated (MWH) 1.387,065 15,955,657 64,400,880
17. Gross Electrical Energy Generated (MWH) 441,252 5,102,520 8,173,898
18. Net Electrical Energy Generated (MWH) 417.138 4.832.614 7,753,334
19. Unit Service Factor 70.8 85.7 90.0
20. Unit Availability Factor 70.8 85.7 90.0
21. Unit Capacity Factor (Using MDC Net) 68.8 81.4 86.5 67.5 79.9 84.9
22. Unit Capacity Factor (Using DER Net)
23. Unit Forced Outage Rate 0.0 11.6 8.1
24. Shutdowns Scheduled Over Next 6 Months (Typc. Date,and Duration of Each1:

N/A

25. If Shut Down At End Of Report Period. Estimated Date of Startup:

12/12/82

26. Units in Test Status 1 Prior to Commercial Operation):

Forecast Achiesed

)

INITIA L CRITICALITY 5/06/81 5/08/81 INITIA L ELECTRICITY 5/24/81 5/25/81 COMMFRCIAL OPERATION 8/01/81 7/30/81 (4/77 )

a DOCKE1NO.

50-364 s

UNIT J.M. Farley-Unit 2 11/04/82 i

DALE CO.stPLETE D 11Y W. G. Hairston, III i

1ELLfilONE (205)899-5156 October

.\\tCNill AVER AGE DA!Lh POWEli L EVEL DAY AVEllAGE D.\\ll.Y l'Oh Eit LEVEL '

DAY

(.'.the Net )

(.\\lWe Net) d 800 37 809 1

2 791 13 nna f

804 19 795 3

797 20 789 4

795 785 5

21 794 22 742 6

795 7 23 794 4 ]

g 796 25 '

9

, 796 26 10 796 '

gg 27 l2 794 23,

797 29 g3 14 806 30 809 33 15 806 16 I

e L'iSil UCllONS On t!nt formu.liu the moge daily umt powe-levelin htWe Net for each d:y in the reporimg monih. Compute to

, the neatne whule ne;r.mt.

1 j

0 (77) 1,

.,g

.r 3-6 8

s l

\\

UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-364 UNIT NAM E

.T. M. Farley-Unit 2 DATE 11/04/82 l

REPORT MONTil ocenhor _ 1982 COMPLETED BY L! r:. n if rs t on. III TELEPilONE (205) 899-5156 i

I i

I c

rs 3 so ~-

6 r

5 *4 liCCH5CC 54 8.4 2 _C E

9 c

Cause & Currective

~~u No.

Date g

3g

,3 g 5 Event

s ?

3 Action to g

m-u Repor: #

v) U Eu Prevent Recurrence ggg g

O :::

a:

6 013 821022 S

217.3 C

1 NA NA NA Unit was taken off line for the i

Cycle I - Cycle II refueling outage.

l 1

l i

l l

i i

I i

2 3

4 F: Forced Reason:

Method:

Exhibit G Instructions S: Scheduled A-Equipment Failure (Explain)

I-Manual for Preparation of Data B Maintenance of Test 2 Manual Scram.

Entry Sheets for I.icensee C-Refueling 3 Automatic Scram.

Event Repini (1.ER) File (NUREG.

~

D Regulatmy Restriction 4 Other (Explain) 01611 E-Operator Training & license Examination F Adminisisative 5

G Opesatsunal Lesor (Explain) thlnbit 1 Same Sousee 19/77) ll Of hes (F aplain) i

.l

JOSEPH M. FARLEY NUCLEAR PLANT UNIT 2 NARRATIVE

SUMMARY

OF OPERATIONS October, 1982 In the month of October there was one unit shutdown on October 22, 1982, which initiated the Cycle I - Cycle II refueling.

The following safety-related maintenance was performed in the month of October:

1.

Performed miscellaneous maintenance on diesel generators.

2.

Repacked 2E Service Water pump.

3.

Repacked #7 River Water pump.

4.

Performed annual inspection on Spent Fuel Pool Cask crane.

5.

Repaired leaking Spent Fuel Pool check valve V013 (Pen. #95).

i l

i l

l

--n e-, -

n-----

-,n-,

--n-

--e

+ -,

4 STEAM GENERATOR TUBE PLUGGING Based on industry experience and past experience at FNP, the majority of Westinghouse steam generator tube leaks occur on the steam generator inner row tubes. Therefore, a management decision was made to plug all the inner row tubes of the three Unit 2 steam generators to prevent unplanned outages in the future. Also, titree additional tubes on Steam Generator 2A were plugged.

Dates of Plugging:

10/28/82 - 11/01/82 All (94) S/G 2A inner row tubes were plugged.

In addition, the three following tubes on S/G 2A were also plugged.

Row Column 28 10 29 11 30 12 All (94) S/G 2B inner row tubes were plugged.

All (94) S/G 2C inner row tubes were plugged.

i l

l 1

i

t OPERATING DATA REPORT DOCKET NO. 50-364 DATE 11/04/82 COMPLETED BY W.G.Hairston, III TELEPHONE (205)89f-5156 OPERATING STATUS

1. Unit Name:

J SePh M. Farley - Unit 2 Notes

2. Reporting Period:

October, 1982

1) Cumulative data since 2652 7/30/81, date of commer-
3. Licensed Thermal Power (MWt):

860 cial operation.

4. Nameplate Rating (Gross MWe):
5. Design Electrical Rating (Net MWe):

829

6. Maximum Dependable Capacity (Gross MWe):

854.7 813.7

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Nnmber 3 Through 7) Since Last Report. Give Reasons:

N/A

9. Power Level To Which Restricted. If Any (Net MWe):

N/A

10. Reasons For Restrictions,if Any:

N/A This Month Yr.-to-Date Cumulatise 745 7,296 11,017

11. Hours in Reporting Period
12. Number Of Hours Reactor Was Critical 528 6,346.2 10,032.4
13. Reactor Reserve Shutdown Hours 0

97.6 138.4

14. Ilours Generator On.Line 527.7 6,254.2 9,920.7 t
15. Unit Resene Shutdown Hours 0

0 0

16. Gross Thermal Energy Generated (MWH) 1.387,065 15,955,657 64,400,880 i
17. Gross Electrical Energy Generated (MWH) 441,252 5,102,520 8,173,898
18. Net Electrical Energy Generated (MWH) 417.138 4.832,614 7,753,334
19. Unit Senice Factor 70.8 85.7 90.0 70.8 85.7 90.0
20. Unit Asailability Factor i
21. Unit Capacity Facto IUsing MDC Net) 68.8 81.4 86.5 67.5 79.9 84.9
22. Unit Capacity Factor (Using DER Net)
23. Unit Forced Outage Rate 0.0 11.6 8.1
24. Shutdowns Scheduled Oser Next 6 Months (Type.Date and Duration of Eacht:

N/A 12/12/82

25. If Shut Down At End Of Report Period. Estimated Date of Startup:

s'

26. Units in Test Status (Prior to Commercial Operation):

Forecast Achiewd 5/06/81 5/08/81 INITI A L CRITICALITY INITIAL ELECTRICITY 5/24/81 5/25/81 COMMERCIAL OPEst ATION 8/01/81 7/30/81 (4/77 )

50-364 D00'El NO. _

UNIT J.M. Ferley-Unit 2 s,

11/04/82 DALE _

i W. G. Hairston, III CO.stPLETED BY T

1ELLPllONE (205)899-5156 October 3fCNill DAY AVERAGE DTil.Y l'Oh Eit LEVEL '

DAY AVERAGE D \\lLY POWI:!( L EVEL (MWe Net)

(.'.t h e-Ne t )

800 17 809 791 13 gn3 2

804 g9 795 3

789 797 20 4

785 _ _

~

795 y

742 794 22 6

< M 23 7

.s. g

4 794

]

796 25 '

9

. 796 '

26 10 796 n

it 794 23 12 -

797

,y 13

~ 806 30 g.g

  • 809 3g g5 806 16 I

i i

i INSTTit1CilONS On this fornnt. list the asetsge daily unit power !cielin MWe Net for each d:y in the reposung inuaith.Coen

, the ficJtdt whoie si ;iwaii.

a e

(9/77)

i O.,

.2 O

O e

4 0

i

. :~

e UNIT SilUTDOWNS AND POWER REDUCT10NS DOCKET NO. 50-364 UNI.' N AM E L M. Farlev-U11t 2 DATE 11/04/82 COMPLETED BY u c h irston. III l

REPORT MONTil ocenhor _ 1982 TELEPilONE (205) 89c-5156 l

I "i

Licensee Ev, fg

.! E 3

h Ek Cause & Correceive No.

Date R

ij g 2s5 Event u?

$q Action so 50

$E 5

j gg g Repor: #

Prevent Recurrence 6

013 821022 S

217.3 C

1 NA NA NA Unit was taken off line for the Cycle I - Cycle II refueling outage.

4 l

I 2

3 4

F: Forted Reason:

Method:

Exhibit G Instructions S: Scheduled A Equipment Failure (Explain) 1 Manual for Preparation of Dais il Maintenance or Test 2 Manual Scram.

Entry Sheets for Licensee C Refueling 3 Autonutic Scram.

Event Report (1.ER) File (NUREG.

D-Regulatiuy Resisiciion 4 Other (Explain) 0161i E-Operator Training & license Exainination F Administsative 5

G Opciational I.isos (linplam) lishibit I - Same Sousee 19/77) 11 Othes ll% plain)