ML20027C508

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Monthly Operating Rept for Sept 1982
ML20027C508
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 10/01/1982
From: Auterino L
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
Shared Package
ML20027C507 List:
References
NUDOCS 8210180091
Download: ML20027C508 (6)


Text

{{#Wiki_filter:(...- .A OPERATING DATA REPORT DOCKET NO. 50-286 DATE 10/1/82 COMPLETED BY L. Auterino TELEPHONE f oi 41 7'4o-8200 OPERATING STATUS es

1. Unit Name:

Indian Point No. 3 Nuclear Power Pi et

2. Reporting Period:

September 1982

3. Licensed Thermal Power (MWt):

3o25

4. Nameplate Rating (Gross MWe):

1013 965

5. Design Electrical Rating (Net MWe):

7

6. Maximum Dependable Capacity (Gross MWe):

926

7. Maximum Dependable Capacity (Net MWe):

891

8. If Changes Occur in Capacity Ratings (!tems Number 3 Through 7) Since Last Report. Give Reasons:
9.. Power Level To Which Restricted,If Any (Net MWe):
10. Reasons For Restrictions,if Any:

This Month Yr. to Date Cumulative' 720 6,551.0 53,352.0

11. Hours in Reporting Period 0

1,984.6 34,090.8

12. Number Of Hours Reactor Was Critical

-43. Reactor Reserve Shutdown Hours 0 0 0

14. Hours Generator On-Line 0

1.969.6 32.913.1 --{S. Unit Reserve Shutdown Hours 0 0 0 0 5,060,030 86.143.401-

16. Gross Thermal Energy Gener:ted (MWH) 0 1,502,170 26,298,300
17. Gross Electrical Energy Generated (MWH) 0 1,436,036 25,183.443 l

..18. Net Electrical Energy Generated (MWH) j

19. Ur.it Service Factor 0

30.1 61.7

20. Unit Availability Factor 0

3(). ]_ 61.7

21. Unit Capacity Factor (Using MDC Net) 0 2a.6 53.0 0

22.7 48.9

22. Unit Capacity Factor (Using DER Net)
23. Unit Forced Outage Rate 0

2.3 la.3

24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each):

4 ~ Refuelino outace in prooress. Upon completion of scheduled 25, if Shut Down At End Of Report Period. Estimated Date of Startup: maintenanco Fet. dato (,la n AM

26. Units in Test Status (Prior to Commercial Operation):

Fcrecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPER ATION 8210100091 820912 PDR ADOCK 05000286 R PDR L9/77 )

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-286 Indian Point UNIT Mn 3 10/1/82 DATE COMPLETED BY L. Auterino TELEPHONE (914) 739-8200 MONTH September 1982 DAY-AVERAGE D. PMR LEVEL DAY AVERAGE DAILY POWER LEVEL I

  1. "*' E 0

0-1 17 2 0 I8 0 0 3 19 0 0 0 4 20 0 0 5 21 0 0 6 22 0 0'~ ~ - - ~ ~ ~ - ~ ~ ~~ ~ ~~ 7 0 0 8 24 9 0 0 3 0 0 10 26 0 0 11 27 0 0 12 3 13 0 0 29 0 14 30 0 0 15 3l 16 0 INSTRUCTIONS On this format. list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole rnegawatt. (9/77)

g UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-286 UNITNAME Ind ian Point No. 3 DATE 10/1/82 REPORT MONTil September 1982 COMPLETED BY L. Auterino TELEPIIONE (9141 739-8200 ~ e. E E u .E g } }.E 5 Licensee E* je. Cause & Corrective No. Date g 3g ,s& Event p gO Action to '8 H fE - 5 3g3 Report # mO Prevent Recurrence c e o .c 38 O 3 04 82/03/25 S 720 B&C N/A N/A N/A Unit in a scheduled cycle III-IV refueling and maintenance outage. I 2 3 4 F: Fr :ed Reason: Method: Exhibli - Inst ructions S: SJ.icduled A Equipment Failure (Explain) 1 Manual for Preparation of Data B Maintenance or Test 2 Manual Scram. Entry Sheets for Licensee 'C-Refueling 3-Automatic Scram. Event Report (LER) File (NUREG-D Regulatory Restriction 4-Other (Ernlain). 0161) E-Operator Training A License Examination ~ ~ F Administrative 5 G-Operational Error (Explain) Exhibit, Same Source (9/77) Il-Other (Explain)

HONTilLY MA'INTENANCE REPORT ..e September 1982 Month h'R a DATE EQUIPMENT MALFUNCTION CORRECTIVE ACTION ~ ~ I-3012 9-23

  1. 32 Fan Cooler Unit Air Jams in Mid-Position Disassembled and cleaned pivot point Damper "D" I-3032 9-23
  2. 32 Fan Cooler Unit Air Frozen in open position Disassembled and Cleaned pivot point Damper "B"
  3. 32 Fan Cooler Unit Air Limit switch inoperable Tightened limit switch Damper "C"
  4. 32 Fan Cooler Unit Air Limit switch inoperable Tightened limit switch,

Damper "D I-3047 9-20 Fuel Storage Bldg. Crane Main hoist inoperable Replaced worn electrical contacts J b e o Q q l*f' e e

HONTIILY I & C CATEGORY I REPORT September 1982 ~ ~ ~ ' Month W.H. No. DATM EQUIPMENT HALFUNCTION CORRECTIVE ACTION IC-I-287-3B 11-29-79 R-7 Incore Instrument No response to Check-Source Repaired loose ccnnection dn Check-source solenoid Room Area Monitor IC-1-347-lC 4-23-82 LC-427GY Steam Generator Contact Failure Replaced Relay Low Level Protection Test Relay IC-1-942-2 12-20-81 3-PIA-1053 Small Gas No output from transmitter Replaced pneumatic relay decay tank pressure indicator ) IC-1-1019-3C 10-29-80

  1. 32 Static Inverter No output from power Replaced defective zener diode module IC-1-1077-2 2-10-81 Nuclear Instrumentation Flux alarm driver trans-Replaced transformer system computer and rate former defective drawer IC-1-1686-2 8-18-82 RE-101 Area Radiation Spiking of Alarms Repaired broken wire from switch Monitor for Saw=ge to circuit board Treatment Pldrit IC-1-1702-2 8-18-82 RE-101 Area Radiation Spiking of Alarms Repaired broken wire from switch Monitor for Sewage to circuit board Treatment Plant 0

SUMtMRY OF OPERATING EXPERIENCE Indian Point Unit 3 remained shutdown for the entire reporting period. Unit repairs, modifications and preventive maintenance is proceeding as scheduled. Preoaratory work for steam generator sleeving and girth weld repairs are.in progress. g .}}