ML20024G699

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Denies 901218 Application & Affidavit in Support of Withholding Response to Violations/Nonconformances Noted in Insp Rept 99900031/90-01 (Ref 10CFR2.790)
ML20024G699
Person / Time
Issue date: 04/10/1991
From: Grimes B
Office of Nuclear Reactor Regulation
To: Bolleter U
SULZER BINGHAM PUMPS, INC.
References
REF-QA-99900031 EA-90-122, NUDOCS 9104250345
Download: ML20024G699 (6)


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10 CFR 50.73 PHILADELPHI A ELECTRIC COMPANY LIMERICK GENER ATING ST ATION P. O. DOX A B AN ATOG A, PENNsV LV ANI A 19464 (216) 327 1200 s at. anon

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April 23,1991 Docket Nos. 50-352 50-353 License Nos. NPf-39 NPf-85 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555

SUBJECT:

Licensee Event Report Limerick Generating Station - Units _j and */

This LER reports an in advertent actuation of the Unit 2 Priniary Containment and Reactor Vessel isolation Control System and a Secondary Containment isolation. Engineered Safety features, which occurred due to a loss of power. A fuse blew during testing of the Division 111 125 VDC Safeguard Battery Charger which is suspected of causing a trip of a 2A Reactor Protectton System /Uninterruptible Power Supply distribution panel power supply breaker.

Reference:

Docket Nos. 50-352 50-353 Report Number:

2-91-002 Revision Humber:

00 Event Date:

March 24, 1991 Report Date:

April 23, 1991 facility:

Limerick Generating Station P.O. Box A, Senatoga, PA 19464 This LER is being submitted pursuant to the requirements of 10 CfR 50.73(a)(2)(iv).

Very truly yours, e

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T. T. Martin, Administrator, Region 1. USNRC

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On March 24.'1991, while Unit 2 was shutdown. various actuations of the Unit 2 Primary Containment and Reactor Vessel isolation Control System and a Unit 2

-Reactor Enclosure Secondary Containment isolation occurred. These are Engineered Safety feature actuations. The actuations are suspected to be the result of a blown 300 amp fuse in the Division Ill 125 VDC circuitry during load testing of the Division Ill Safeguard Battery Charger. This blown fuse caused a transient condition in the DC control power to the second of two sets of undervoltage and overvoltage relays for the 2A Reactor Protection System /UninterruptiblePowerSupply(RPS/UPS)distributionpanelpowersupply breakers.. The loss of. control power is suspected of causing;one of the

protective relays to trip resulting in a trip of the associated RPS/UPS:

distribution panel. power supply breaker.: The power supply breaker was reclosed and.the 2B loop of Shutdown Cooling was returned to service within 24 minutes.

All systems responded _as designed during the loss of power. The primary cause of the blown fuse was a lack of information from the manufacturer of a battery capacity test system used to test battery chargers. The appropriate battery

-charger test procedures will be revised to require testing to be performed with the test equipment in the proper mode.. The cause of the trip of the 2A RPS/UPS distribution panel power supply breaker is still under investigation and the results will be provided in a supplement to this LER.

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Unit 2wasinOperationalCondition4(ColdShutdown)at0%powerlevel. The

'B' loop of the Residual lleat Removal (RHR) (Ells:00) system was in service in the Shutdown Cooling Mode with Reactor Coolant temperature at 124 degrees f.

The Unit 2 Division til 125 VDC Safeguard Battery 18 month inspection was being performed.

Unit I was in Operational Condition 1 (Power Operation ) at 100X power level.

Description of the Event:

On March 24, 1991, at 1833 hours0.0212 days <br />0.509 hours <br />0.00303 weeks <br />6.974565e-4 months <br />, various actuations of the Unit 2 Primary Containment and Reactor Vessel isolation Control System (PCRVICS) (Ells:JM), and a Unit 2 Reactor Enclosure Secondary Containment isolatton occurred. These are Engineered Safety feature (ESF) actuations. These actuations occurred while utility employed Instrumentation and Controls (It,C) Technicians were performing SurveillanceTest(ST)procedureST-4-095-923-2,"Divisiontil125VDCSafeguard Battery 18 Month inspection." The actuations are suspected to be the result of a blown 300 amp fuse in the Division ill 125 VDC circuitry in fuse box 200105 which blew during load testing of the Division til 125 VOC Safeguard Battery Charger (seefigure1). This blown fuse caused a transient condition in the DC control power to the second of two sets of undervoltage and overvoltage relays for the 2A Reactor Protection System Uninterruptible Power Supply (RPS/UPS)

DistributionPanel(2AY160)powersupplybreakers. The loss of control power is suspected of causing one of the voltage relays to trip resulting in a trip of the associated 2A RPS/UPS distribution panel power supply breaker. This breaker trip resulted in a loss of power to the 2AY160 Panel. Main Control Room (MCR) operations personnel immediately received an "A Channel RPS Out of. Service" annunciation and other annunciations associated with the loss of power to the 2A RPS channel as a result of the blown fuse in fuse box 200105.

This loss of power resulted in isolation of the following Unit 2 systems or subsystems by closing their inboard primary containment isolation valves:

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'B' loop-of RHR in the Shutdown Cooling mode, o

DrywellChilledWater(DWCW)(E!!S:KM),

o Reactor En::losure Cooling Water (RECW) (Ells:CC),

o Primary Containment Instrurint Gas (PCIG) (Ells:LK). and o

Reactor Water Cleanup (RWCU) (Ells:CE).

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a un s w,, m lhe following system lines received isolation signals but no valve motton occurred since the associated valves were in the normally closed position:

o Unit 2 RHR heat exchanger vacuum breaker (Ells:VACB) lines, o

Unit 1 and Unit 2 Primary Containment Nitrogen inerting, o

Unit I and Unit 2 Primary Containment Purge Supply and Exhaust. and o

Unit I and Unit 2 Primary Containment Exhaust to Reactor Enclosure Equipment Compartment Exhaust.

The following ESf's also initiated as designed due to the loss of RPS power.

The Unit 2 Reactor Enclosure (RE) Heating Ventilation and Air Conditioning (HVAC)systemisolated. The 'A' trains of the Standby Gas Treatment System (SGTS) (Ells:BM), a common plent system, and the Unit 2 Reactor Enclosure Recirculation System (RERS) (Ells:VA) automatically initiated thus completing the Unit 2 RE Secondary Containment isolation.

Licensed MCR operators immediately entered fvent (E) Procedure E-2AY160, " Loss of '2A' RPS and UPS Power," Off Normal (0N) Procedure ON-ll3, " Loss of RECW "

and General Plant (GP) Procedure GP-B ' Primary and Secondary Containment Isolation Verification and Reset." The 2A RPS/UPS distribution panel power supply breaker was reclosed and the 28 loop of Shutdown Cooling was returned to service at 1857 hours0.0215 days <br />0.516 hours <br />0.00307 weeks <br />7.065885e-4 months <br />. The elapsed time of this event was 24 minutes.

The Division 111 125 VDC Safeguard battery was inspected and tested to ensure that no damage had occurred as a result of blowing the 300 amp fuse, inspection of the affected bus section, cabling and connections was performed and no sign of damage was identified. Data taken for cell voltage, specific gravity and ductor readings were within acceptable limits.

A four hour notification was made to the NRC at 2204 hours0.0255 days <br />0.612 hours <br />0.00364 weeks <br />8.38622e-4 months <br /> on March 24, 1991, in accordance with the requirements of 10CFR 50.72(b)(2)(ii), since this event resulted in automatic ESF actuations. This report is being submitted in accordance with the requirements of 10CFR 50.73(a)(2)(iv).

Analysis of the Event:

All systems responded as designed during the loss of RPS power to panel 2AY160.

During the 24 minutes that shutdown cooling was not in service, reactor coolant temperature increased approximately 17 degrees from 124 degrees to 141 degrees.

The maximum reactor coolant temperature allowed by Technical Specifications (15) is 200 degrees while in Operational Condition 4.

Operations personnel had ample time to restore shutdown cooling prior to exceeding the TS limit since it would have taken approximately one hour and 20 minutes to reach this temperature limit. Additionally, the redundant loop of shutdown cooling was oper4 ale in the event that the 'B' loop could not be restored to operation.

The isolation of

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m s.o.-. w.mn the.0WCW system, the RECW system, and the PClG system had no affect on plant operations since'the plant was shutdown for refueling. There was no release of radioactive material to the environment as a result of this event.

If this event had occurred during full power operation, the potential exists that this event could have resulted in securing of the Reactor Recirculation Pumps followed by a plant shutdown if immediate corrective actions were not taken quickly enough by-licensed MCR operati6ns personnel. Plant shutdown could have also been required due to Drywell temperature and pressure-increases as a result of'the isolation of DWCW and the loss of Drywell cooling. Additionally, if the PCIG system were left out-of-service for a long period of time, the Main SteamisolationValves(MSIVs)couldhavedriftedclosed.

immediate and follow-up actions for this type of event, loss of power to an RPS power distribution panel, are provided in procedures E-2AY160, OH-ll3, and GP-8.

Licensed MCR operators receive requalification training to-review and practice 4

responses to simulated plant transients of this type. This training reinforces immediate operator actions, minimizing the time that systems are isolated, and reducing the impact on the plant. Therefore, as a result of this adequate procedural guidance, training, and prompt operator actions, the consequences of this type of event were and would be minimized.

Cause of the Event:

The cause of:the ESF actuations was due to the loss of power to the 2A RPS/UPS Distribution Panel'when one of the power supply breakers for this panel tripped.

The actuation logics of the affected ESfs perform their safety function upon loss of power, and hence, the system isolations and actuations occurred. The cause of the trip of the RPS distribution panel power supply breaker is suspected to be related to the blown fuse 300. amp in the Division Ill Safeguard 125 VDC circuit since no other power transients occurred prior to the event and 1

the Division =lli 125 VDC circuit provides control power to the two protective relays for'the breaker that tripped.

The primary cause of the blown-fuse was a lack of information from Alber Engineering, Inc., the manufacturer of the BCT-1000 Batte.*y Capacity Test System, concerning the limitations of the use of this test equipment in the automatic mode while testing battery chargers. When used in the !AUT0' mode

-during performance of procedure ST-4-095-923-2 on the battery charger, the micro-processor in the BCT-1000 detected changes in voltage as a result'of be_ing connected to a rectified A.~C. voltage source (i.e. the battery charger and the battery). :The microprocessor in the BCT-1000 responds to a 9 millivolt change in the DC voltage being monitored. Voltage signal ripple on the output of the

' battery charger caused the computer memory to saturate and the test equipment to

-lose control of the current flow through the test equipment. A sharp increase in current flow through the test equipment exceeded the capacity of the battery charger-and drew excessive current from the battery.

This caused the 300 amp-fuse in the battery output circuit to blow.- After the initial transient, the

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The cause of the trip of the 2A RPS/UPS distribution panel power supply breaker is still under investigation. The overvoltage and undervoltage relays are designed to " fail-as-is" on a loss of control power. During this event, one of the relays apparently caused the power supply breaker to trip, although no flags indicating the cause for the trip were displayed on either of the relays.

Testing has been performed on the undervoltage and overvoltage relays and both functioned properly. The 125 VDC spiking which occurred during this event was simulated during bench testing and the breaker trip could not be duplicated.

The relays have been reinstalled in the circuit and have successfully passed a calibrational/ functional surveillance test and are considered operable. No previous relay trips of this type have been experienced at Limerick Generating Station. The investigation into the breaker trip is on going and the manufacturer of the relays, Asea Brown Boveri, will be consulted. The results of the investigation will be provided in a supplement to this LER to clarify the cause and address any additional corrective actions. The supplement to this LER is expected to be submitted by July 23, 1991.

Corrective Actions:

The following Unit 1 and Unit 2 procedures for divisional safeguard battery 10-month _ testing and preventative maintenance will be revised.

The procedures will require battery charger testing to be performed with the BCT-1000 test equipment in the ' MANUAL' mode:

ST-4-095-921-1 ST-4-095-921-2 ST-4-095-922-1 ST 4-095-922-2 ST-4-095-923-1 ST-4-095-923-2 ST-4-095-924-1 S1-4-095-924-2 and PMQ-095-001.

Unit 2 procedures scheduled to be performed have been revised prior to performance and all indicated procedures are expected to be permanently revised by June 21, 1991.

A letter has been sent from the plant staff to Alber Engineering, Inc., the test equipment manufacturer. This letter recommended that Alber include the information that clearly describes the limitations of the use of the BCT-1000 test equipment on battery chargers in their instruction manual. Additionally, an Operating Experience Report on this event has been issued on the INP0 Nuclear Hetwork.

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~<nec w w einn Previous Similar Occurrences:

Several LERs reported PCRVICS isolations due to loss of power to the RPS panel i

however, none were due to the same cause as the event reported in this LER.

Therefore, the corrective actions implemented for these events could not have prevented this event.

Tracking Codes: X3: Test Equipment malfunct' ion or misapplication 0: Procedure Deficiency i

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DI V. 111 BATTERIES BATTERY CHARGER

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A 2A RPS POWER BUS

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