ML20024G106

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Insp Rept 50-263/75-01 on 750115-17.Noncompliance Noted: Detailed Written Procedures Not Prepared for Insp & Repair of Loop a RHR HX in Progress on 750117
ML20024G106
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 02/11/1975
From: Dance H, Kohler J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20024G105 List:
References
50-263-75-01, 50-263-75-1, NUDOCS 9102070536
Download: ML20024G106 (9)


See also: IR 05000263/1975001

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U. S. NUCLEAR REGULATORY COFDilSSION

DIRECTORATE OF REGULA ?ORY OPERATIONS

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REGION III

Report of Operations Inspection

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IE Inspection Report No. 050-263/75-01

Licensee:

Northern States Power Company

414 Nicollet Mall

Minneapolis, Minnesota

55401

Monticello Nuclear Generating Plant

License No. DPR-22

Monticello, Minner.ota

Category:

C

Type of Licensee:

BWR (GE) 575 Mwe

Type of Inspection:

Routine, Announced

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Dates of Inspection:

January 15 - January 17, 1975

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Dates'of Previous" Inspection:

December 26-27,1974 (REP)

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Principal Inspector:

J . E. Kohler

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(Date)

Accompanying Inspector:

H. C. Dance

Other Accompanying Personnel:

None

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Reviewed By:

H. C. Dance

Senior Reactor Inspector

'(Da't e )

Reactor Operations Branch

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9102070536 750212

PDR

ADOCK 05000263

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SUMMARY OF FINDINGS

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Enforcement Action

The following noncompliance item was noted during the inspection.

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Violations:

None.

Infractions

Technical Specification 6.5.C. states that detailed written procedures,

including the applicable check-off and instructions, chall be prepared

and followed for preventive or corrective maintenance of plant equipment

and systems that could have an effect on nucicar safety.

Contrary to the above, detailed written procedures had not been prepared

for the inspection and repair of the "A" Loop Residual Heat Removal Heat

Exchanger in progress on January 17, 1975.

This infraction was identified by the inspector and had the potential

for causing or contributing to an occurrence with safety significance.

Deficiencies: None.

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Licensee Action on Previously Identified Enforcement Items:

Not applicable.

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Unusual Occurrences:

None.

Other Significant Findings: None.

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.anatemert Interview

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At the conclusion of the inspection the inspectors met with Messrs. C.

Laraon, Plant Manager: M. Clarity, Superintendent Plant Engineering and

Radiation Protection: W. Anderson, Superintendent Operations and Main-

tenance; and D. Antony, Plant Engineer, Operat ' >ns; and discussed the

following:

1.

The inspector stated that the failure to have a procedure detailing

repair plans of the No. 11 RHR Heat Exchanger was considered an

inf raction to Technical Specifications 6.5.C.

The licensee indicated

corrective action would be taken.

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2.

The inspector stated that review of the May 1974 startup check-

sheets did not indicate if identified abnormalities had been

corrected, such an locking requited valves or by issuance of

WRA's.

The review also indicated revisions may be in order for

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several checksheets. The licensee stated that data sheets are

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completed and reviewed within the guidelines provided in Operations

Manual Volume C.1.

The licensee indicated a review would be made

of the checksheets in view of the above comments.

3.

The inspectors discussed with the licensee preliminary comments per-

taining to the proposed standardized technical specifications for

engineered safety feature filtration systems.

The licensee plans

to submit his comments to the Directorate of Licensing.

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REPORT DETAILS

1.

Persons Contacted

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C. Larson, Plant Manager

M. Clarity, Superintendent, Plant Engineering and Radiation Protection

W. Anderson, Superintendent, Operation and K11ntenance

W. Sparrow, Operations Supervisor

W. Shamla, Plant Engineer, Technical

D. Nevinski, Engineer

J. Henage, Engineer

D. Antony, Plant Engineer, Operations

B. Day, Engineer

J. Pasch, Engineer

L. Eliason, Radiation Protection Engineer

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P. Krumpus, Quality Assurance Engineer

D. Shea, NUS Corporation

L. Lieber, General Elcetric Company

J. Zilinski, General Electric Company

2.

Present Plant Status

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The Monticello Generating Station is. presently shutdown for

refueling and inspection of Jet Pumps, 4 inch recirculation

This refueling outage was

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piping, and feedwater spargers.,Ed, because+ fuel" performance...va-

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earlier than had been anticipat

as indicated by higher than normal off-gas release rates',

required lower power operation to minimize fuel deterioration.

Presently the core consists of three types of fuel assemblies.

They are the original 7 x 7 fuel, improved 7 x 7 fuel with

champhored pellet design, and the new 8 x 8 matrix fuel.

The

core contained 116 8 x 8 fuel assemblies prior to the present

refueling outage, and 80 additional 8 x 8 fuel assemblies are

scheduled to be inserted in the core to replace leaking or orig-

Burnup on the lead asacably as of January 9, 1975, was

inal fuel.

about 15,000 mwd /t, while the average burnup was about 13,897 mwd /t.

Detection of leaking fuel assemblies was done in the fuel storage

Because

pool by sipping and analyzing the coolant for Xe-136.the end of the

the fuel sipping investigation was not completed at

inspection, the following information was obtained from the

licensee by telephone on January 24, 1975:

A total of 54 fuct assemblica (all 7 x 7) were identified as

a.

Of these 54 assemblies, 42 were positively ident-

leaking.

ified as leaking, giving a full scale reading on radiation

monitoring equipment, and 12 assemblies were suspected of

leaking.

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b.

The configuration of the core at the end of the present

refueling outage, January, 1975, will be 168 of the

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o-iginal 7 x 7 fuel assemblies, 20 of the improved 7 x 7

fuel, and 196 of the 8 x 8 fuel assemblies.

The earliest date at which the entire core will be composed

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of 8 x 8 fuel is scheduled to be Septemocr, 1975.

3.

Reactor Refuelinn Activities

The inspector verified that Technical Specifications 3.10 and

a.

4.10 were incorporated in the detailed procedures in use for

the refueling outage,

b.

The Shif t Supervisor's Log and Control Room Log was reviewed

from January 9 to January 15, 1975.

No deficiencies were noted.

Drywell deinerting was noted to have been initiated as permitted

by technical specifications prior to the reactor shutdown. On

January 13, 1975, the fuel handling gripper was noted to b

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been successfully tested with a simulated 1,500 lb. load,

The normal vertilation system was maintaining secondary con-

c.

tainment in the reaccor building by drawing a vacuum of at

least .25 inches water gauge differential pressure. The

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standby-gan treatment system was successfully tested on

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January 10, 1975, prios to the present. outage, as called for

in Technical Specification 4.7.C.1.d.

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procedures were reviewed confirmir,c th:.t the refueling

interlocks were successfully tested on JaL aary 13, 1975.

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c.

The inspector confirmed that the control room was in constant

communication with personnel perfortaing the refueling opera-

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tions through telephone and Di radio,

f.

The inspector reviewed the licensee's method of progranming

fuel aasembly moves during the refueling.

The fuel moves

planned were determined by members of the nucicar technical

staff. The fuel movement procedure was then checked by a

computer program that verified the configuration of fuel in

the core and the fuel storage pool.

The program was abic

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to detect any logic errors. This was demonstrated during

the inspection. Once the logic for a particular fuel move

was accepted h/ the computer, it van printed cut in copien

of four, and became the master procedure used on the

refueling bridge, defining the nequence of fuel assembly

moves to take place. Logic of the sequence of fuel troves

was independently verified by two members of the nuclear

technical staff prior to approval,

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The inspectors verified that the core was accurately identified

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schematic diagrams located on the refueling floor, and

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in the nucicar staff office. All fuel movement done on tha

refueling bridge was followed in the control room with an

identica.1 fuel movement procedure list.

Fuel inspec'tions of designated assemblies were performed by

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members of the Cencral Electric Company. Visual inspection

of individual fuel rods as well as eddy current and ultrasonic

testing of selected f uel rods was being performed.

1.

The inspectors verified that fuel sipping activities, to

determine Icaking ! ;' assemblies, was perf ormed in accord-

How-

ance with approved fuel sipping procedures No. 9008a.

ever, no acceptance criteria was set to establish tbc lower

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limit of marginal leaking fuel assemblies.

The licensee had prescheduled all activ'ities expected during

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the outage and was updating daily the activities for the next

three days. Review of the major maintenance activities estab-

lished that procedures existed f or the bulk of activities,

such as required surveillancs tests. safety /rcifef valve

pilot and in-place leakage tests, and control rod drive over-

haul.

An exception was noted in the case of the No. 11 RHR

Heat Exchanger inspection to determine cause of internal

leakage. No procedure existed describing the proposed plan

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of inspection or repair. Discussion with supervisory person-

nel established that a vendor's manus 1 and drawing were7e*

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available and a verbal plan of approach was established.

The

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heat exchanger is manuf actured by Perfiex and is of a two pass

floating head design.

The Work kcqucst Authorization listed

the valve positioning and tag requirements, but no other require-

ment cuch c.s testing.

The absence of a maintenance procedure

is contrary to Technical Specification 6.5.C which requiren

detailed written procedures to bc prepared and followed for

prevention or corrective maintenance of plant equipment and

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systems that could have an ef fect on nuclear safety.

4.

The inspectors confirmed the following activities during refueling:

Core monitoring in the control room during refueling operations

a.

in accordance with Technical Specification 3.10(b) and 4.10(b).

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b.

Containment integrity was main *ained in accordance with

Technical Specification 3.8.C defining the requirements for

maintaining secondary containment integrity.

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c.

Fuel movement of at least two fuel bundles was conducted

in accordance with established procedure specified by the

cottputer printed fuel movement sequence list.

d.

Core internals, Icads, and vessel studs were stored to pro-

tect ar,ainst damage,

llousekeeping on the refueling deck and bridge as well ar.

c.

radiation protection requirements were acceptable.

f,

in accordance with Technical Specification 6.1.C the coniposition

of the crew on the ref ueling deck and in the cont rol room

was acceptable,

n.

In accordance wit h Technical Spacification "l.10.C f uel pool

storane water level was inaintained at a level of at least

33 feet.

h.

As required by Technicial Specification 3.10.A the reactor node

switch vac locked in the ref uel position during the refueling.

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Control blade reinoval checks were confirtned to be included

on the fuel novement sequence sheets.

5.

Startun ,Proced,urey

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The inspector confirmed"that selected startup procedures were com '

pleted in mid May 1974, the previous refuelinp outate.

The systems

confirmed were the recirculat ion, nuclear instrumentation, condensate

and f eedwater, control reid drive, and the core spray.

Several

notations of snecific plant status were noted on the procedures

and check lists reviewed, but no nathod uas available to confirm that

the anomalics had been corrected or revisionr. to the data t.heets

made. The licensee indicated this area would be reviewed.

The

licensee also indicated that similar system checks are performed

durint refuelinn outages, et.rrently in progrees, to estahlinh that

system lineups are proper.

In addition, the inspector confirmed

that the system check lists had been conpleted and that both

control rod drive sequences with a predicted critical rod pos-

ition were available prior to the startup.

6.

Vencel internaln

The inspector 3 witnessed a portion of the jet pump insnection being

performed with t he aid of an underwater television camera and beinp,

recorded on tapes.

flenolut ion van good. Gl personnel. responsible

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for the inspection stated no abnormal conditions were noted on

either the jet pumps or the f eedwater spargers.

.Sa_f_ety/ Relief Valves (S/RV)

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The inspector reviewed the licensee's increased / surveillance as

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a result of the S/RV premature of extended operation.

Temperature

plots (approximately 4 per week) are being maintained by the engineer

responsibic for the S/RV offluent lines. To improve sensitivity,

the licensee plann to relocate four thercocouples presently located

6-12 inches from the valve discharge flange, to a 22 5/8" location,

conenon to the four newiv" installed (5/74) ef'1uent lines.

A temocr-

ature range of about 12'0 - 250"F has been experienced on the 600 F

recorder.

A common alarm point is in use.

Procedures had been

prepare l and work scheduled f or the it. place testing of the first

stage pilots on the S/RV's this outane.

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Control Rod Driven

The inspector confirmed that procedures existed for replacement of

25 CRD 4 during the outage.

Included in the CLD replacement will

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be the

ist four drives, with one nil inner screens (other CRD's

have ten mil screen sir.e.)

Review of recordn indicated scram

times for 90% int.crtion on three of the drives with one mil screen

vere 3.63 to 4.45 seconds compared to an average of 2.60 seconds

for the,50% sampling of other CRD's taken in November 1974. All

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of the above scram times are within requirements of Technical Specification 3.3.C.

Two of the core's 121 CRD's have modified

inner screens nounted on the stop pisten.

The licensee stated

no problems have been experienced with these irives, and that

current plans do not include such modification on other drives.

9.

Standhv Cas Treatment Sv a t em _(SGTS1

In accordance with Surveillance RequircrTnt 4.8.b, the inspector

confirmed that the SG'IS was tested on knuary 1975,11ay 1974

November 1974 and found that the filters were freon tested at

'? 99% removal efficiency and the llEPA filters were DOP tested

at ) 99% rernoval efficiency.

The inspector also reviewed with the utility their preliminary

comments on the proposed standardized technical specifications for

enginected safety features filtration systems to be r.ubmitted to

Licensing for review.

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Ltr Mager to O'1,eary, dtd 11/25/74 (A0 263/74-24).

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UNITE D' $1 Af t $

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NUCLEAR REGULATORY COMMIS$10N

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OFFICE OF INSPECTION AND ENFORCE!!ENT

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REGION lll

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799 noottvrLt noAp

OLEN ELLYN. ILLit40ll 40437

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IE Inspection Report No.

n e n_ g3 p e_n1

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Tranornittal Date

February 12 ; 1(175

Distribution:

Distribution:

IE Chief. FSLEis

IE Chief. FSLEB

IE:l!Q (5)

IElllQ (4)

DR Confrni Tiins

L D/D for Fucis & Materials

Regulatory Standards (3)

DR Central Files

' Licensing (13)

IE Files

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IE Files

IE Chief ,11LPPB

L:D/D for Reactor Project

B.

IE Inquiry Report No.

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Transmittal Date

Distribution:

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4, *Dist.ribution:

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IE Chicf, FS&EB

TE Cliief.4 FS&EB

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IE:11Q (5)

IE UQ

DR Central Files

DR Central Files

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Regulatory Standards (3)

IE Files

!

Licensing (13)

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IE Files

C.

Incident Notification From:

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(Licenuce 6 Docket No. (or License No.)

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Transmittal Date

Distribution:

Distribution:

IE Chief , FS6EB

IE Chief , FS;EB

IE:11Q (4)

IElllQ (4)

Licenning, (4)

L:D/D for Fueln 6 Materials

DR Central Files

DR Central F13 cs

IE Files

IE Files

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