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LER-1983-016, /03L-0:on 830405,MSIV Drain Valve 2B21-F016 Would Not Close.Caused by Dirty Torque Switch Contacts.Contacts Disconnected,Cleaned & Retightened.Valve Cycled Properly |
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| 3661983016R03 - NRC Website |
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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (7 77)
LICENSEE EVENT REPORT CONTROL BLOCK: l l
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60 ti DOCKET NUMBER 68 69 EVENT DATE 74 76 REPORT DATE 80 m l HNP-2-3109 "MSIV DRAIN VALVE LSFT" h EVENT DESCRIPTloN AND FRoBABLE CONSEQUENCES procedure was in progress. Logic was l
initiated to close drain valve 2821-F016. Indicator lamps on the con-l Io iai I
,,,,, ; trol panel 2Hll-P602 gave a double indication. It was determined that l
valve 2B21-F016 would not close and, therefore, would not meet the re-
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l O l6 l l Quirements of Tech. Specs. Section 3.6.3.2. The valve was placed in the
- o,,i l open position and the test terminated. The health and safety of the g
public were not affected by this non-repetitive event.
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,,,o,l The valve would not close because of dirty contacts on the torque j
swJtch. The contacts were disconnected, cleaned, and re-tightened.
The
,,,,jg valve was then cycled properly by using its control switch.
The logic system functional test HNP-2-3016 was resumed and completed
,,,3, successfully.
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REMASED OF RELEASE liTil L.ZJ @ lZ jgl NA l
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PERSONNEL EXPOS ES NUMBER TYPE
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NAME OF PREPARER PHONE:
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NARRATIVE
REPORT FOR LER 50-366/1983-016 LICENSEE
- GEORGIA POWER COMPANY FACILITY NAME
- EDWIN I.
HATCH DOCKET NUMBER
- 50-366' Tech. Specs. section(s) which requires report:
This 30 day LER is required by Tech. Specs. Section 6.9.1.9.b due to the event's showing that tne unit was not meeting the requirements of Unit 2 Tech. Specs. Section 4.6.3.2.
Plant conditions at the time of the event (s):
This event occurred on 4-5-83 with the unit shutdown for refueling.
Detailed description of the event (s):
On 4-5-83 (reference Deviation Report Number 2-83-48) and again on 4-11-83 (reference Deviation Report Number 2-83-53), with LSFT HNP-2-3109
" MAIN STEAM DRAIN VALVES" in progress, orain valve 2B21-F016 failed to cycle fully upon logic signal.
With the valve in the open position, logic was initiated to close the valve.
Upon initiation the valve began to close and stuck in the partially open/ closed position.
Double indication was observed on control panel 2Hll-P602.
The LSFT was terminated and the valve placed in the open position.
Consequences of the event (s):
Plant was shutcown at the time of the event; therefore, there were no significant consequences of this event.
The health and safety of the public were not affected by this event.
't Status of redundant or backup subsystems and/or systems:
Plant was shutdown at the time of the event, no backup system required.
Justification for continued operation:
Plant was shutdown at the time of the event.
Valve has been fixed and functionally tested.
If repetitive, nuraber of previous LER:
This is a non-repetitive event.
Impact to other systems and/or Unit:
This event had no effect on any other systems or on the other Unit.
Cause(s) of the event (s):
The cause of the event was dirty contacts on the torque switch preventing continuous signal and travel of the valve.
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NARRATIVE' REPORT FOR LER 50-366/1983-016
'Page Two
' Immediate Corrective Action:
The contacts on the torque switch were disconnecteo, cleaned and re-tightened.
The valve was then cycleo using the control switch.
The LSFT was successfully completed and the _ system returneo to service on 4-12-83.
Supplemental Corrective Action:
No supplemental corrective action is required.
Scheduled (future) corrective action:
No scheduled (future) corrective action is required.
Action to prevent recurrence (if different from corrective actions):
The corrective actions taken should be sufficient to preclude recurrence.
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| 05000366/LER-1983-001, Forwards LER 83-001/03L-0 | Forwards LER 83-001/03L-0 | | | 05000321/LER-1983-001, Forwards LER 83-001/03L-0 | Forwards LER 83-001/03L-0 | | | 05000321/LER-1983-001-03, /03L-0:on 830102,during Surveillance Procedure, Two Control Room Ventilation Bypass Isolation Valves Would Not Close within Required 7 S.Caused by Instrument Drift. Rate Set Valves Adjusted | /03L-0:on 830102,during Surveillance Procedure, Two Control Room Ventilation Bypass Isolation Valves Would Not Close within Required 7 S.Caused by Instrument Drift. Rate Set Valves Adjusted | | | 05000366/LER-1983-001-03, /03L-0:on 830107,while Performing ECCS Status Check Procedure,Drywell Hydrogen Oxygen Analyzer Discovered Inoperative.Caused by Moisture Accumulation in Regulator Sensing Line.Water Removed.Pump Diaphragms Replaced | /03L-0:on 830107,while Performing ECCS Status Check Procedure,Drywell Hydrogen Oxygen Analyzer Discovered Inoperative.Caused by Moisture Accumulation in Regulator Sensing Line.Water Removed.Pump Diaphragms Replaced | | | 05000321/LER-1983-002, Forwards LER 83-002/03L-0 | Forwards LER 83-002/03L-0 | | | 05000321/LER-1983-002-03, /03L-0:on 830104,while Performing Hydraulic Shock & Sway Arrestor Insp & Functional Test Surveillance Procedure,Snubber Discovered Inoperable.Caused by Component Failure Due to Low Hydraulic Fluid.Snubber Replaced | /03L-0:on 830104,while Performing Hydraulic Shock & Sway Arrestor Insp & Functional Test Surveillance Procedure,Snubber Discovered Inoperable.Caused by Component Failure Due to Low Hydraulic Fluid.Snubber Replaced | | | 05000366/LER-1983-002-03, /03L-0:on 830118,primary Containment Isolation Reactor Water Level low-low Instrument Channel B Found Out of Calibr.Caused by Setpoint Drift.Instrument Recalibr | /03L-0:on 830118,primary Containment Isolation Reactor Water Level low-low Instrument Channel B Found Out of Calibr.Caused by Setpoint Drift.Instrument Recalibr | | | 05000366/LER-1983-002, Forwards LER 83-002/03L-0 | Forwards LER 83-002/03L-0 | | | 05000321/LER-1983-003, Forwards LER 83-003/03L-0 | Forwards LER 83-003/03L-0 | | | 05000321/LER-1983-003-03, /03L-0:on 830105,NRC Notified Util of Incorrect Page in Tech Specs.P 3.5-9 Stated That Six of Seven Instead of Seven Automatic Depressurization Valves Should Be Operable.Caused by Personnel Error in Inserting Wrong Rev | /03L-0:on 830105,NRC Notified Util of Incorrect Page in Tech Specs.P 3.5-9 Stated That Six of Seven Instead of Seven Automatic Depressurization Valves Should Be Operable.Caused by Personnel Error in Inserting Wrong Rev | | | 05000366/LER-1983-003-03, /03L-0:on 830214,drywell 2(HO) B Analyzer Would Not Calibr.Cause Not Stated.Sample Pump Head Assemblies & Diaphragms Replaced & Bypass Check Valves Cleaned.A & B Analyzers Will Be Replaced W/Improved Model | /03L-0:on 830214,drywell 2(HO) B Analyzer Would Not Calibr.Cause Not Stated.Sample Pump Head Assemblies & Diaphragms Replaced & Bypass Check Valves Cleaned.A & B Analyzers Will Be Replaced W/Improved Model | | | 05000366/LER-1983-003, Forwards LER 83-003/03L-0 | Forwards LER 83-003/03L-0 | | | 05000366/LER-1983-004-03, /03L-0:on 830113 & 20,standby Gas Treatment Fan Failed to Start Automatically W/Switch in Run Position. Caused by Loose Auxiliary Switch Mounting Screw & Failure of Filter Train Heater Control Latching Relay.Switch Repaired | /03L-0:on 830113 & 20,standby Gas Treatment Fan Failed to Start Automatically W/Switch in Run Position. Caused by Loose Auxiliary Switch Mounting Screw & Failure of Filter Train Heater Control Latching Relay.Switch Repaired | | | 05000366/LER-1983-004, Forwards LER 83-004/03L-0 | Forwards LER 83-004/03L-0 | | | 05000321/LER-1983-004, Forwards LER 83-004/03L-0 | Forwards LER 83-004/03L-0 | | | 05000321/LER-1983-004-03, /03L-0:on 830108,control Room Supply Fan a Found Inoperable.Caused by Component Failure Due to Inoperable Time Delay Relay & Flow Switch.Relay & Switch Replaced & Returned to Operable Status.Fan a Returned to Svc on 830111 | /03L-0:on 830108,control Room Supply Fan a Found Inoperable.Caused by Component Failure Due to Inoperable Time Delay Relay & Flow Switch.Relay & Switch Replaced & Returned to Operable Status.Fan a Returned to Svc on 830111 | | | 05000366/LER-1983-005-03, /03L-0:on 830128,during Performance of Routine Panel walkdown,2A Recirculation Pump Discharge Valve Position Not Illuminated.Caused by Circuit Breaker Being in Off Position | /03L-0:on 830128,during Performance of Routine Panel walkdown,2A Recirculation Pump Discharge Valve Position Not Illuminated.Caused by Circuit Breaker Being in Off Position | | | 05000321/LER-1983-005-03, /03L-0:on 830106,power Supply for Standby Gas Treatment Fan 1A Found Inoperable.Caused by Power Supply Breaker Being Off.Breaker Turned on | /03L-0:on 830106,power Supply for Standby Gas Treatment Fan 1A Found Inoperable.Caused by Power Supply Breaker Being Off.Breaker Turned on | | | 05000321/LER-1983-005, Forwards LER 83-005/03L-0 | Forwards LER 83-005/03L-0 | | | 05000366/LER-1983-005, Forwards LER 83-005/03L-0 | Forwards LER 83-005/03L-0 | | | 05000321/LER-1983-006-03, /03L-0:on 830126,during Refueling Outage,Plant Svc Water Turbine Bldg Isolation Valves a & D Failed to Isolate & Pump 1A Failed to Start.Caused by Disconnected Control Wire Lifted for Unknown Reasons | /03L-0:on 830126,during Refueling Outage,Plant Svc Water Turbine Bldg Isolation Valves a & D Failed to Isolate & Pump 1A Failed to Start.Caused by Disconnected Control Wire Lifted for Unknown Reasons | | | 05000321/LER-1983-006, Forwards LER 83-006/03L-0 | Forwards LER 83-006/03L-0 | | | 05000366/LER-1983-006-03, /03L-0:on 830224,reactor Water Low Level Instrument Switches Discovered Double Actuating.Caused by Magnetic Source Being Out of Adjustment.Switches Readjusted | /03L-0:on 830224,reactor Water Low Level Instrument Switches Discovered Double Actuating.Caused by Magnetic Source Being Out of Adjustment.Switches Readjusted | | | 05000366/LER-1983-006, Forwards LER 83-006/03L-0 | Forwards LER 83-006/03L-0 | | | 05000366/LER-1983-007, Forwards LER 83-007/03L-0 | Forwards LER 83-007/03L-0 | | | 05000366/LER-1983-007-03, /03L-0:on 830401,RHR Flow Indicator 2C82-R004 on Remote Shutdown Panel Found to Be Reading Inaccurately, Rendering Instrument Loop Inoperable.Caused by Component Failure.Defective Amplifier Card Replaced | /03L-0:on 830401,RHR Flow Indicator 2C82-R004 on Remote Shutdown Panel Found to Be Reading Inaccurately, Rendering Instrument Loop Inoperable.Caused by Component Failure.Defective Amplifier Card Replaced | | | 05000321/LER-1983-007, Forwards LER 83-007/03L-0 | Forwards LER 83-007/03L-0 | | | 05000321/LER-1983-007-03, /03L-0:on 830218,HPCI Turbine Would Not Trip at Less than 5,000 Rpm.Caused by Chipped Ball on ball-tappet assembly.Ball-tappet Assembly Replaced | /03L-0:on 830218,HPCI Turbine Would Not Trip at Less than 5,000 Rpm.Caused by Chipped Ball on ball-tappet assembly.Ball-tappet Assembly Replaced | | | 05000321/LER-1983-008, Forwards LER 83-008/03L-0 | Forwards LER 83-008/03L-0 | | | 05000321/LER-1983-008-03, /03L-0:on 830112,during Performance of Clean Radwaste Water Processing Procedure,Personnel Discharged Waste Sample Tank a to River Before Sample Analyzed.Caused by Personnel Error.Responsible Individual Reprimanded | /03L-0:on 830112,during Performance of Clean Radwaste Water Processing Procedure,Personnel Discharged Waste Sample Tank a to River Before Sample Analyzed.Caused by Personnel Error.Responsible Individual Reprimanded | | | 05000366/LER-1983-008, Forwards LER 83-008/03L-0 | Forwards LER 83-008/03L-0 | | | 05000366/LER-1983-008-03, /03L-0:on 830207,reactor Coolant Recirculation Pump 2A Tripped.Cause Attributed to Spurious Trip of 4160-volt Bus.Volt Bus re-energized & Pump Restarted | /03L-0:on 830207,reactor Coolant Recirculation Pump 2A Tripped.Cause Attributed to Spurious Trip of 4160-volt Bus.Volt Bus re-energized & Pump Restarted | | | 05000366/LER-1983-009, Forwards LER 83-009/03L-0 | Forwards LER 83-009/03L-0 | | | 05000366/LER-1983-009-03, /03L-0:on 830212,RCIC Trip & Throttle Valve Failed to Manually Trip.Caused by Failed Torque Switch in Limitorque Valve Operator.Torque Switch Replaced.Rcic Trip & Throttle Valve Reset | /03L-0:on 830212,RCIC Trip & Throttle Valve Failed to Manually Trip.Caused by Failed Torque Switch in Limitorque Valve Operator.Torque Switch Replaced.Rcic Trip & Throttle Valve Reset | | | 05000321/LER-1983-009, Forwards LER 83-009/03L-0 | Forwards LER 83-009/03L-0 | | | 05000321/LER-1983-009-03, /03L-0:on 830126,while Performing Reactor High Pressure Instrument Ft&C Procedure,Reactor Pressure Instrument B Actuated at 164 Psig,Above Tech Spec Limit. Caused by Setpoint Drift.Instrument Recalibr | /03L-0:on 830126,while Performing Reactor High Pressure Instrument Ft&C Procedure,Reactor Pressure Instrument B Actuated at 164 Psig,Above Tech Spec Limit. Caused by Setpoint Drift.Instrument Recalibr | | | 05000366/LER-1983-010-03, /03L-0:on 830318,discovered Safety/Relief Valve Tailpipe Temp Recorder 2B31-R614 Inoperable.Caused by Component Failure.Pulsing Capacitor & Fuse Replaced & Recorder Returned to Svc | /03L-0:on 830318,discovered Safety/Relief Valve Tailpipe Temp Recorder 2B31-R614 Inoperable.Caused by Component Failure.Pulsing Capacitor & Fuse Replaced & Recorder Returned to Svc | | | 05000366/LER-1983-010, Forwards LER 83-010/03L-0 | Forwards LER 83-010/03L-0 | | | 05000321/LER-1983-010, Forwards LER 83-010/03L-0 | Forwards LER 83-010/03L-0 | | | 05000321/LER-1983-010-03, /03L-0:on 830110,during Reactor Coolant Instrumentation Lines Excess Flow Check Valve Operability review,12 Valves Found Inoperable.Caused by Electrical & Mechanical Component Failures.Valves Repaired/Replaced | /03L-0:on 830110,during Reactor Coolant Instrumentation Lines Excess Flow Check Valve Operability review,12 Valves Found Inoperable.Caused by Electrical & Mechanical Component Failures.Valves Repaired/Replaced | | | 05000321/LER-1983-011-03, /03L-0:on 830204,during Performance of Sys Walkdown,Circuit Which Supplies Essential Control Power to Trip Circulating Water Pump Feeder Breakers Found Terminated.Caused by Improper Const Installation | /03L-0:on 830204,during Performance of Sys Walkdown,Circuit Which Supplies Essential Control Power to Trip Circulating Water Pump Feeder Breakers Found Terminated.Caused by Improper Const Installation | | | 05000366/LER-1983-011, Forwards LER 83-011/03L-0 | Forwards LER 83-011/03L-0 | | | 05000366/LER-1983-011-03, /03L-0:on 830210,during Shift Surveillance Check Procedure,Drywell Torus Temp Recorder Found Inoperable. Caused by Failed Internal Parts.Parts Replaced | /03L-0:on 830210,during Shift Surveillance Check Procedure,Drywell Torus Temp Recorder Found Inoperable. Caused by Failed Internal Parts.Parts Replaced | | | 05000321/LER-1983-011, Forwards LER 83-011/03L-0 | Forwards LER 83-011/03L-0 | | | 05000321/LER-1983-012, Forwards LER 83-012/03L-0 | Forwards LER 83-012/03L-0 | | | 05000366/LER-1983-012, Forwards LER 83-012/03L-0 | Forwards LER 83-012/03L-0 | | | 05000321/LER-1983-012-03, /03L-0:on 830124,plant Svc Water Pump 2A Would Not Start Automatically on Low Header Pressure.Caused by Failure of Pump Motor Start Relay Holding Coil.Relay Replaced | /03L-0:on 830124,plant Svc Water Pump 2A Would Not Start Automatically on Low Header Pressure.Caused by Failure of Pump Motor Start Relay Holding Coil.Relay Replaced | | | 05000366/LER-1983-012-03, /03L-0:on 830307,RCIC Isolated on Exhaust Diaphragm High Pressure During Surveillance Procedure HNP-2-3405.Caused by Component Failure.Inboard & Outboard Rupture Discs Replaced & Added to Yearly Maint Schedule | /03L-0:on 830307,RCIC Isolated on Exhaust Diaphragm High Pressure During Surveillance Procedure HNP-2-3405.Caused by Component Failure.Inboard & Outboard Rupture Discs Replaced & Added to Yearly Maint Schedule | | | 05000366/LER-1983-013-03, /03L-0:on 830320,RHR Svc Water Loop a Discharge Valve Drifted Closed.Caused by Dirty Manual Pushbutton Switch on Indicator Controller.Switch Cleaned | /03L-0:on 830320,RHR Svc Water Loop a Discharge Valve Drifted Closed.Caused by Dirty Manual Pushbutton Switch on Indicator Controller.Switch Cleaned | | | 05000321/LER-1983-013-03, /03L-0:on 830222,during Performance of HPCI Pump Operability Procedure,Hpci Turbine Exhaust Diaphragms Ruptured.Caused by Personnel Error.Hpci Valve & Diaphragms Repaired & Installed.Personnel Counseled | /03L-0:on 830222,during Performance of HPCI Pump Operability Procedure,Hpci Turbine Exhaust Diaphragms Ruptured.Caused by Personnel Error.Hpci Valve & Diaphragms Repaired & Installed.Personnel Counseled | |
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