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LER-1983-017, /03L-0:on 830406,during HNP-2-3322,w/unit in Cold Shutdown,Hpci Pump Discharge Valve 2E41-F006 Failed to Open. Caused by Loose Wire on Terminal Block Inside Valve Operator.Wire Tightened.Valve Cycled |
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| 3661983017R03 - NRC Website |
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NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7 77)
LICEN$EE EVENT REPORT
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8 60 61 DOCKET NUM3ER 68 69 EVENT CATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lo l2l l During performance of "HPCI AUTOMATIC ACTUATION" procedure (HNP-2-3322),
I lo l3l l the HPCI pump discharge valve (2E41-F006) failed to open as required by l
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0 s l Perable during shutdown. The health and safety of the public were not l
l0 l7l l not affected by this non-repetitive event.
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that prevented the 2E41-F006 valve from operating is unknown. The loose l
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NARRATIVE
REPORT FOR LER 50-366/1983-017 LICENSEE
- GEORGIA POWER COMPANY FACILITY NAME
- EDWIN I.
HATCH DOCKET NUMBER
- 50-366 Tech. Specs. section(s) which requires report:
This 3n-day-LER is required by Tech. Specs. section 6.9.1.9.b~.
due to the event's showing that the unit was not meeting the requirements of Tech.
Specs. section 4.5.1.c.1.
Plant conditions at the time of the event (s):
On April 6, 1983, the plant was in cold shutdown for a refueling outage.
Detailed description of the-event (s):
B During performance of "HPCI AUTOMATIC ACTUATION" procedure (HNP-2-3322),
the HPCI pump discharge valve (2E41-FOO6) failed to open.
Consequences of the event (s):
The plant was in cold shutdown at the time of the event.
HPCI is not required to be operable in cold shutdown.
There were no consequences of this event.
The health and safety of the public were not affected by this event.
Status of redundant or backup subsystems and/or systems:
'No redundant or backup systems are required in cold shutdown.
Justification for continued operation:
Unit was in cold shutdown during refueling outage and HPCI was not required to be operable.
If repetitive, number of previous LER:
This is a non-repetitive event.
Impact to other systems and/or Unit:
This' problem does not affect the other plant systems, nor does it affect Unit 1.
Cause(s) of the event (s):
The cause of the event was attributed to a loose wire located on the motor terminal block inside of the value operator.
The cause of the loose id re that prevented the 2E41-FOO6 value from operating is unknown.
'D I
Narrative Report for LER 50-366/1983-017 Page Two
Immediate Corrective Action
The loose wire was tightened and 2E41-F006 valve was cycled.
Supplemental Corrective Action:
The 2E41-F006 will be functionally tested prior to startup.
Scheduled (future) corrective action:
No scheduled future corrective action is required.
Action to prevent recurrence (if different from corrective-actions):_
No further action is required to prevent recurrence.
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| 05000366/LER-1983-001, Forwards LER 83-001/03L-0 | Forwards LER 83-001/03L-0 | | | 05000321/LER-1983-001, Forwards LER 83-001/03L-0 | Forwards LER 83-001/03L-0 | | | 05000321/LER-1983-001-03, /03L-0:on 830102,during Surveillance Procedure, Two Control Room Ventilation Bypass Isolation Valves Would Not Close within Required 7 S.Caused by Instrument Drift. Rate Set Valves Adjusted | /03L-0:on 830102,during Surveillance Procedure, Two Control Room Ventilation Bypass Isolation Valves Would Not Close within Required 7 S.Caused by Instrument Drift. Rate Set Valves Adjusted | | | 05000366/LER-1983-001-03, /03L-0:on 830107,while Performing ECCS Status Check Procedure,Drywell Hydrogen Oxygen Analyzer Discovered Inoperative.Caused by Moisture Accumulation in Regulator Sensing Line.Water Removed.Pump Diaphragms Replaced | /03L-0:on 830107,while Performing ECCS Status Check Procedure,Drywell Hydrogen Oxygen Analyzer Discovered Inoperative.Caused by Moisture Accumulation in Regulator Sensing Line.Water Removed.Pump Diaphragms Replaced | | | 05000321/LER-1983-002, Forwards LER 83-002/03L-0 | Forwards LER 83-002/03L-0 | | | 05000321/LER-1983-002-03, /03L-0:on 830104,while Performing Hydraulic Shock & Sway Arrestor Insp & Functional Test Surveillance Procedure,Snubber Discovered Inoperable.Caused by Component Failure Due to Low Hydraulic Fluid.Snubber Replaced | /03L-0:on 830104,while Performing Hydraulic Shock & Sway Arrestor Insp & Functional Test Surveillance Procedure,Snubber Discovered Inoperable.Caused by Component Failure Due to Low Hydraulic Fluid.Snubber Replaced | | | 05000366/LER-1983-002-03, /03L-0:on 830118,primary Containment Isolation Reactor Water Level low-low Instrument Channel B Found Out of Calibr.Caused by Setpoint Drift.Instrument Recalibr | /03L-0:on 830118,primary Containment Isolation Reactor Water Level low-low Instrument Channel B Found Out of Calibr.Caused by Setpoint Drift.Instrument Recalibr | | | 05000366/LER-1983-002, Forwards LER 83-002/03L-0 | Forwards LER 83-002/03L-0 | | | 05000321/LER-1983-003, Forwards LER 83-003/03L-0 | Forwards LER 83-003/03L-0 | | | 05000321/LER-1983-003-03, /03L-0:on 830105,NRC Notified Util of Incorrect Page in Tech Specs.P 3.5-9 Stated That Six of Seven Instead of Seven Automatic Depressurization Valves Should Be Operable.Caused by Personnel Error in Inserting Wrong Rev | /03L-0:on 830105,NRC Notified Util of Incorrect Page in Tech Specs.P 3.5-9 Stated That Six of Seven Instead of Seven Automatic Depressurization Valves Should Be Operable.Caused by Personnel Error in Inserting Wrong Rev | | | 05000366/LER-1983-003-03, /03L-0:on 830214,drywell 2(HO) B Analyzer Would Not Calibr.Cause Not Stated.Sample Pump Head Assemblies & Diaphragms Replaced & Bypass Check Valves Cleaned.A & B Analyzers Will Be Replaced W/Improved Model | /03L-0:on 830214,drywell 2(HO) B Analyzer Would Not Calibr.Cause Not Stated.Sample Pump Head Assemblies & Diaphragms Replaced & Bypass Check Valves Cleaned.A & B Analyzers Will Be Replaced W/Improved Model | | | 05000366/LER-1983-003, Forwards LER 83-003/03L-0 | Forwards LER 83-003/03L-0 | | | 05000366/LER-1983-004-03, /03L-0:on 830113 & 20,standby Gas Treatment Fan Failed to Start Automatically W/Switch in Run Position. Caused by Loose Auxiliary Switch Mounting Screw & Failure of Filter Train Heater Control Latching Relay.Switch Repaired | /03L-0:on 830113 & 20,standby Gas Treatment Fan Failed to Start Automatically W/Switch in Run Position. Caused by Loose Auxiliary Switch Mounting Screw & Failure of Filter Train Heater Control Latching Relay.Switch Repaired | | | 05000366/LER-1983-004, Forwards LER 83-004/03L-0 | Forwards LER 83-004/03L-0 | | | 05000321/LER-1983-004, Forwards LER 83-004/03L-0 | Forwards LER 83-004/03L-0 | | | 05000321/LER-1983-004-03, /03L-0:on 830108,control Room Supply Fan a Found Inoperable.Caused by Component Failure Due to Inoperable Time Delay Relay & Flow Switch.Relay & Switch Replaced & Returned to Operable Status.Fan a Returned to Svc on 830111 | /03L-0:on 830108,control Room Supply Fan a Found Inoperable.Caused by Component Failure Due to Inoperable Time Delay Relay & Flow Switch.Relay & Switch Replaced & Returned to Operable Status.Fan a Returned to Svc on 830111 | | | 05000366/LER-1983-005-03, /03L-0:on 830128,during Performance of Routine Panel walkdown,2A Recirculation Pump Discharge Valve Position Not Illuminated.Caused by Circuit Breaker Being in Off Position | /03L-0:on 830128,during Performance of Routine Panel walkdown,2A Recirculation Pump Discharge Valve Position Not Illuminated.Caused by Circuit Breaker Being in Off Position | | | 05000321/LER-1983-005-03, /03L-0:on 830106,power Supply for Standby Gas Treatment Fan 1A Found Inoperable.Caused by Power Supply Breaker Being Off.Breaker Turned on | /03L-0:on 830106,power Supply for Standby Gas Treatment Fan 1A Found Inoperable.Caused by Power Supply Breaker Being Off.Breaker Turned on | | | 05000321/LER-1983-005, Forwards LER 83-005/03L-0 | Forwards LER 83-005/03L-0 | | | 05000366/LER-1983-005, Forwards LER 83-005/03L-0 | Forwards LER 83-005/03L-0 | | | 05000321/LER-1983-006-03, /03L-0:on 830126,during Refueling Outage,Plant Svc Water Turbine Bldg Isolation Valves a & D Failed to Isolate & Pump 1A Failed to Start.Caused by Disconnected Control Wire Lifted for Unknown Reasons | /03L-0:on 830126,during Refueling Outage,Plant Svc Water Turbine Bldg Isolation Valves a & D Failed to Isolate & Pump 1A Failed to Start.Caused by Disconnected Control Wire Lifted for Unknown Reasons | | | 05000321/LER-1983-006, Forwards LER 83-006/03L-0 | Forwards LER 83-006/03L-0 | | | 05000366/LER-1983-006-03, /03L-0:on 830224,reactor Water Low Level Instrument Switches Discovered Double Actuating.Caused by Magnetic Source Being Out of Adjustment.Switches Readjusted | /03L-0:on 830224,reactor Water Low Level Instrument Switches Discovered Double Actuating.Caused by Magnetic Source Being Out of Adjustment.Switches Readjusted | | | 05000366/LER-1983-006, Forwards LER 83-006/03L-0 | Forwards LER 83-006/03L-0 | | | 05000366/LER-1983-007, Forwards LER 83-007/03L-0 | Forwards LER 83-007/03L-0 | | | 05000366/LER-1983-007-03, /03L-0:on 830401,RHR Flow Indicator 2C82-R004 on Remote Shutdown Panel Found to Be Reading Inaccurately, Rendering Instrument Loop Inoperable.Caused by Component Failure.Defective Amplifier Card Replaced | /03L-0:on 830401,RHR Flow Indicator 2C82-R004 on Remote Shutdown Panel Found to Be Reading Inaccurately, Rendering Instrument Loop Inoperable.Caused by Component Failure.Defective Amplifier Card Replaced | | | 05000321/LER-1983-007, Forwards LER 83-007/03L-0 | Forwards LER 83-007/03L-0 | | | 05000321/LER-1983-007-03, /03L-0:on 830218,HPCI Turbine Would Not Trip at Less than 5,000 Rpm.Caused by Chipped Ball on ball-tappet assembly.Ball-tappet Assembly Replaced | /03L-0:on 830218,HPCI Turbine Would Not Trip at Less than 5,000 Rpm.Caused by Chipped Ball on ball-tappet assembly.Ball-tappet Assembly Replaced | | | 05000321/LER-1983-008, Forwards LER 83-008/03L-0 | Forwards LER 83-008/03L-0 | | | 05000321/LER-1983-008-03, /03L-0:on 830112,during Performance of Clean Radwaste Water Processing Procedure,Personnel Discharged Waste Sample Tank a to River Before Sample Analyzed.Caused by Personnel Error.Responsible Individual Reprimanded | /03L-0:on 830112,during Performance of Clean Radwaste Water Processing Procedure,Personnel Discharged Waste Sample Tank a to River Before Sample Analyzed.Caused by Personnel Error.Responsible Individual Reprimanded | | | 05000366/LER-1983-008, Forwards LER 83-008/03L-0 | Forwards LER 83-008/03L-0 | | | 05000366/LER-1983-008-03, /03L-0:on 830207,reactor Coolant Recirculation Pump 2A Tripped.Cause Attributed to Spurious Trip of 4160-volt Bus.Volt Bus re-energized & Pump Restarted | /03L-0:on 830207,reactor Coolant Recirculation Pump 2A Tripped.Cause Attributed to Spurious Trip of 4160-volt Bus.Volt Bus re-energized & Pump Restarted | | | 05000366/LER-1983-009, Forwards LER 83-009/03L-0 | Forwards LER 83-009/03L-0 | | | 05000366/LER-1983-009-03, /03L-0:on 830212,RCIC Trip & Throttle Valve Failed to Manually Trip.Caused by Failed Torque Switch in Limitorque Valve Operator.Torque Switch Replaced.Rcic Trip & Throttle Valve Reset | /03L-0:on 830212,RCIC Trip & Throttle Valve Failed to Manually Trip.Caused by Failed Torque Switch in Limitorque Valve Operator.Torque Switch Replaced.Rcic Trip & Throttle Valve Reset | | | 05000321/LER-1983-009, Forwards LER 83-009/03L-0 | Forwards LER 83-009/03L-0 | | | 05000321/LER-1983-009-03, /03L-0:on 830126,while Performing Reactor High Pressure Instrument Ft&C Procedure,Reactor Pressure Instrument B Actuated at 164 Psig,Above Tech Spec Limit. Caused by Setpoint Drift.Instrument Recalibr | /03L-0:on 830126,while Performing Reactor High Pressure Instrument Ft&C Procedure,Reactor Pressure Instrument B Actuated at 164 Psig,Above Tech Spec Limit. Caused by Setpoint Drift.Instrument Recalibr | | | 05000366/LER-1983-010-03, /03L-0:on 830318,discovered Safety/Relief Valve Tailpipe Temp Recorder 2B31-R614 Inoperable.Caused by Component Failure.Pulsing Capacitor & Fuse Replaced & Recorder Returned to Svc | /03L-0:on 830318,discovered Safety/Relief Valve Tailpipe Temp Recorder 2B31-R614 Inoperable.Caused by Component Failure.Pulsing Capacitor & Fuse Replaced & Recorder Returned to Svc | | | 05000366/LER-1983-010, Forwards LER 83-010/03L-0 | Forwards LER 83-010/03L-0 | | | 05000321/LER-1983-010, Forwards LER 83-010/03L-0 | Forwards LER 83-010/03L-0 | | | 05000321/LER-1983-010-03, /03L-0:on 830110,during Reactor Coolant Instrumentation Lines Excess Flow Check Valve Operability review,12 Valves Found Inoperable.Caused by Electrical & Mechanical Component Failures.Valves Repaired/Replaced | /03L-0:on 830110,during Reactor Coolant Instrumentation Lines Excess Flow Check Valve Operability review,12 Valves Found Inoperable.Caused by Electrical & Mechanical Component Failures.Valves Repaired/Replaced | | | 05000321/LER-1983-011-03, /03L-0:on 830204,during Performance of Sys Walkdown,Circuit Which Supplies Essential Control Power to Trip Circulating Water Pump Feeder Breakers Found Terminated.Caused by Improper Const Installation | /03L-0:on 830204,during Performance of Sys Walkdown,Circuit Which Supplies Essential Control Power to Trip Circulating Water Pump Feeder Breakers Found Terminated.Caused by Improper Const Installation | | | 05000366/LER-1983-011, Forwards LER 83-011/03L-0 | Forwards LER 83-011/03L-0 | | | 05000366/LER-1983-011-03, /03L-0:on 830210,during Shift Surveillance Check Procedure,Drywell Torus Temp Recorder Found Inoperable. Caused by Failed Internal Parts.Parts Replaced | /03L-0:on 830210,during Shift Surveillance Check Procedure,Drywell Torus Temp Recorder Found Inoperable. Caused by Failed Internal Parts.Parts Replaced | | | 05000321/LER-1983-011, Forwards LER 83-011/03L-0 | Forwards LER 83-011/03L-0 | | | 05000321/LER-1983-012, Forwards LER 83-012/03L-0 | Forwards LER 83-012/03L-0 | | | 05000366/LER-1983-012, Forwards LER 83-012/03L-0 | Forwards LER 83-012/03L-0 | | | 05000321/LER-1983-012-03, /03L-0:on 830124,plant Svc Water Pump 2A Would Not Start Automatically on Low Header Pressure.Caused by Failure of Pump Motor Start Relay Holding Coil.Relay Replaced | /03L-0:on 830124,plant Svc Water Pump 2A Would Not Start Automatically on Low Header Pressure.Caused by Failure of Pump Motor Start Relay Holding Coil.Relay Replaced | | | 05000366/LER-1983-012-03, /03L-0:on 830307,RCIC Isolated on Exhaust Diaphragm High Pressure During Surveillance Procedure HNP-2-3405.Caused by Component Failure.Inboard & Outboard Rupture Discs Replaced & Added to Yearly Maint Schedule | /03L-0:on 830307,RCIC Isolated on Exhaust Diaphragm High Pressure During Surveillance Procedure HNP-2-3405.Caused by Component Failure.Inboard & Outboard Rupture Discs Replaced & Added to Yearly Maint Schedule | | | 05000366/LER-1983-013-03, /03L-0:on 830320,RHR Svc Water Loop a Discharge Valve Drifted Closed.Caused by Dirty Manual Pushbutton Switch on Indicator Controller.Switch Cleaned | /03L-0:on 830320,RHR Svc Water Loop a Discharge Valve Drifted Closed.Caused by Dirty Manual Pushbutton Switch on Indicator Controller.Switch Cleaned | | | 05000321/LER-1983-013-03, /03L-0:on 830222,during Performance of HPCI Pump Operability Procedure,Hpci Turbine Exhaust Diaphragms Ruptured.Caused by Personnel Error.Hpci Valve & Diaphragms Repaired & Installed.Personnel Counseled | /03L-0:on 830222,during Performance of HPCI Pump Operability Procedure,Hpci Turbine Exhaust Diaphragms Ruptured.Caused by Personnel Error.Hpci Valve & Diaphragms Repaired & Installed.Personnel Counseled | |
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