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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217G3541999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbaps,Units 2 & 3. with ML20212A5871999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Peach Bottom,Units 2 & 3.With ML20210N7641999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for PBAPS Units 2 & 3. with ML20209H1121999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbaps,Units 2 & 3. with ML20195H8841999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbaps,Units 2 & 3. with ML20206N1661999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pbaps,Units 2 & 3. with ML20205P5851999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Peach Bottom Units 2 & 3.With ML20207G9971999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Peach Bottom Units 2 & 3.With ML20199E3471998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Peach Bottom,Units 1 & 2.With ML20198B8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pbaps,Units 2 & 3. with ML20195E5341998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pbaps,Units 2 & 3. with ML20154H5541998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Pbaps,Units 2 & 3. with ML20151Y2901998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Pbaps,Units 2 & 3. with ML20237A5351998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pbaps,Units 2 & 3 ML20236M3471998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Pbaps,Units 2 & 3 ML20248M3001998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pbaps,Units 2 & 3 ML20247G0721998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Pbaps,Units 2 & 3 ML20216F3831998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Peach Bottom,Units 2 & 3 ML20216G1991998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Peach Bottom Atomic Power Station,Units 1 & 2 ML20202F7341998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Pbaps,Units 2 & 3 ML20198N8851997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Peach Bottom,Units 2 & 3 ML20203J7311997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Pbaps,Units 2 & 3 ML20199D1241997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Peach Bottom,Units 2 & 3 ML20198J8871997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Pbaps,Units 2 & 3 ML20217A8061997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for Peach Bottom Units 2 & 3 ML20210J7111997-07-31031 July 1997 Monthly Operating Repts for Jul 1997 for Pbaps,Units 1 & 2 ML20141H2071997-06-30030 June 1997 Monthly Operating Repts for June 1997 for PBAPS ML20148K6251997-05-31031 May 1997 Monthly Operating Repts for May 1997 for Peach Bottom Atomic Power Station Units 2 & 3 ML20141D3691997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Peach Bottom Units 2 & 3 ML20137V9731997-03-31031 March 1997 Monthly Operating Repts for Mar 1997 for Peach Bottom Atomic Power Station Units 2 & 3 ML20136G3671997-02-28028 February 1997 Monthly Operating Repts for Feb 1997 for PBAPS ML20138K5551997-01-31031 January 1997 Monthly Operating Repts for Jan 1997 for Peach Bottom Units 2 & 3 ML20133H6121996-12-31031 December 1996 Monthly Operating Repts for Dec 1996 for Peach Bottom 2 & 3 ML20132B9481996-11-30030 November 1996 Monthly Operating Repts for Nov 1996 for Peach Bottom Units 1 & 2 ML20134M0501996-10-31031 October 1996 Monthly Operating Repts for Oct 1996 for Peach Bottom Unit 2 & 3 ML20129A9871996-09-30030 September 1996 Monthly Operating Repts for Sept 1996 for Peach Bottom Unit 2 & 3 ML20117N1601996-08-31031 August 1996 Monthly Operating Repts for Aug 1996 for Peach Bottom Atomic Power Station Units 1 & 2 ML20116M1641996-07-31031 July 1996 Monthly Operating Repts for Jul 1996 for Peach Bottom Units 2 & 3 ML20115F8541996-06-30030 June 1996 Monthly Operating Repts for June 1996 for Peach Bottom Units 1 & 2 ML20116M1701996-06-30030 June 1996 Revised MOR for June 1996 for Peach Bottom Unit 3 ML20117M6781996-05-31031 May 1996 Monthly Operating Repts for May 1996 for Peach Bottom Atomic Power Station ML20117F8161996-04-30030 April 1996 Monthly Operating Repts for April 1996 for PBAPS ML20107D9381996-03-31031 March 1996 Monthly Operating Repts for March 1996 for PBAPS ML20106G8101996-02-29029 February 1996 Monthly Operating Repts for Feb 1996 for Peach Bottom Atomic Power Station Units 1 & 2 ML20149K9331996-01-31031 January 1996 Monthly Operating Repts for Jan 1996 for PBAPS Units 2 & 3 ML20096F4151995-12-31031 December 1995 Monthly Operating Repts for Dec 1995 for Pbaps,Units 2 & 3 ML20095G9381995-11-30030 November 1995 Monthly Operating Repts for Nov 1995 for PBAPS Units 2 & 3 ML20094L6301995-10-31031 October 1995 Monthly Operating Repts for Oct 1995 for Peach Bottom Units 2 & 3 ML20093G3571995-09-30030 September 1995 Monthly Operating Repts for Sept 1995 for PBAPS Units 1 & 2 ML20092G3231995-08-31031 August 1995 Monthly Operating Repts for Aug 1995 for Peach Bottom Units 2 & 3 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000278/LER-1999-005-03, :on 990920,uplanned Esfas During Planned Mod Activitives in Main CR Were Noted.Caused by Inattention to Detail by Individuals Performing Work.All CR Mods Were Ceased to Allow Review of Mod Work Packages.With1999-10-20020 October 1999
- on 990920,uplanned Esfas During Planned Mod Activitives in Main CR Were Noted.Caused by Inattention to Detail by Individuals Performing Work.All CR Mods Were Ceased to Allow Review of Mod Work Packages.With
ML20217K9931999-10-14014 October 1999 Safety Evaluation Supporting Amend 234 to License DPR-56 ML20217B4331999-10-0505 October 1999 Safety Evaluation Supporting Amend 233 to License DPR-56 05000278/LER-1999-004-03, :on 990901,3A RPS Bus Was Inadvertently Deenergized,During Planned Mod Activities on Main CR Panel. Caused by Electrician Failing to Self Check Work.All CR Work Was Ceased Immediately & Shutdown Meeting Held1999-10-0101 October 1999
- on 990901,3A RPS Bus Was Inadvertently Deenergized,During Planned Mod Activities on Main CR Panel. Caused by Electrician Failing to Self Check Work.All CR Work Was Ceased Immediately & Shutdown Meeting Held
ML20217G3541999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbaps,Units 2 & 3. with ML20216H7091999-09-24024 September 1999 Safety Evaluation Supporting Amends 229 & 232 to Licenses DPR-44 & DPR-56,respectively ML15112A7681999-09-20020 September 1999 SER Accepting Revision 25 of Pump & Valve Inservice Testing Program,Third 10-year Interval for Plant,Units 1,2 & 3 ML20212D1281999-09-17017 September 1999 Safety Evaluation Supporting Proposed Alternatives CRR-03, 05,08,09,10 & 11 05000278/LER-1999-003-03, :on 990814,HPCIS Was Declared Inoperable Due to Erratic Behavior Resulting in Loss of Single High Train Safety Sys.Caused by Weakness in Procedural Guidance. Readjusted Hydraulic Governor Needle Valve.With1999-09-13013 September 1999
- on 990814,HPCIS Was Declared Inoperable Due to Erratic Behavior Resulting in Loss of Single High Train Safety Sys.Caused by Weakness in Procedural Guidance. Readjusted Hydraulic Governor Needle Valve.With
ML20212A5871999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Peach Bottom,Units 2 & 3.With ML20211D5501999-08-23023 August 1999 Safety Evaluation Supporting Amends 228 & 231 to Licenses DPR-44 & DPR-56,respectively ML20212H6311999-08-19019 August 1999 Rev 2 to PECO-COLR-P2C13, COLR for Pbaps,Unit 2,Reload 12 Cycle 13 ML20210N7641999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for PBAPS Units 2 & 3. with 05000277/LER-1999-005-01, :on 990616,failure to Maintain Provisions of FP Program Occurred.Caused by Less than Adequate Engineering Rigor in Both Development & Review Analysis.Fire Watch Immediately Established.With1999-07-16016 July 1999
- on 990616,failure to Maintain Provisions of FP Program Occurred.Caused by Less than Adequate Engineering Rigor in Both Development & Review Analysis.Fire Watch Immediately Established.With
ML20209H1121999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbaps,Units 2 & 3. with ML20195H8841999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbaps,Units 2 & 3. with 05000278/LER-1999-002-02, :on 990406,safeguard Sys to Unrelated Door Was Inadvertently Disabled by Security Alarm Station Operator. Caused by Noncompliance with Procedures & Less than Adequate Shift Turnover.Briefed Personnel on Event.With1999-05-0606 May 1999
- on 990406,safeguard Sys to Unrelated Door Was Inadvertently Disabled by Security Alarm Station Operator. Caused by Noncompliance with Procedures & Less than Adequate Shift Turnover.Briefed Personnel on Event.With
ML20206N1661999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pbaps,Units 2 & 3. with ML20206A2921999-04-20020 April 1999 Safety Evaluation Concluding That Proposed Changes to EALs for PBAPS Are Consistent with Guidance in NUMARC/NESP-007 & Identified Deviations Meet Requirements of 10CFR50.47(b)(4) & App E to 10CFR50 05000278/LER-1999-001-03, :on 990312,ESF Actuation of Rcics Occurred Due to High Steam Flow Signal During Sys Restoration.Temporary Change to Restoration Procedure Was Initiated to Open RCIC Outboard Steam Isolation Valve in Smaller Increments1999-04-0808 April 1999
- on 990312,ESF Actuation of Rcics Occurred Due to High Steam Flow Signal During Sys Restoration.Temporary Change to Restoration Procedure Was Initiated to Open RCIC Outboard Steam Isolation Valve in Smaller Increments
ML20205K7411999-04-0707 April 1999 Safety Evaluation Supporting Amends 227 & 230 to Licenses DPR-44 & DPR-56,respectively ML20205P5851999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Peach Bottom Units 2 & 3.With ML20207G9971999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Peach Bottom Units 2 & 3.With 05000278/LER-1998-009-01, :on 981227,unplanned Esfa Were Noted.Caused by Transformer Insulator Failure.Replaced Failed Insulator. with1999-01-20020 January 1999
- on 981227,unplanned Esfa Were Noted.Caused by Transformer Insulator Failure.Replaced Failed Insulator. with
ML20199E3471998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Peach Bottom,Units 1 & 2.With ML20206P1651998-12-31031 December 1998 Fire Protection for Operating Nuclear Power Plants, Section Iii.F, Automatic Fire Detection ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20206D3651998-12-31031 December 1998 1998 PBAPS Annual 10CFR50.59 & Commitment Rev Rept. with ML20206D3591998-12-31031 December 1998 1998 PBAPS Annual 10CFR72.48 Rept. with 05000277/LER-1998-008-01, :on 981130,circuit Breaker SU-25 Tripped.Caused by Less than Adequate Procedural Guidance.Operators Verified Sys Integrity & Successfully Returned Sys to Svc.With1998-12-30030 December 1998
- on 981130,circuit Breaker SU-25 Tripped.Caused by Less than Adequate Procedural Guidance.Operators Verified Sys Integrity & Successfully Returned Sys to Svc.With
05000277/LER-1998-007-02, :on 981107,failure to Meet TS & Associated LCO Requirments of Absolute Difference in APRM & Calculated Power of Less than 2% Was Noted.Caused by Substitute Valves Being Used.Removed Substitute Valves.With1998-12-0404 December 1998
- on 981107,failure to Meet TS & Associated LCO Requirments of Absolute Difference in APRM & Calculated Power of Less than 2% Was Noted.Caused by Substitute Valves Being Used.Removed Substitute Valves.With
ML20196G7021998-12-0202 December 1998 SER Authorizing Proposed Alternative to Delay Exam of Reactor Pressure Vessel Shell Circumferential Welds by Two Operating Cycles ML20196E8261998-11-30030 November 1998 Response to NRC RAI Re Reactor Pressure Vessel Structural Integrity at Peach Bottom Units 2 & 3 ML20198B8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pbaps,Units 2 & 3. with 05000278/LER-1998-005-03, :on 981025,inadvertent Unit 3 Electrical Bus E33 Trip (Esfa) During Performance of Unit 2 Electrical Bus E32 Surveillance Test Was Noted.Caused by Personnel Error. Sp S12M-54-E32-XXF4 Was Completed.With1998-11-20020 November 1998
- on 981025,inadvertent Unit 3 Electrical Bus E33 Trip (Esfa) During Performance of Unit 2 Electrical Bus E32 Surveillance Test Was Noted.Caused by Personnel Error. Sp S12M-54-E32-XXF4 Was Completed.With
ML20206R2571998-11-17017 November 1998 PBAPS Graded Exercise Scenario Manual (Sections 1.0 - 5.0) Emergency Preparedness 981117 Scenario P84 ML20198C6751998-11-0505 November 1998 Rev 3 to COLR for PBAPS Unit 3,Reload 11,Cycle 12 ML20195E5341998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pbaps,Units 2 & 3. with ML20155C6071998-10-26026 October 1998 Safety Evaluation Supporting Amend 226 to License DPR-44 ML20155C1681998-10-22022 October 1998 Safety Evaluation Accepting Proposed Alternative Plan for Exam of Reactor Pressure Vessel Shell Longitudinal Welds ML20155H7721998-10-12012 October 1998 Rev 1 to COLR for Peach Bottom Atomic Power Station Unit 2, Reload 12,Cycle 13 05000277/LER-1998-006-02, :on 980915,automatic RWCU Isolation Occurred While Placing RWCU Sys in Svc.Caused by Unexpected Surge of Water.Procedure Change Was Initiated to Open MO-2-12-74 & RWCU Sys Was Successfully Returned to Svc.With1998-10-0909 October 1998
- on 980915,automatic RWCU Isolation Occurred While Placing RWCU Sys in Svc.Caused by Unexpected Surge of Water.Procedure Change Was Initiated to Open MO-2-12-74 & RWCU Sys Was Successfully Returned to Svc.With
ML20154J2401998-10-0505 October 1998 Safety Evaluation Supporting Amends 224 & 228 to Licenses DPR-44 & DPR-56,respectively ML20154H4771998-10-0505 October 1998 Safety Evaluation Supporting Amends 225 & 229 to Licenses DPR-44 & DPR-56,respectively ML20154G6821998-10-0101 October 1998 SER Related to Request for Relief 01A-VRR-1 Re Inservice Testing of Automatic Depressurization Sys Safety Relief Valves at Peach Bottom Atomic Power Station,Units 2 & 3 ML20154G6631998-10-0101 October 1998 Safety Evaluation Supporting Amends 223 & 227 to Licenses DPR-44 & DPR-56,respectively ML20154H5541998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Pbaps,Units 2 & 3. with 05000278/LER-1998-004-03, :on 980820,automatic RWCU Isolation Occurred While Placing B RWCU Sys Demineralizer in Svc.Caused by less-than-adequate Control of Equipment.Isolated B Demineralizer & Returned RWCU Sys to Svc1998-09-18018 September 1998
- on 980820,automatic RWCU Isolation Occurred While Placing B RWCU Sys Demineralizer in Svc.Caused by less-than-adequate Control of Equipment.Isolated B Demineralizer & Returned RWCU Sys to Svc
05000277/LER-1998-005-02, :on 980824,noted Failure to Meet TS Actions for Suppression chamber-to-drywell Vacuum Breaker Not Being Fully Seated.Caused by Personnel Failing to Take All TS Required Actions.Temporary Procedure Changes Were Made1998-09-18018 September 1998
- on 980824,noted Failure to Meet TS Actions for Suppression chamber-to-drywell Vacuum Breaker Not Being Fully Seated.Caused by Personnel Failing to Take All TS Required Actions.Temporary Procedure Changes Were Made
ML20153B9651998-09-14014 September 1998 Safety Evaluation Supporting Amend 9 to License DPR-12 1999-09-30
[Table view] |
Text
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PHILADELPHIA ELEC1RIC COMPANY
(
l PEACH IKYr'!OM ATOMIC POWER STATION j
R. D.1, Box 208 1
i Delta. Pennsyhwua 17314 j
rs4cm monoes.7m roe se or a scausmc2 (717)4567014 j
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D. M. $mith I.
Vice President 14 arch 19,1990 j
Docket Nos. 50 277 l
50 278 p
U.S. Nuclear Regulatoly Commission Document Control Desk Washington? DC 20555 n
~
SUBJECT:
Peach Bottom Atomic Power Station Monthly Operating Report i
Gentlemern t
Enclosed are twelve copies of the monthly operating report for Peach Bottom Units 2 and 3 for the month of February 1990 forwarded pursuant to Technical Specification 6.9.1.d under the guidance of Regulatory Guide 10.1, Revision 4.
Sincerely, l
Ti~k!Ya.s S D.1115dir l
1
&4/97 6 i
DMS/TEC/MJB: cmc
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Enclosure cc:
R.A. Burricelli, Public Service Electric & Gas T.M. Gerusky, Commonwealth of Pennsylvania r
l JJ. Lyash, USNRC Senior Resident Inspector T.E. Magette, State of Maryland W.T. Russell., Administrator, Region I, USNRC l
H.C. Schwemm, Atlantic Electric J. Urban, Delmarva Power INPO Records Center t
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NRC Monthly Operations Summary --
Peach Bottom Atomic Power Station February 1990 1
UNIT 2 4
Unit 2 beganihe month at 95% power and increasing. One hundred percent power was acheived late on.
-- February 1, and was maintained until February 3, when the unit took a 200 MWe load drop for rod pattern
{
adjuatment. Pour was returned to 100% the same day.
r Power was reduced to 62% on February 5 because of a leak in the "2A' feedwater heater After the "A"-
4 feedwater string was removed from service, power was increased to nominal 73% The unit remained at this'-
level for the rest of the month.
UNIT 3 The unit began the rnonth recovering from an outage caused by an EHC leak. Startup activities were in progress.
On February 7, follo*g maintenance on the HPCI gland seal condensate pump and recite M G set brushes, and a trip of the "C" RFP,100% power was acheived. The unit remained at nominal 100% power for the rest of the month.
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Docket No. 50-277
. Attachment to -
Monthly Operating Report for February 1990.
t UNIT 2 REFUELING INFORMATION 1..
Name of facility:
Peach Bottom Unit 2 4;
- 2.
Scheduled date for next refueling shutdown:
Reload 8 scheduled for January 6,1991 3.
Scheduled date for restart following refueling:
Restart following refueling scheduled for April 5,1991 14.
Will refueling or resumption of operation therefore require a technical specification change or other license amendment?
L No.
If answer is yes, what, in general, will these be?
E
- 5. -
Scheduled date(s) for submitting proposed licensing action and supporting information:
Not applicable.
6.
Important licensing considerations associated with refueling, e.g., new or different fuel design or supplier, 1 i unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:
In order for PECo to do reload licensing analyses in-house for Unit 2 Cycle 9, NRC approval of one report (PECO FMS-006) must be obtained by May 31,1990. This report is the last in a series of six reports to demonstrate PECo's ability to perform the analyses. The report has been submitted and is scheduled for completion in May 1990.
7.
The number of fuel assemblics (a) in the core and (b) in the spent fuel storage pool:
(a)
Core - 764 Fuel Assemblies I
(b)
Fuel Pool 1734 Fuel Assemblies,58 Fuel Rods Docket No. 50 277 CC0290.NRC 2
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- Attachment to Monthly Operating Report for February 1990 Page 2 UNIT 2 REFUELING INFORM ATION (Continued) 8.
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, m number of fuel assemblies:
The spent fuel pool storage capacity has been relicensed for 3819 fuel assemblies.
9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present capacity:
September 2003 without full core offload capability.
September 1997 with full core offload capability.
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b mi Docket No. 50-278 Attachment to ;-
Monthly Operating Report for February 1990 j
UNIT 3 REFUELING INFORMATION-
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1.
Name of facility:
t Peach Bottom Unit 3 l
i
-i 2.-
Scheduled date for next refueling shutdown:
- Reload 8 scheduled for August 31,1991 i
3.
Scheduled date for restart following refueling i
Restart following refueling scheduled for October 29,1991
' 4.
Will refueling or resumption of operation thereafter require a technical specification change or other
[
license amendment? -
1 i
- No.
If answer is yes,.what, in general, will these be?
- 5. -
Scheduled date(s) fer submitting proposed licensing action and supporting information:
6.-
Important licensing considerations associated with refueling, e.g., r-wdifferent fueldesign or supplier, J
unreviewed design or performance analysis methods, significant duqu in fuel design, new operating
.p procedures:
None expected, i
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l Docket No. 50-278
- Attachment to Monthly Operating Report for February 1990 Page 2 UNIT 3 REFUELING INFORMATION (Continued) 7.
The number of fuel assemblics (a) in the core and (b) in the spent fuel storage poti 1
(a)
Core 764 Fuel Assemblics (b)
Fuel Pool.14% Fuel Assemblies,6 Fuel Rods 8.
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, m number of fuel assemblies:
The spent fuel pool storage capacity has been relicensed for 3819 fuel auemblics. Modification of the fuel pool is expected to be complete in the fourth quarter of 1990.
9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the
~
present capacity:
l With the current fuel pool capacity (prior to the completion of the fuel poci reracking modification):
September 1996 without full core ofiload capability.
End of next cycle with full core offload capability (est. January 1991).
With increased fuel pool capacity (subsequent to the completion of the fuel pool rcracking modification):
~
l' September 2004 without full core offload capability, September 1998 with full core offload capability.
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CC0290.NRC
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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50 - 277 UNIT PEACH BOTTOM UNIT 2 DATE MARCH 15, 1989 CDMPANY PHILADELPHIA ELECTRIC COMPANY M. J. BARON SUPERVISOR REPDRTS GROUP PEACH BOTTDM ATDMIC POWER STATION TELEPHONE (717) 456-7014 EXT, 3321 MONTH FEBRUARY 1990 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE CA!LY POWER LEVEL
-(MWE-NET)
(HWi-NET) l' 986 17 746 2
1029-18 750 3
925 19 754 4
1059 20 755 5
920 21 750 6
749 22 732 7
741 23 741 8
741 24 7 53 9
740 25 751 10 734 26 751 11 737 27 751 12 737 28.
751 13 746 14 755 15 754 16 7 54 h
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4
. AVERAGE DAILY UNIT PDVER LEVEL DOCKET NO. 50 - 278 UNIT PEACH BOTTDM UNIT 3 DATE MARCH 15. 1989 COMPANY PHILADELPHIA ELECTRIC CDMPANY M. J; BARON SUPERVISDR REPORTS GROUP PEACH BOTTOM ATDMIC POWER STATION TELEPHONE (717)456-7014 EXT,3321 MONTH FEBRUARY 1990 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-NET)
(MWE-NET) 1 138 17 1075 2
535.
18 1075 3
911 19 1075-4 917 20 1075 5-872 21 1067 6
1047 22 1076 7
1067 23 1068 8
1071 24 -
1063 9
1071 25 1070 10 1075 -
26 1078 11.
1079 27 1066 12 1075 28 1083 13 1075~
14 1071 15 1079 16 1075
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-L OPERATING DATA REPORT-q.
DOCKET NO. 50 - 277I i[
DATE MARCH IS, 1989 u
COMPLETED BY PHILADELPHIA ELECTRIC C0t;PANY il M. J. BARON-SUPERVISOR
' REPORTS GROUP.
i PEACH BOTTOM ATOMIC POWER STAT;0N
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j TELEPHONE (717)456-7014 EXT.3321
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b OPERATING STATUS f
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- 1. UNIT N8E: PEACH BOTTOM UNIT 2 NOTESt~
2.-REPORTING PERIOD: FEBRUARY 1990
- 3. LICENSED. THERMAL-POWER (MWT):
3293-
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'4,NAMEPLATERATING(GROSSMWE):
1152 E,DESIGNELECTRICALRATING(NETMWE):
1065 6;MAXIMUMDEPENDABLECAPACITY(GROSSMWE): 1098 f;:
.7. MAXIMUM DEPENDABLE CAPACITY (NET MWE):
1055
-8. 1F CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST-REPORT, G1VE REASONS:
na
~I
.9.POWERLEVELTOWHICHRESTRICTED,IFANY(NETMWE):
i
- 10. REASONS FOR RESTRICTIONS, IF ANY:
-1
+
.+
y
-THIS MONTH:
YR-TO-DATE
' CUMULATIVE
- 11. HOURS IN REPORTING PERIOD -
672-
-1.416 137,232 g'..-
1
-12. NUMBER OF HOURS REACTOR WAS CRITICAL 1672.0
' 1,371.4-80,898.7-
- 13. REACTOR RESERVE. SHUTDOWN HOURS.
'O.D.
0.0 0.0 :
- 14. HOURS GENERATOR ON-LINE' 672.0 1,353.2 77,958.5 l
15; UNIT RESERVE SHUTDOWN HOURS
- 0. 0 -
0.0 0.0
- 16. GROSS THERMAL ENERGY GENERATED (MWH)
'1,690.464 3,899,064 229,195,257 L 17.GROSSELECTRICAL'ENERGYGENERATED(MWH) 546,800 1,274.200 75,334,090
- t 18.NETELECTRICALENERGYGENEP.TED(MWH) 530,213 1,236,291
,72,091,140-PAGE 1 0F 2
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OPERATINGDATAREPORT(CONTINUED)
-DOCKET NO 50 - 277 DATE MARCH 15. 1989 THIS MONTH YR-TD-DATE CUMULATIVE
- 19. UNIT SERVICE FACTOR 100.0 -
95.6 56.8
- 20. UNIT AVAILABILITY FACTOR 100.0 95.6 56.8
- 21. UNIT CAPACITY FACTOR (USING MDC NET) 74.8 82.8.
49.8
- 22. UNIT"APACITYFACTOR(USINGDERNET) 74.1 82.0 49.3
- 23. UNIT FORCED OUTAGE RATE 0.0 4.4 14.3
- 24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE DATE. AND DURATION OF EACH):
.MID-CYCLE MAINTENANCE OUTAGE, 29 DAYS, BEGINNING MARCH 3.
- 25. IF SHUTDOWN AT END OF REPORT PERIOD, ESilMATED DATE OF STARTUP:
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
FORECAST ~
ACHIEVED INITIAL CRITICALITY 09/16/73
-. INITIAL ELECTRICITY 02/18/74 COMMERCIAL OPERATION 07/05/74 PAGE 2 0F 2
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OPERATING DATA REPORT DOCKET N0. 50 - 278-DATE MARCH 15, 1989-COMPLETED BY PHILADELPHIA ELECTRIC COMPANY M. J. BARON SUPERVISOR REPORTS GROUP PEACH BOTTOM ATOMIC POWER STATION TELEPHONE (717) 456-7014 EXT. 3321 OPERAT]NG STATUS
- 1. UNIT NAME: PEACH BOTTOM UNIT 3 NOTES:
- 2. REPORTING PERIOD: FEBRUARY, 1990
- 3. LICENSED THERMAL POWER (MWT):
3293 4.NAMEPLATERATING(GROSSMWE):
1152 5.DESIGNELECTRICALRATING(NETMWE):
1065 6.MAXIMUMDEPENDABLECAPACITY(GROSSMWE): 1098
- 7. MAXIMUM DEPENDABLE CAPACITY (NET MWE):
1035
- 8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT, GIVC REASONS:
1:
- 9. POWER LEVEL TO WHICH RESTRICTED,' IF ANY (NET MWE):
10, REASONS FOR RESTRICTIONS IF ANY:
THIS MONTH YR-TO-DATE CUMULATIVE t
- 11. HOURS IN REPORTING PERIOD 672 1,416 133,128
- 12. NUMBER OF HOURS REACTOR WAS CRITICAL 672.0 1,355.3 78,514.1
- 13. REACTOR RESERVE SHUTDOWN HOURS 0.0
'O0 0.0
- 14. HOURS GENERATOR ON-LINE 661.6 1,318.5 75,720.7
- 15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0 16, GROSS THERMAL ENERGY GENERATED (MWH) 2,096,808 4,205,760 220,368,629
- 17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 691,400 1,379,100 72,251,232
- 18. NET ELECTRICAL ENERGY GENERATED (MWH) 672,745 1,341,223 69,183,691 l
PAGE 1 0F 2 5
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3 OPERATING DATA REPORT (CONTINUED)
DOCKET NO. 50 - 278
- -E DATE MARCH 15. 1989 1
THIS MONTH YR-TO-DATE CUMULATIVE 19, UNIT SERVICE FACTOR 98.5 93.1-
~56.9
- 20. UNIT AVAILABILITY FACTOR 98.5 93.1 56.9
' 21.- UNIT CAPACITY FACTOR (USING HDC NET) 96.7 91.5 50.2 22.UNITCAPACITYFACTOR(USINGDERNET) 94.0:
88.9 48.8
- 23. UNIT FORCED OUTAGE RATE 1.5 6.9 13.1
- 24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACH):
U
- 25. IF SHUTDOWN AT END OF REPORT PERIOD. ESTIMATED DATE OF STARTUP:
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):
FORECAST ACHIEVED INITIAL CRITICALITY 08/07/74 INITIAL ELECTRICITY 09/01/74 COMMERCIAL OPERATION 12/23/74 PAGE 2 0F 2
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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50 - 277:
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UNIT NAME PEACH BOTTOM UNIT 2 DATE MARCH 15. 1989 REPORT HONTH FEBRUARY, 1990 COMPLETED BY PHILADELPHIA ELECTRIC COMPANY F
M. J. BARON 9
R SUPERVISOR REPORTS GROUP i
PEACH BOTTOM ATOMIC POWER STATION TELEPHONE (717) 450-7014 EXT. 3321 METHOD OF LICENSEE-SYSTEM COMPONENT CAUSE AND CORRECTIVE TYPE DURATION REASON SHUTTING DOWN EVENT CODE CODE ACfl0N TD
. NO.
DATE (1)
(HOURS)
(2)
REACTOR (3)
REPORT f (4)
(5)
PREVENT RECURRENCE-2-
900203 0.0-H 4
N/A
-RB CONR00 CONTROL R00 PATTERN ADJUSTHENT.
REACTOR WAS NOT SHUT DOWN.
~3
'900205 F
' O.0 '
A 4
N/A HH HTEXCH 2A FEEDWATER HEATER TUBE LEAK.
REACTOR WAS NOT SHUT DOWN.
L(1)-
(2)
(3)
'(4)
F - FORCED REASON
'HETH00 EXHIBIT G - INSTRUCTIONS
~ S. SCHEDULED A-EQUIPMENTFAILURE(EXPLAIN)-
1 - MANUAL FOR PREPARATION OF DATA B - MAINTENANCE OR TEST 2 - MANUAL SCRAM.
ENTRY SHEETS FOR LICENSEE-C - REFUELING 3 - AUTOMATIC SCRAM.
EVENT REPORT (LER)
D - REGULATORY RESTRICTION 4 - OTHER (EXPLAIN)
FILE (NUREG-0161)
,E - OPERATOR TRAINING + LICENSE EXAMINATION :
F - ADMINISTRATIVE (5)
G - OPERATIONAL ERROR (EXPLAIN)
H-OTHER(EXPLAIN)
EXHIBIT I - SAME SOURCE
.