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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20045G6671993-07-0202 July 1993 RO:930702,unusual Event Declared When RCS Calculated Unidentified Leak Rate Exceeded 1 Gpm.Caused by Leakage from Reactor Coolant Pump Seal Injection Filter Drain Valve. Valves Corrected to Eliminate Leak ML20043F2961990-06-0808 June 1990 Special Rept SR-1-90-006-00:on 900509,discovered That Tech Spec Temp Limit for Main Steam Penetration Area Exceeded for Greater than 8 H.Caused by Inadequate Operating Procedure for Safeguards Bldg Ventilation Sys.Pipe Supports Insulated ML20042E5341990-04-16016 April 1990 Special Rept 1-SR-90-005-00:on 900404,positive Moderator Temp Coefficient Noted During Low Physics Testing Due to High Boron Concentration in Moderator.Rod Withdrawal Limits Imposed Per Tech Spec 3.1.1.3a,Action a.1 ML20012D9531990-03-21021 March 1990 Special Rept 1-SR-90-002:on 900221,RCS Pressure Transient Resulted in Automatic Actuation of Pressurizer Porv.Caused by Failure of Procedure to Consider Variation in Plant Response for Stated Sys.Operating Procedure Will Be Revised ML20012B8541990-03-13013 March 1990 Special Rept:On 900312,ESF Actuation Signal Occurred Which Resulted in Initiation of Train a Safety Injection & RCS Pressure Transient.Caused by Failed Blocking Diode Due to Short.Plant Restored to Stabilized Condition ML19309B8571980-03-28028 March 1980 Supplemental Ro:Violation Found Re Piping Min Wall Thickness.Cause Unstated.Engineering Review in Progress. Progress Rept Will Be Submitted by 800418 1993-07-02
[Table view] Category:LER)
MONTHYEARML20045G6671993-07-0202 July 1993 RO:930702,unusual Event Declared When RCS Calculated Unidentified Leak Rate Exceeded 1 Gpm.Caused by Leakage from Reactor Coolant Pump Seal Injection Filter Drain Valve. Valves Corrected to Eliminate Leak ML20043F2961990-06-0808 June 1990 Special Rept SR-1-90-006-00:on 900509,discovered That Tech Spec Temp Limit for Main Steam Penetration Area Exceeded for Greater than 8 H.Caused by Inadequate Operating Procedure for Safeguards Bldg Ventilation Sys.Pipe Supports Insulated ML20042E5341990-04-16016 April 1990 Special Rept 1-SR-90-005-00:on 900404,positive Moderator Temp Coefficient Noted During Low Physics Testing Due to High Boron Concentration in Moderator.Rod Withdrawal Limits Imposed Per Tech Spec 3.1.1.3a,Action a.1 ML20012D9531990-03-21021 March 1990 Special Rept 1-SR-90-002:on 900221,RCS Pressure Transient Resulted in Automatic Actuation of Pressurizer Porv.Caused by Failure of Procedure to Consider Variation in Plant Response for Stated Sys.Operating Procedure Will Be Revised ML20012B8541990-03-13013 March 1990 Special Rept:On 900312,ESF Actuation Signal Occurred Which Resulted in Initiation of Train a Safety Injection & RCS Pressure Transient.Caused by Failed Blocking Diode Due to Short.Plant Restored to Stabilized Condition ML19309B8571980-03-28028 March 1980 Supplemental Ro:Violation Found Re Piping Min Wall Thickness.Cause Unstated.Engineering Review in Progress. Progress Rept Will Be Submitted by 800418 1993-07-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E8021999-10-0707 October 1999 CPSES Unit 1 Cycle 8 Colr ML20217G4151999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Cpses,Units 1 & 2 ML20212F7671999-09-24024 September 1999 SER Granting Relief Request C-4 Pursuant to 10CFR50.55a(g)(6)(i) for Unit 2,during First 10-year ISI Interval & Relief Requests B-15,B-16 & B-17 Pursuant to 10CFR50.55a(g)(6)(i) ML20216J5701999-09-16016 September 1999 Rev 2 to CPSES Unit 2 Cycle 5 Colr TXX-9920, Monthly Operating Repts for Aug 1999 for Cpses.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Cpses.With ML20211M2981999-08-0606 August 1999 Rev 1 to CPSES Fuel Storage Licensing Rept, CPSES Credit for Soluble Boron & Expansion of Spent Fuel Storage Capacity, Consisting of Revised Title Page and 4-1 ML20210U4081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Cpses,Units 1 & 2 ML20210D8321999-07-23023 July 1999 Safety Evaluation Accepting Relief Requests Re Use of 1998 Edition of Subsections IWE & Iwl of ASME Code for Containment Insp ML20209H7661999-07-15015 July 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Comanche Peak Steam Electric Station,Units 1 & 2 ML20209H2721999-07-0909 July 1999 2RF04 Containment ISI Summary Rept First Interval,First Period,First Outage ML20209H2631999-07-0909 July 1999 2RF04 ISI Summary Rept First Interval,Second Period,Second Outage ML20209G7501999-07-0808 July 1999 SER Finding That Licensee Individual Plant Exam of External Events Complete with Regard to Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given Design, Operation & History of Comanche Peak Steam Electric Station ML20196L0191999-07-0808 July 1999 Safety Evaluation Granting Request Relief B-6 (Rev 2),B-7 (Rev2),B-12,B-13,B-14 & C-9,pursuant to 10CFR50.55a(g)(6)(i).Technical Ltr Rept Also Encl ML20210J9391999-06-30030 June 1999 CPSES Commitment Matl Change Evaluation Rept 0003,for 970802-990630 ML20209G0801999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Cpses,Units 1 & 2 ML20196J0621999-06-29029 June 1999 Safety Evaluation Supporting Proposed Changes to Emergency Plan Re Licenses NPF-87 & NPF-89 Respectively ML20195G5141999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Comanche Peak Steam Electric Station,Units 1 & 2.With ML20216E0711999-05-21021 May 1999 1999 Graded Exercise - Comanche Peak Steam Electric Station ML20206Q0091999-05-14014 May 1999 Safety Evaluation Accepting GL 92-08, Thermo-Lag 330-1 Fire Barriers, Dtd 921217,for Comanche Peak Electric Station,Unit 1 ML20206H2061999-05-0606 May 1999 SER Accepting Exemption to App K Re Leading Edge Flowmeter for Plant,Units 1 & 2 ML20196L2241999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Cpses,Units 1 & 2 ML20205R5701999-04-14014 April 1999 Rev 6 to ER-ME-067, TU Electric Engineering Rept,Evaluation of Thermo-Lag Fire Barrier Sys ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205J7831999-04-0101 April 1999 Rev 0 to ERX-99-001, CPSES Unit 2 Cycle 5 Colr ML20205N3101999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Cpses,Units 1 & 2 ML20204H6371999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Comanche Peak Units 1 & 2 ML20205N1481999-02-28028 February 1999 Corrected Monthly Operating Rept for Feb 1999 for CPSES, Units 1 & 2 ML20203A4881999-02-0303 February 1999 Safety Evaluation Granting Requests for Relief B-3 - B-6,C-2 & C-3 for Plant,Unit 2 ML20210J9201999-02-0101 February 1999 CPSES 10CFR50.59 Evaluation Summary Rept 0008,for 970802- 990201 ML20202D0101999-01-27027 January 1999 Safety Evaluation Supporting First 10-yr Interval ISI Program Plan Requests for Relief B-9,B-10 & B-11 for CPSES, Unit 1 ML20199E9961998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Cpses,Units 1 & 2 ML20207D6091998-12-31031 December 1998 1998 Annual Operating Rept for Cpses,Units 1 & 2. with ML20197K2371998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Cpses,Units 1 & 2 ML20195F3161998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Cpses,Units 1 & 2 ML20154M8841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Cpses,Units 1 & 2 ML20154B5741998-09-30030 September 1998 Safety Evaluation Re Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Motor-Operated Valves. Licensee Has Established Acceptable Program ML20151W0361998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Cpses,Units 1 & 2. with ML20151Q1211998-08-14014 August 1998 Rev 0 to Control of Hazard Barriers ML20237C4061998-08-14014 August 1998 Safety Evaluation Supporting Request to Implement Risk Informed IST Program ML20237C6721998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Cpses,Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236R0711998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Cpses,Units 1 & 2 ML20249B2581998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Cpses,Units 1 & 2 ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20247G3241998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Cpses,Units 1 & 2 ML20216B8661998-04-0101 April 1998 Rev 0 to ERX-98-001, CPSES Unit 1 Cycle 7 Colr ML20216J3061998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Cpses,Units 1 & 2 ML20216J1861998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Comanche Peak Steam Electric Station ML20197A6951998-02-24024 February 1998 Inservice Insp Summary Rept,First Interval,Second Period, First Outage ML20199J5391998-02-0202 February 1998 CPSES Commitment Matl Change Evaluation Rept 0002 for 960202-970801 1999-09-30
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- ll'E:ll:- Log- # TXX-90114
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- - -File # 10250-905.4 nlELECTRIC March 21, l990
- Wmiasm J. CahiR. Jr.
Emunvr nt brMrM Mr.:R.:D. Martin,-'RegioniIV i
U. S. Nuclear Regulatory Commission l611 Ryan. Plaza, Suite 1000,
' Arlington. Texas 76011
SUBJECT:
COMANCHE' PEAK STEAM-ELECTRIC' STATION (CPSES)
DOCKET NO. 50 445 AUTOMATIC OPERATION OF PRESSURIZER PORV IN RESPONSE TO A LTOP SIGNAL SPECIAL REPORT NO.'l-SR-90-002 Gentlemen:-
. Enclosed:is- a 30 day special report submitted in accordance with CPSES Unit 1 Technica11 Specification 3.4.8.3, " Reactor Coolant System Overpressure
_ Protection Systems."
Sincerely.
William J. Cahill; Jr.
By: W
'D.~R. Woodlan Docket Licensing Manager JLR/vid Enclosure-c Document Control Desk
- U. S. Nuclear Regulatory Commission Washington D. C. 20555-Resident Inspectors. CPSES (3) 900321 %
j900329014j DR ADOCK 05000445 Ed
,[/'f, PDC w M
400 North Olive Street L.B. 81 Dallas. Texas 75201 2
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(. IEnclosura TXX 90114 fpagt 1 of 23 .
w i
. . TU Electric Comanche Peak Steam Electric Station, Unit 1 Docket No. 50-445 q
Automatic Operation of Pressurizer Power Operated Relief Valve in Response to -
a Low Temperature Overpressure Protection Signal Special Report No.1-SR 90-002-00 ;
1.0' REPORT REQUIREMENT On February 21,1990, a Reactor Coolant System (RCS) pressure transient -
resulted in the automatic actuation of a Pressurizer Power Operated Relief Valve (PORV). This Special Report is being submitted in accordance with Comanche Peak Steam Electric Station Unit 1 Technical Specification 3.4.8.3, REACTOR -
COOLANT SYSTEM OVERPRESSURE PROTECTION SYSTEMS LIMITING
' CONDITION FOR OPERATION. Specification 3.4.8.3 requires that a Special y Report be submitted to the Nuclear Regulatory Commission pursuant to ',
Specification 6.9.2 describing any event in which a Pressurizer PORV, or the Residual Heat Removal suction relief valves, or the RCS vents are used to : !
mitigate a RCS pressure transient.
E i 2.0 ' EVENT DESCRIPTION On February 21,1990, at approximately 1317 CST, with the plant in cold '
ll shutdown and RCS temperature at 140 degrees F, a Pressurizer PORV L automatically opened in response to a Low Temperature Overpressure .
l Protection (LTOP) signal Just prior to the event the RCS fill and vent procedure had been completed up to the vent of the RCS following the fourth Reactor Lr Coolant Pump (RCP) one minute run. At the time of the event, the RCS was in a lf water solid condition and was being pressurized to 325 psig in preparation for L the RCP ten minute runs. Letdown flow had been reduced to a flowrate less than the charging flowrate, resulting in an increasing RCS pressure. The solid plant l pressure response to the reduced letdown flowrate was quicker than anticipated by the Reactor Operator (RO) and resulted in RCS pressure exceeding the target L: - value. The RCS reached a maximum pressure of 436 psig. The system functioned as designed, causing a Pressurizer PORV to open for approximately 4 seconds, preventing the RCS pressure from exceeding the applicable limits. The ;
n RO. reduced charging flow and increased letdown flow, stabilizing RCS pressure E at 260 psig within two minutes. A review of recorded data subsequent to the event verified that the open PORV resulted in a drop in RCS pressure to 350 psig and a corresponding rise in the Pressurizer Relief Tank level.
E: , 4 E5 closure TXX-90114 r
i
.I 3.0 CAUSE OF EVENT' I
E .
The following have been identified as causes for the event:
-+ The procedure for filling and venting the RCS requires that the operator perform an iterative process, but does not consider the variation in plant _ i
. response to identical instructions in going from a system containing air to a -
water solid system. The procedure does not adequately caution the RO of '
the change in expected plant response.-
-The process for pressurizing the RCS following' a vent had been to :
completely isolate letdown flow resulting in a loss of-letdown flow alarm ;
for the failed fuel monitor. The alarm, which should have alerted the RO to insufficient letdown flow, had become an expected alarm.
- 4.0 CORRECTIVE ACTION' The pressure transient was discussed with the RO, and the need for increased board awareness during solid plant operations was reinforced. A Lessons ,
Learned summary was reviewed by all crews, and increased sensitivity of the ,
' plant to changes in letdown and charging was discussed
~
' T_he operating procedure will be revised as follows to incorporate lessons learned from this event:
- Eliminate repetitive steps for which differing plant responses are expected, a Instruct the operator to avoid completely securing letdown flow, ensuring normal operation of the failed fuel monitor, and adequate operator response to a loss-of-flow alarm,
. Cautions will be added to alert the operator of expected plant responses in transitioning from a system with air to a water solid system,-
- Incorporate instructions for establishing a pressurizer bubble using decay-heat and pressurizer heaters prior to starting an RCP in order to reduce the number of evolutions occurring during solid plant opertations.
I 1
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