05000260/LER-1981-049-03, /03L-0:on 810927,containment Atmosphere Dihydrogen Analyzer Removed from Svc for Maint for Approx 3.5-h.Caused by Tripping of Sample Return Pump Due to Setpoint Drift on Vacuum Switch.Switches Calibr

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/03L-0:on 810927,containment Atmosphere Dihydrogen Analyzer Removed from Svc for Maint for Approx 3.5-h.Caused by Tripping of Sample Return Pump Due to Setpoint Drift on Vacuum Switch.Switches Calibr
ML20011A852
Person / Time
Site: Browns Ferry 
Issue date: 10/26/1981
From: Holder G
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20011A850 List:
References
LER-81-049-03L-03, LER-81-49-3L-3, NUDOCS 8111030286
Download: ML20011A852 (2)


LER-1981-049, /03L-0:on 810927,containment Atmosphere Dihydrogen Analyzer Removed from Svc for Maint for Approx 3.5-h.Caused by Tripping of Sample Return Pump Due to Setpoint Drift on Vacuum Switch.Switches Calibr
Event date:
Report date:
2601981049R03 - NRC Website

text

NBC FOR,A 366 U. S. NUCLEAR REGULATORY COMMIS$10N (7 77)

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60 61 DOCKET NUMBER 68 69 EVENT DATE 14 l's REPOhT DATE 80 EVENT OESCRIPTION AND PROBABLE CONSEQUENCES h l o 12 ] l During normal operation, containment atmosphere IL, analyzer was removed from service l

o ;3; l for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 37 minutes for maintenance, due to sample return pump tripping.

I j o l4 l l 2 - If m-76-104 was declared inoperal.

during this time. (T. S. 3. 7. II. 2) There was 1

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CAUSE OESCRIPTION AND CORRECTIVE ACTIONS 77

[ i j o l l Setpoint drif t on the Static-0-Ring model 54NN-KA-YI-CIA vacuum switch caused the 1

[ i li l l sample return p.np to trip. Switches pS-76-103B and pS-76-104B were calibrated.

I ii;7i j adjusted to wichin prescribed setpoint limits, and returned to service. This is 1

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. Antification and in.cript:an f ( L currence 11., analyzer was removed f rom service for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 37 minutes for maintenance m-76-104 was declared inoperable during due to sample return pump tripping.

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this time.

t' nditions i rior

  • o ()ccu: rence Unit 1 in refueling outage.

Unit 2 at 99%.

Unie 3 at 97%.

.i c t a.:-

,pecifi d in t he Technica! Specification Surveiiiance Heiluiremenb met h. inoperalde equipment.

Ded e t. ib e. _ _

v None

' Pim ent C a u :> e )f ( Ee.. renct-Setpoint drift on the vacuum switch caused the sample return pump to trip.

.b, p.s of, Occu rrent.

There was no danger to the health or safety of the public, no release of activ'ty, no damage to the plant or equipment, and no resulting significant chain of evei.ts, f'

n ( t ice /.M ion :

Switches PS-76-103F, and PS-76-104B were calibrated, adjusted to within prescribed setpoint limits, and returned to service. This is considered a randon failure and no further recurrence control is required.

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f i c <. p.: sibility - Document C.)nt rol Supervisor

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