ML20011A416

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Monthly Operating Rept for Sept 1981
ML20011A416
Person / Time
Site: FitzPatrick 
Issue date: 10/01/1981
From: Zufelt E
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
Shared Package
ML20011A415 List:
References
NUDOCS 8110130324
Download: ML20011A416 (4)


Text

OPERATING DATA REPORT DOCKETNv. 50-333 DATE October 1981 COMPLETED BY E. Zufeg TELEPi10NE (X15)347 X840 OPERATING STATUS Notes

1. Unit Name:

Fit 2 Patrick

2. Reporting Period:

810901-810930 2436

3. Licensed Thermal Power (MWI):

883

4. Nameplate Rating (Gross AlWe):
5. Design Electrical Rating (Net AlWe):

R21 C. Masimum Dependable Capacity (Gross MWe):

830 810

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

NONE

9. Power Level To Which Restricted,If Any (Net MWe):

NONE

10. Reasons For Restrictions.lf Any:

nis Month Yr.-to.Date Cumulative I1. Ilours in Reporting Period 720 6551 5416S

12. Number Of Ilours Reactor Was C-itical 720 591'.7 XSS26.7
13. Reactor Reserve Shutdown flours 0

0 0

14. Ilours Generator On-Line 720 5818.5 3'~?1.3
15. Unit Reserve Shutdown flours 0

0 0

16. Gross Thermal Energy Generated (MWil) 1274208 13033872 77217466 t 7. Gross Electrical Energy Generated (MWil) 442690 4511510 26341020 if. Net Electrical Energy Generated (MWil) 435215 4373365 25498445
19. Unit Service Factor 100. 0'e 88.8%

69.6*6

20. Unit Availability Factor 100.0*6 88.8%

69.6%

21. Unit Capacity Factor (Using MDC Net) 74.6*6 82.4%

6 3. 0*r,

22. Unit Capacity Factor (Using DER Net) 73.6*6 81.3*6 57.3*6
23. Unit Forced Outage Rate
0. 0*6 11.2%

17.2's

24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Eachli Refueline and maintenance outace scheduled to commence in October.

Dtiration is presentiv planned for 110 days.

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation):

Forecast Achieved INITIAL CRITICA LITY INITIA L ELECTRICITY COMM ERCIAL OPER ATION

'8110130324 811002

.PDR ADOCK 05000333 g

PDR

~

50-333 DOCKET NO.

UNIT SliUTDOWNS AND POWER REDUCTIONS UNIT NAME JAFNPP DATE October 1981-COMPLETED BY E. Zufelt REPORT MONTH September.1981 TELEPilONE r3151312-3Rta

's E

c w

!?

3

$5 Licensee

,E v,

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Cause & Corrective No.

DJte F

E2 s

2 E5 Event 3 '2 c.

Action to e

.5 5 =!

Report a NC

!0 Prevent Recurrence e

V 6

NONE l

l l

I 2

3 4

F: Forced Reason:

Method:

Exhibit G. Instructions S: Scheduled t Equipment Failure (Explain) 1 Manual for Preparation of Dat i B Maintemnce of Test 2-Manual Scram.

Enta Sheets for Li;ensee C Refueling 3 Automatic Scram.

, Event Report (LER) File (NUREG D-Regulatory Restriction 4 Other (Explain) 0161)

E-Operator Training & License Examination F-Administ rative 5

G Operational Error (Explain)

Exhibit I - Same Source ll-Other ( Explain)

POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT SAFETY RELATED F.LECTRICAL a MECHANICAL MAINTENANCE

SUMMARY

September 19PJ K REO ES DATE SYSTEM HOW OETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE T

EN 8/25/81 08 4993 Short circuit in cable Replaced cable 72 OPS ue t fled ng.

Refuel l

Bridge J

9/15/81 27 8714 Bench test Centrifugal switch hitting Spliced wire S taped back 3

Spare metal

wire, i

bellows pump i

i

]/23/81 10 14085 OPS Vibration.

Replaced hand wheel 2

RilR-24A l

o k

(

JAMES A. FITZPATRICK NUCLEAR POWER PLANT Maintenance Summary ISC September 1981 rk Request #

Cause of Results of Action taken to Repair Date System How Detected Component #

Malfunction R.1 function Preclude Time Recurrence (Hours) 13969 Recorder not Tightened set l

9/18/81 17 RR-433B OPS Loose set screw correct screw 4.0 14430 Replaced defective 9/15/81 17 RIS-432A OPS Use/ Age Erratic slidewire 14.0 I

9/15/81 17 OPS Drift Calibrated 14.0 R S-32B hg

  1. #*i 6

'po[t Replaced switch 9/23/81 23 IfC Age /Use 2.0 p3, 3

l I

14571 l

0 AZ-101A OPS Drift Downscale Adjusted zero 4.0 2

l 12079 Pens stuck 973733

'7 OPS Stripped bu11 gear downscale Replaced gear 5.0 3

l RR-104A 12423 Indication out Replaced gauge

{

I l

9/28/81 76 P2-P1 OPS Age of tolerance and calibration 8.0 t

ll 13966 9/24/S1 76 OPS Unknown Damaged Replaced 5.0 P1-105 Spuri us alarms Replaced card 4.0 9/23/81 76 F re panel OPS ad t

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