05000318/LER-1981-042-03, /03L-0:on 810821,pressurizer Level Deviated from Program Level by More than 5%.Caused by Normal Startup Operations

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/03L-0:on 810821,pressurizer Level Deviated from Program Level by More than 5%.Caused by Normal Startup Operations
ML20010G034
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 09/04/1981
From: Junge M
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010G021 List:
References
LER-81-042-03L, LER-81-42-3L, NUDOCS 8109150253
Download: ML20010G034 (1)


LER-1981-042, /03L-0:on 810821,pressurizer Level Deviated from Program Level by More than 5%.Caused by Normal Startup Operations
Event date:
Report date:
3181981042R03 - NRC Website

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NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7 771 LICENSEE EVENT REPORT CONTRO BLOCK: l l

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8 60 61 DOCKET NUMBER 68 63 EVEN T DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121l At 1640 during routine niant start-up. nressurizer level devinted from I

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