LER-1981-043, /01T-0:on 810815,4,160-volt Shutdown Board U-2 Was Made Critical from Cold Condition W/Start Bus Undervoltage Relays Out of Svc for Start Bus 1A.Caused by Personnel Error.Relays Were Reconnected |
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3 U. S. NUCLE A") CEGULATORY COMMISSION.
NRc FOsts ass (7-7H 4
LICENSEE EVENT REPORT
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C LVENT DESCRIPTION AND PRO /4dLE CONSEQUENCES h c
shutdown l
8,1 On 8/15/81 at 2102, while_ performing modificating on U-1 and U-2 4160 volt boards, U-2 was made critical from a cold condition with start bus undervoltage relays l o
I l out of service for the 1A start bus. (T.S. 3.9.A.4.e).
This condition was not
,i o 4 determined until 8/19/81 at 1145. There was no danger to the health or safety of I
0 s,1 g I the public. Redundant systems were available and operable. There were no previous l
l o i i similar events.
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40 el 42 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h During preliminary review of modification workplan which contained l M l Personnel arror.
it was not I
i the removal from service of the 1A start bus undervoltage relays, i i The relays l
g i recognized that the Tech. Spec. 4.9.A.4.e did not permit this activity.
This is considered a random
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@ l were reconnected immediately on discovery of error.
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@ l event and no further recurrence control is required.
DISCOVERY DESCRIPTION h 7
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Form HF 17
'l@nness,cc Valley Authority DF 15.2 llrowns Ferry Nuclear Plant 6/04/81 1,Rit SUPPL.liMENTAl. INFORMATION DFitO-50.,26,0. /.81043 Technical Specification involved 3.9.A.4.e_, _ _,
Heported Under Technical Specification,6_.7.2.a(2)
- 1) ate of Occut rence _ 8/15/81 Time of Occurrence,2102 -
,,, U n it 2
Identificati0n and 1)escription of Occurrence While performing modification on U-1 aid'0-2' 4160 voit shutdown boards, U-2
~
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was made criticd1 from a cold condition with start bus undeivoltage relays out>
of service for the 1A start bus.
i-Conditions Prior to Occurrence:
Unit i refuel Fg outage.
~
Unit-2 in routine startup.
Unit 3 at 95%.
l I
Action specified in the Technical Specification Surveillance Requirements met f
due to. inopepi e enipment. Des _cribe.
bl i
Nona l
t Personnel error. During preliminary review of j
Apparent Cause of Occurrence:
l inodification wdrEpTali which c'5ntained the removal from service of the 1A start l
bus undervoltage relays, it was not recognized that the Tech. Spec. 3.9.A.4.e There was another separate modification and work-did not permit this activity.
to be done relating to degraded voltage which existing Tech. Spec did allow.
i plan It was recognized start bus initiated logic modification needed to be done at the l
However, it same time separate degraded voltage modification was being done.
was not recognized start bus modification required a Tech. Spec. change which had l
I been submitted to-NRC but not approved.
There was no danger to the health or safety of the public, Analysis of Occurrence:
no release of activity, no damage to the plant or equipment, and no resulting significant chain of events.
Corrective Action
Undervoltage start bus relays were reconnected immediately i
This is considered a random event and no further upon discovery of the error.
control is required.
I recurrenc.!
1 Ifailure Data:
None
.Itetention :
Per' d - 1.ifetime; Responsibility - Document Control Supervisor
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