ML20010C449

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Monthly Operating Repts for Jul 1981
ML20010C449
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 08/10/1981
From: Harrison F
CAROLINA POWER & LIGHT CO.
To:
Shared Package
ML20010C448 List:
References
NUDOCS 8108200093
Download: ML20010C449 (10)


Text

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f/' . APPENDIX M

DOCKET NO: 050-0325

' UNIT: Brunswick 'No. I' DATE: August 1981 COMPLETED BY: Frances Harrisoa OPERATIONS

SUMMARY

BRUNSWICK UNIT NO.1

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Brunswick Unit No. I was off the line for~the entire month of July for a planned maintenance outage.

There are 476 BWR and 160 PWR spent fuel bundles in the Brunswick Unit No.1 fuel pool.

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-APPENDIX B 2 AVERAGE DAILY. POWER LEVEL 9 t

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3 DOCKET NO. 050-0325  ;

!! UNIT BRUNSWICK UNIT.l' '

DATE-08/03/81 . .

' COMPLETED BY FRANCES HARRI'60N

TELEPHONE 919-457-9521.

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.JULYL81 i.

.. . .. .i i  ; DAY AVG. DAILY POWER LEVEL DAY AVG. DAILY: POWER LEVEL

j. (MWE-NETL (MWE-NET) i '

1 -8. 17 -8.  !

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j. ~2 -8. 18 -10.

-3 -9. 19' -10. -

4 -11. 20 -10.  !

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! 5- -12. 21 -10.

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j 6 -13. 22 -11.  !

[ 7 -14 23 -10.  !

I' i j 8 -11. 24 -10. i j 9. -7 25 -10. l i- i

.10 -7. 26 -10. I r

[ 11 -9. 27 -9.

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! 12 -8. 28 -9. j i

i I' 13 -9. 29 -9. -l i

14 -10, 30 -9.  !

' 15 ~9 31 -9.

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16 -10.

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n .c l0PERATING' DATA REPORT ~

DOCKET NO.'050-0325~

DATE 08/03/81 COMPLETED BY FRANCES HARRISON TELEPHONE 919-457-952

' OPERATING STATUS-l- 1. UNIT NAME: BRUNSWICK UNIT'1 I NOTES I

2. REF ORTING PERIOD: JULY 81 I I.
3. L)CERSED THERMAL POWER (MWT):'2436 I I
4. NAMEPLATE RATING-(GROSS MWE): 867.0 I Iz
5. DESIGN ELECTRICAL ~ RATING (NET MWE): 821.0 I I 6.JMAX DEPENDABLE CAPACITY (CROSS MWE): S15.0 -I I
7. MAX DEPENDABLE CAPACITY (NET.MWE): 790.6 -------------------------------

9.'IF CHANGES.0CCUR IN CAPACITY RATINGS (ITEMS 3 THRU 7) SINCE LAST REPORT, GIVE REASONS:

9. DOWER LEVCL TO WHICH RESTRICTED IF ANY (NET MWE): NONE
10. REASONS FOR .7ESTRICTION IF ANY:

THIS YR TO CUtR'L MONTH DATE ATIVE

11. HOURS IN REPORTING PERIOD 744.0 5087.0 38328.0
12. NUMBER OF HOURS REACTOR WAS CRITICAL 39.3 2173.6 25975.7
13. RE4CTOR RESERVE SHUTDOWN HOURS 0.0 0.0 1647.1
14. HOURS GENERATOR ON LINE 0.0 2056.8 24438.7
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
16. GROS; THERMAL ENERGY GENERATED (MWH) 0.0 3841575.6 49965308.5 17.-GROSS ELECTRICAL ENERGY GENERATED (MWH) 0.0 1256185.0 16581779.0
18. NET ELECTRICIAL ENERGY. GENERATED (MWH) -7182.0 1192167.0 15939601.0
19. UNIT SERVICE FACTOR 0.0 40.4 63.8
20. UNIT AVAILABILITY FACTOR 0.0 40.4 63.8
21. UNIT CAPACITY FACTOR (USING MDC NET) -1.2 29.7 52.6 2,I . UNIT CAPACITY FACTOR (USING DER NET) -1.2 28.5- 50.7
23. UNIT FORCED OUTAGE RATE 0.0 8.3 17.4 24 SHUTDOWNS SCHEDULED OVER'NEXT 6 MONTHS (TYPE, DATER At:D DURATION OF EACH):

25.-IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF START UP: 9/25/8'

26. UNITS IN TEST STATUS (PRIOR TO COMMERICIAL OPERATION): FORCAST ACHEIV'D INITIAL' CRITICALITY -------- --------

INITIAL ELECTRICITY -------- --------

COMMERICIAL OPERATION -------- --------

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UNIT SIIUTDOWNS AND POWER REDUCT10NS UNIT N AME arunswick i DATE Aucust 19R1 _

F"' " " "*""i=on COMPLETED BY REPORT SiONT., July 19R1 TELEP!IONE (919) 457 4991

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E E

Cause & Cortcetive

.$ g 3 42E Liecnsec ,E r, y'^], Action to

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Event i No. Date  :- 73 2 4 E E E~ gG EO Prevent Recurrence

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Report # 6 ~

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S 744 B 1 N/A Itaintenance Outape l * .

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1 2 Alethod: Exhibit G Instructions Reason: for Preparation of Data F: Forced 1 -hf anual S: Scheduled A.I~quipment Failure (Explain) 2-Manual Scrarn. Entry Sheets for Licensee 11 Maintenance of Test 3 Automatic Scram. Esent Report (LER) File (NUREC.

4 C Itefuelmg 4 Continuations 0161)

D.Itegulatory Itestriction E Operator Training 1 License Examination 5-Load Reductions 3 F-Administrative 1 6-Other Exhibit 1.Same Sourec C. Operational Error (Explain) [

9/77) liother(Explain) i

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OPERATING. DATA' REPORT ,

DOCKET NO. 050-0324

~DATE 08/03/91 COMPLETED BY FRANCES HARRISON.

TELEPHONE 919-457-9521. a OPERATINGjSTATUS ,

1.. UNIT NAME: BRUN9 WICK UNIT 2 I NOTES I 4

7. REPORTING PERIOD: JULY 81 I I ,
3. L JCENSED THERMAL POWER (MWT): 2436

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. 4. NAMEPLATE RATING (GROSS.MWE): 867.0 I I

'5. DESIGN ELECTRICAL inifNG (NET MWE): 921.0 I I

6. MAX DEPENDABLE CAPACITY-(GROSS MWE): 815.0 I I
7. MAX LEEPENDABLE CAPACITY (NET MWE): 790.0 ---------- ------------------~~ '
8. IF CHANGES OCCUR IN CAPACITY. RATINGS (ITEMS 3 THRU 7) 52NCE LAST REPORT,

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GIVE REASONS:

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'9 POWER LEVEL TO WHICH RESTRICTED IF ANY (NET MWE): NONE

10. RE950NS FOR RESTRICTION IF ANY:

THIS YR TO CUMUL MONTH DATE ATIVE

11. HOURS IN REPORTING PERIOD 744.0 5087.0 50352.0

'12. NUMBER OF HOURS REACTOR WAS CRITICAL 505.3 2724.4 31746.7'

13 REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 0.0 1/ HGURS GENERATOR ON LINE 443.6 2447.2 29411.5.

- UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0

o. GROSS THERMAL ENERGY GENERATED (MWH) 775438.1 4033239.2 53644620.1 ,

1 .7. GROSS ELECTRICAL ENERGY GENERATED (MWH) 137571 0 1364545.0 17928991.0 l id. NET ELECTRICIAL ENERGY GENERATED (MWH) 244569.0 1290837.0 17196266.0

19. UNIT SERVICE FACTOR 59.6 48.1 58.4-
20. UNIT AVAILABILITY FACTOR 59.6 48.1 58.4
21. UNIT CAPACITY FACTOR (USING MDC NET) 41.6 32.1 43.2-

.2. UNIT CAPACITY FACTOR (USING DER NET) 2 40.0 30.9 41.6

23. UNIT FORCED OUTAGE RATE 40.4 S0.0- .18.3 24.-SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):
25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF START UP: ~0/ 0/ 0
26. UNITS IN TEST STATUS (PRIOR TO COMMER1CIAL OPERATION): FORCAST ACHEIVED. '

1NITIAL CRITICALITY --------- --------

INITIAL ELECTR: CITY -------- --------

-COMMERICIAL OPERATION --------- - - - - - - - -

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APPENDIX B AVERAGE DAILY POWER LEVEL l

l, DOCKET NO. 050-0324

~ UNIT BRUNSWICK ~ UNIT-2

[' DATE 08/03/81-ij *'c '

l COMPLETED BY FRANCES.HARFISON l . TELEPHONE 919-457-9521 l'

l l TVULY181 i-

f. DAY AVG. DAILY POWER LEVEL DAY AVG. DM Y POWER LEVEL -

"- (MWE-NET)- -(MWE-NET) l l

l-1- '682. 17 623.

I 2 46. 19 142. l 3 192. 19 -15.

4 534. 20 -14. --

l 5 660. 21 -14.

6 663. 22 -13.

3 7~ 674. 23 - 1 ~2 .

l 8 661. 24 -11.

9 654. 25 -12.

I 10 670. 26 '

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i 11 82. Zi -11.

12 -4. 28 258.

13- 414. 29 353.

14 608. 30 413. .j 1

S '31 669. 675. l l

16 634. l l'

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APPENDIX DOCKET NO: 050-0324 UNIT: Brunswick No. 2 DATE: '.ugust 1981 COMPLETED BY: Frances Harrison OPERATIONS

SUMMARY

BRUNSWICK LHIT NO. 2 Brunswick Unit No. 2 operated at a 59.6% availability factor for the montt. of July with 41.6% capacity factor. There were three "off-line" outages this month, they are detailed in Appendix D, the unit shutdowns and power reductions log.

There are 264 BWR and 144 PWR spent fuel bundles in the Brunswick Unit No. 2 fuel pool, w -_

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UNIT SilUTDOWNS AND POWER REDUCTIONS h E f.,h Brunsu e ?

DATE A"R"St 1981 -

COMPLETED BY Frances tiarrison July 1981 TELEP!!ONE

( 919)4ai-n21 REPORT MONTil

-, .$ g 3 .7h Licensee Event

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c-3 Cause & Corrective Action to Date c- E i E E J~ Prevent Recurrence No.

u$O Report - rN 0

  1. 5s e 3e di

- C 81-019 81/07/03 F 32.8 B 3 N/A CD VALV0P Failure of.2-B21-F022C MSIV (inboaru) .

disk separated from. stem. Outage was extended because of loss of feedwater

- codtrol. .

. Shut 2-B21-F028C, hung Shift Foreman's clearance on both F022 & F028G.

-s Repressurizing to reactor pressure prior to valving.

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I 2 Method: Exhibit G. Instructions F: Forced Reason: 1 M.mual for Pseparation of Data S: Scheduled A l'qmpment liilure (Explain) 2 Manual Scrarn. Entry Sheets for Licensee n Mainte unee or Test 3 Automatic Scram. Esent Reper 'LERI Fi:e(NUREG-C Refueling 0161)

- D Regulatory Restrietion 4 Continuations E-Operator Trainmga Licenw Examination 5-Load Reductions 5 F-Administrative 6-Other Exhibit I- Same Souree

  • i G Operational Error (Explain) -

l Il Other (Explain)  ;

(9/77)

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DOCKET NO. 050-0Us 9

UNIT SilUTDOWNS AN9 POWER REDI.'CTIONS UNIT NAME T ri m eA <-t-DATE Anonne 1991 COMPLETED BY _ Frances p,rrhon July 1981 ( 91914 57-o c;?1 REPORT MONTil TELEPl!ONE 1

1, Cause & Corrective

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.3 y J Event sy c3 Date 5- 4 NV Prevent Recurrence u!"

N**. i Report #

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N/A Outage cause being invastigated 81-020 81/07/1L 1 40.2 A 3 -

by Engineering *

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I 2 Method: Exhibit G-Instructions fleason . for Preparation of Data F: ForecJ 1. Manual Entry Sheets for Licensee S: Scheduled A 1 qmpment railure (E- ain) 2 Manual Scram.

11 Maintenance of Test - Esent Report (LER) File (NUREC.

3.Aurumatic Scram.

C Itefuehng 4 Continuations 0161)

D Itegulatory liestriction E Operator Training & License Examination 5-Load Reductions I F Adnnnistrative 6-Other Exhibit ! Same Sourec

  • G Operational Error (Explain)

($1/77) It Other (Exr. lain)

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DOCKET NO. 050-0325 UNIT SliUTDOWNS AND POWER REDUCTIONS UNIT N A*.lE Brunswick 2 DATE August 1981 COMPLETED BY Francac u,rricon REPORT MONTil July 1981 TELEPliONE (otous7 out

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. ~45 Licensec ,E g E*

o. Cause & Correetive No. Date g 3g g ,g y 5 Event :t y c3 /.etion to o$U H 5 3i5 Report - 'N U Prevent Rscurrence

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~ .81-021 8/07/81 F 227.4 A 1 N/A CD VALV0P MSIV Repairs Removed and repaired stem disc assembly and ensured stem and '

, disc were pinned properly a

s 3 4 1 2 Reason: Method: Exhibit G -Instructions F: Forced for Preparation of Data A Fquipment Failure (Explain) 1. Manual S: Scheduled Entry Sh:ets for Licensee

[1 Maintenance of Test 2 Manual Scram.

C Refueling 3-Automatic Scram. Event Report (LER) File (NUREG.

D Regulatory Restriction 4 Continuations 0161)'

E-Operator Training & License Examination 5-Load Reductions 5

F-Admimstrative 6-<)ther Exhibit I Same Source G Operational Error (Explain) '

(*)/77) li-Other (Explain) -