05000260/LER-1981-037-03, /03L-0:on 810708,value for R Factor Found Out of Limits.Caused by Extenuating Circumstances Delaying Actions Necessary to Maintain Compliance W/Limit.Personnel Briefed on Close Monitoring of R Factor During Startup

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/03L-0:on 810708,value for R Factor Found Out of Limits.Caused by Extenuating Circumstances Delaying Actions Necessary to Maintain Compliance W/Limit.Personnel Briefed on Close Monitoring of R Factor During Startup
ML20010B004
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 08/05/1981
From: Holder G
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010B003 List:
References
LER-81-037-03L, LER-81-37-3L, NUDOCS 8108130208
Download: ML20010B004 (2)


LER-1981-037, /03L-0:on 810708,value for R Factor Found Out of Limits.Caused by Extenuating Circumstances Delaying Actions Necessary to Maintain Compliance W/Limit.Personnel Briefed on Close Monitoring of R Factor During Startup
Event date:
Report date:
2601981037R03 - NRC Website

text

NRC OT3 361 U.S. NUCLEAR RE!ULATORY COMMISSION (777) a LICENSEE EVENT REPORT

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60 81 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT OESCRIPTION ANO PROB ABLE CONSEQUENCES h J'o"TTI l Durine start up. while the unit was ascending to full power. SI 2.1 was performed to l

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Tenndssee Valley Authority Form BF 17 firowns Ferry Nuclear Plant DF 15.2 6/04/81 l.Rit SUPPL.EMENTAl, INFORMATION H F RO 260 f 81037 Technical Specification involved,,4.1.B 0/7/01 licported Under Technical Specification 6.7.2.b(2)

  • Date due NRC-Date of Occurrence 7/8/81 Time of Occurrence _2355,_ Unit _, 2 Identification and Description _of,_ Occurrence:

During start up, while the unit was ascending to full power, SI 2.1 and the value for R factor were out of limits.

Conditions Prior to Occurrence:

Unit 1 in refueling outage.

Unit 2 at 50%.

Unit 3 at 100%.

Action specified in the Technical Specification Survei"ance Requirements met due to inoperable equipment.

Describe.

None APRarent Cause of_ Occurrence:

A combination of extenuating circumstances (i.e., TIP problems, start up functions, Xenon) delayed the actions necescary to maintain compliance with the limit.

Analysis of_ Occurrence.

There was no danger to the health or safety of the public, no release of activity, no damage to the plant or equipment, and no resulting significant t

chain of events.

Cor_rective Action:

Control rod moves in conjunction with R factor setpoint, placed R factor in limits to perform SI 2.1 successfully. STA's were briefed on diose monitoring of R factor during start up.

Failure Data: BFRO-50-260/81018.

. Retention :

Per' d - Lifetime; Responsibility - Document Control Supervisor

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