LER-1981-034, /03L-0:on 810630,RHR Svc Water Pumps B2,D-1 & D-2 Were Not in Svc.Caused by Removing B2 from Svc to Change Motor Oil & Tagging Closed Crosstie Valve to Unit 1, FCV-1-74-100.Oil Changed |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2601981034R03 - NRC Website |
|
text
..
. (7 m I LICENSEE EVENT REPORT e
CCNT ACL BLCCK: l l
l 1
I l
(PLEASE PRINT OR TYPE ALL REQUtRED INFORMATIONI lo lil l 31 T_I 31 o f el 21@l ol nl I ol ol ol 01 o l l 01 O l@l 4 I i l 11 il ll@l I
l@
14 15 LICENSE NUM6ER 2$
26 LaCENSE TYPE JO Si CAT 58 7
8 $
LeCENSEE COCE lolil juRCE lL@l0151010]Ol2l610@l016!3l01Slll@l017 12 12 18 11 l@
, CCN'T 60 61 DOCKET NUMBER 68 69 EVENT OATE 74 75 REPCRT QATE 60
?
EVENT OCSCRIPTION AND PROB ABLE CONSECUENCES h lo i2i ! During normal coeration. the RHRSW oumo 32 was removed from service to change oil l
10 j a j i in the motor. This left only one pump (31) aligned to unit 2 and to unit 3 for l
2 was reduced to one cump because the crosstie valve to Unit 1,l [oi4l l standbv coolant. Unit Pump l l o i s i 1 FCV 74-100 was tagged closed eliminating D-1 and D-2 RHRSW pumps from service.
10 IG 1 1 31 is cot cson to units 2 and 3 for,tandbv coolant. See T.S. 3.5.C.3.
There was no l
i o i 7 I l dancer to the health or safety of the oublic and no orevious aimilar events.
l I
6 o is ! I SYSTEM
CAUSE
CAUSE COMP.
'VA LV E CCOE CCCE SU8COCE COMPCNENT CCOE SUSC00E SUSCOCE loiol
- cl =l@ l xl@ l zl@ I z l z l z i z l z i z l@ Iz l@ U @
7 e
9 13 11 12 13 18 19 20 SE CUENTI AL CCCU R R ENCE REPCRT R Eyt$1CN gq EVENT ve4R REPCRT No.
CCCE TYPE No.
O a(g:,pg i a ! tl 1-1 I n l,141 Ld to13I I ti l_J 10 I ar
,_ 21 22 23
!4 26 27 28 29 30 31 32 ACTICN FUTURE EFFECT SHUT 0owN ATT ACMM E NT NPRO-4 PRIME COMe.
COMPONENT TAKEN ACTION oN *LANT METMCC woVR$
$U8MiTTED FORM hUS.
$UP9(!E P.
MANUFACTURER LxJ@l z l@ -' z i@
l z l@
Iofo!olol I Y l@
INi@
ILI@
III919191@
34 JS 25 37 40 41 42 43 44 47 33 CAUSE CESCRIPTION AND CCARECTIVE ACTICNS h I i ! o I L cresstie valve to unit 1. FCV l-74-100. was teased closed, eliminating D-1 and D-2 l
t1 it i l ouweg.,umes frem service.
C'.1 was c'1anned in the 32 eumo motor and the cumo I
ii i 2t I returned to service within one dav.
This is considered a randem event and no
[
l litil I recurrence centrol is recuired.
I la t il l i
a 3 80 STA S
%80WER CTWER STATUS 15 C P OGCONRY CESCRiPTION NA l
l A !hl Admin observaCion l
ji15lI elh Inlofo!hl Adrivirv.:$ r E N' T
Auct NT Cr ACTivery h l LcCAriCN or aELEASE li 16 l [,,J.j @ 'aELEAsEd@[.
aELEAsen c5 A
l NA I
mnm,'a...~s,.:
ma,,..,nN @
.m,,,
- , ! i j } 010 ! 0 @l 7. l@l NA
[
es <>cNNeU,N;u2.Es Ny ve t.4 O E SC FC P fiON Ii i l I d Ol.Sjhl NA I
4 i-u ao LCss Os CR O AM AGE 70 S AC3L tv T495 O ESCRIP TION l i j 'l I dhl NA l
su so cEsCRaTicN @ 8107310394 810722 N AC USE CND 1eiojlNfhl
,.:U E PDR ADOCK 05000260 l
l!Iillll ll ltl1 S
PDR
,a 3 i
to (205) 729-6134 o
Gene Rolder PHONE:
NAME OF DPE 8ARE A
T M
Tennessec Valley Authority Form BF 17 g
P.rowns Ferry Nuclear-Plant BF 15.2 6/04/81 1.F.1: SUPPL.F. MENTAL. IN FORM ATIOn' hFRO 260 /
S1034 Trehnical Specification in co!ved 3.5.C.3.
Iceported Under Technica! Spe cifictition,,6.7.2.bM)
7/30/_81 i) ate of Occurrence 6/30/81 Time of Occurrence 0600 Unit 2
1(lentifica_ tion and,Im u'ipt:on of Occurrence. The RHRSW pump B2 was' removed from service to change the oil in the motor. This left only or.e pump aligned i
to unit 2 and to unit 3 for standby coolant. Unit. 2 was reduced to one p'urtp i
because the crosstie valve to unit 1,FCV 74-100, was tagged closed eliminating D-1 and D-2 RHREW pumps from service.
t Uvnditions Pricr to occurrence:
Unit 1 in refueling outage.
Unit 2 at 99%
! ! ) '!
.)
1 l
Unit 3 at 92%
i
)
Action specified in the Technical Specification SurveiUance Requirements met 1
qtte to inoperable equigmcnt.
Describe.
i Met surveillance requirements of T.S. 4.5.C.4.
i Apparent Cause of 0"currence:
Crosstie valve to unit 1, FCV 74-100 was tagged closed, eliminating D-1 and D-2 RHRSW pumps from service, while RHF.SV pump was removed from servic to change the oil in the motor.
l l
A t uiy:,ir. of, ( lec u rrem e-I There was no danger to the health or safety of the public, no release of i
activity, no damage to the plant or. equipment, and no resulting significant chain of events, i
i i
Cu.r.rechve Action :
Changed ti oil in the motor and returned the pump to service within one day.
This is et
.dered a random event and no further recurrence control is required.
i I9'ilup. Djyp,:
None j
Heren tign :
Per~ >d - I.ifetime; Responsibility - Document Control Supervisor
.?
,p
-~
,-coww q m
--wy-m w,=.-.c,..,.-,ewpm-.,y--y-.w-wr,&m-,
--.my y,-.-2.-w,r,,,,,me,_w.
- - wpr.,-,.,,w,+
e.v.,e-=
c-,-
---*--e-e-
-,me--,.,
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000260/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000260/LER-1981-001-01, /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | | | 05000259/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001-03, /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | | | 05000259/LER-1981-001-03, /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | | | 05000260/LER-1981-002-03, /03L-0:on 810102,scram Discharge Instrument Vol Rod Block Level Switch 2-LS-85-45E Found Set at 27 Gallons. Alarm Switch 2-LS-85-45F Found Inoperable.Caused by Drift of Robertshaw Model SL-305-EI-X.Switch Recalibr | /03L-0:on 810102,scram Discharge Instrument Vol Rod Block Level Switch 2-LS-85-45E Found Set at 27 Gallons. Alarm Switch 2-LS-85-45F Found Inoperable.Caused by Drift of Robertshaw Model SL-305-EI-X.Switch Recalibr | | | 05000296/LER-1981-002-03, /03L-0:on 810104,excess Flow Check Valves in B3 & B7 Instrument Lines to Panel 25-7 Would Not Restrict Flow Properly.Cause Not Stated.Internals Changed & SI 4.7.D.1.d Successfully Completed | /03L-0:on 810104,excess Flow Check Valves in B3 & B7 Instrument Lines to Panel 25-7 Would Not Restrict Flow Properly.Cause Not Stated.Internals Changed & SI 4.7.D.1.d Successfully Completed | | | 05000259/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000259/LER-1981-002-03, /03L-0:on 810114,smoke Detector in Relay Room Alarmed & Would Not Clear.Caused by Detector Sensitivity Increasing Due to Normal,Natural Aging.Detector Replaced & Tested | /03L-0:on 810114,smoke Detector in Relay Room Alarmed & Would Not Clear.Caused by Detector Sensitivity Increasing Due to Normal,Natural Aging.Detector Replaced & Tested | | | 05000296/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000260/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000260/LER-1981-003-03, /03L-0:on 810112,core Spray Pump Discharge Pressure Switch 2-PS-75-16 Found Outside Tech Spec Limits. Caused by Setpoint Drift.Switch Recalibr & Replaced | /03L-0:on 810112,core Spray Pump Discharge Pressure Switch 2-PS-75-16 Found Outside Tech Spec Limits. Caused by Setpoint Drift.Switch Recalibr & Replaced | | | 05000259/LER-1981-003-01, /01T-0:on 810124,Div of Engineering Notified That 1-inch Vent Line on Unit 1 Scram Discharge Vol Not Seismically Qualified.Caused by Piping Configuration Not Conforming to Design Requirements | /01T-0:on 810124,Div of Engineering Notified That 1-inch Vent Line on Unit 1 Scram Discharge Vol Not Seismically Qualified.Caused by Piping Configuration Not Conforming to Design Requirements | | | 05000259/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000260/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000296/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000296/LER-1981-003-03, /03L-0:on 810107,during Refueling Outage,Fuel Pool Cooling Sys Auto Isolated When Power Was Removed.Fuel Pool Sampling Not Performed on 8-h Schedule.Caused by Personnel Error.Personnel Reinstructed | /03L-0:on 810107,during Refueling Outage,Fuel Pool Cooling Sys Auto Isolated When Power Was Removed.Fuel Pool Sampling Not Performed on 8-h Schedule.Caused by Personnel Error.Personnel Reinstructed | | | 05000260/LER-1981-004-01, /01T-0:on 810119,reactor Water Level Switches LIS-3-203A Switch 1 & LIS-3-A,B,C,D Switch 2 Found Outside Tech Specs.Caused by Drift Due to Air Impact Drilling Next to Switch Panel.Switches Recalibr | /01T-0:on 810119,reactor Water Level Switches LIS-3-203A Switch 1 & LIS-3-A,B,C,D Switch 2 Found Outside Tech Specs.Caused by Drift Due to Air Impact Drilling Next to Switch Panel.Switches Recalibr | | | 05000296/LER-1981-004-03, Diesel Generator 3A & Breaker 1836 Tripped from Generator Overspeed During Testing.Caused by Vs Relay on Speed Sensing Panel Energizing at Less than 870 Rpm,Closing Breaker 1836 | Diesel Generator 3A & Breaker 1836 Tripped from Generator Overspeed During Testing.Caused by Vs Relay on Speed Sensing Panel Energizing at Less than 870 Rpm,Closing Breaker 1836 | | | 05000296/LER-1981-004, Forwards Updated LER 81-004/03X-1 | Forwards Updated LER 81-004/03X-1 | | | 05000259/LER-1981-004, Forwards Updated LER 81-004/03L-1 | Forwards Updated LER 81-004/03L-1 | | | 05000259/LER-1981-004-03, Standby Gas Treatment Sys Train C Relative Humidity Heaters Declared Inoperable.Caused by Dwyer Photohelic Pressure Switch/Gage Circuit Hh & Ite Imperial Relay Contact Block Malfunction | Standby Gas Treatment Sys Train C Relative Humidity Heaters Declared Inoperable.Caused by Dwyer Photohelic Pressure Switch/Gage Circuit Hh & Ite Imperial Relay Contact Block Malfunction | | | 05000260/LER-1981-005-03, /03L-0:on 810119,core Max Fraction of Limiting Power Density Exceeded Limit for One Node in Core.Caused by Operation Close to Limit in Conjunction W/Minor (Normal) Perturbation in Monitored Parameters.Power Reduced Slightly | /03L-0:on 810119,core Max Fraction of Limiting Power Density Exceeded Limit for One Node in Core.Caused by Operation Close to Limit in Conjunction W/Minor (Normal) Perturbation in Monitored Parameters.Power Reduced Slightly | | | 05000259/LER-1981-005-04, /04T-0:on 810131,hydrogen Ion Concentration of Reservoir Near Plant Found in Excess of Allowable Discharge Limit.Probably Caused by Upstream Source.Discharge of Spent Regenerants Stopped & Monitoring Program Established | /04T-0:on 810131,hydrogen Ion Concentration of Reservoir Near Plant Found in Excess of Allowable Discharge Limit.Probably Caused by Upstream Source.Discharge of Spent Regenerants Stopped & Monitoring Program Established | | | 05000296/LER-1981-005-03, /03L-0:on 810127,containment Atmosphere Hydrogen analyzer,3-H2M-76-94,removed from Svc.Caused by Maint on Sensing Line at 3-FIC-76-94,Model 1350,due to Water Collection.Water Removed & Lines Returned to Svc | /03L-0:on 810127,containment Atmosphere Hydrogen analyzer,3-H2M-76-94,removed from Svc.Caused by Maint on Sensing Line at 3-FIC-76-94,Model 1350,due to Water Collection.Water Removed & Lines Returned to Svc | | | 05000296/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000260/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000259/LER-1981-005, Forwards LER 81-005/04T-0 | Forwards LER 81-005/04T-0 | | | 05000259/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000259/LER-1981-006-03, /03L-0:on 810211,while Performing SI 4.2.B-57,RHR Area Cooling Fan Temp Switch 1-TS-64-68 Failed to Operate. Caused by Switch T675A1540 Failure.Switch Replaced,Calibr & 4.2.B-57 Completed | /03L-0:on 810211,while Performing SI 4.2.B-57,RHR Area Cooling Fan Temp Switch 1-TS-64-68 Failed to Operate. Caused by Switch T675A1540 Failure.Switch Replaced,Calibr & 4.2.B-57 Completed | | | 05000296/LER-1981-006-03, /03L-0:on 810128,containment Atmosphere Hydrogen Analyzer Removed from Svc.Caused by Maint on Sensing Lines Due to Effect of Water Accumulation on Model 76-01A625 Timer.Water Removed & Monitor Returned to Svc | /03L-0:on 810128,containment Atmosphere Hydrogen Analyzer Removed from Svc.Caused by Maint on Sensing Lines Due to Effect of Water Accumulation on Model 76-01A625 Timer.Water Removed & Monitor Returned to Svc | | | 05000296/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000260/LER-1981-006-03, /03L-0:on 810121,core Max Fraction of Limiting Power Density Exceeded Limit.Caused by Power Increase in Conjunction W/Inoperable Process Computer.Power Reduced & Control Rod Pattern Adjustment Made on 810123 | /03L-0:on 810121,core Max Fraction of Limiting Power Density Exceeded Limit.Caused by Power Increase in Conjunction W/Inoperable Process Computer.Power Reduced & Control Rod Pattern Adjustment Made on 810123 | | | 05000260/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000260/LER-1981-007-03, /03L-0:on 810129,during Power Increases,Tech Spec Limit of 13.33 Kw/Ft for Linear Heat Generation Rate Exceeded in One Node.Node Reached 13.77 Kw/Ft.Caused by Xenon Transient Resulting from Increased Core Power | /03L-0:on 810129,during Power Increases,Tech Spec Limit of 13.33 Kw/Ft for Linear Heat Generation Rate Exceeded in One Node.Node Reached 13.77 Kw/Ft.Caused by Xenon Transient Resulting from Increased Core Power | | | 05000260/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000259/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000259/LER-1981-007-03, /03L-0:on 810210,during Fire Door Insp,Fire Door Damper (Door 472) Not Closed.Caused by Paint Buildup in Operating Mechanism.Damper Closed & Other Dampers Inspected. Procedure for Insp & Preventive Maint Will Be Written | /03L-0:on 810210,during Fire Door Insp,Fire Door Damper (Door 472) Not Closed.Caused by Paint Buildup in Operating Mechanism.Damper Closed & Other Dampers Inspected. Procedure for Insp & Preventive Maint Will Be Written | | | 05000296/LER-1981-007-03, /03L-0:on 810202,setpoint for 3-PS-1-76 Below Tech Specs Limit.Caused by B2TA12SS Setpoint Drift.Switch Recalibr & Verified.Switch to Be Replaced W/Analog Trip Sys by DCR 1398 | /03L-0:on 810202,setpoint for 3-PS-1-76 Below Tech Specs Limit.Caused by B2TA12SS Setpoint Drift.Switch Recalibr & Verified.Switch to Be Replaced W/Analog Trip Sys by DCR 1398 | | | 05000296/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000260/LER-1981-008-03, /03L-0:on 810220,reactor Core Isolation Cooler Turbine Trip & Throttle Valve Closed & Would Not Reopen. Caused by Overload Heater Relay.Relay Replaced | /03L-0:on 810220,reactor Core Isolation Cooler Turbine Trip & Throttle Valve Closed & Would Not Reopen. Caused by Overload Heater Relay.Relay Replaced | | | 05000259/LER-1981-008-01, /01T-0:on 810226,secondary Containment Integrity Lost When Exterior Equipment Access Door 229 & Interior Personnel Door 228 Opened Simultaneously.Caused by Lack of Interlocks Between Doors.Interlocks to Be Installed | /01T-0:on 810226,secondary Containment Integrity Lost When Exterior Equipment Access Door 229 & Interior Personnel Door 228 Opened Simultaneously.Caused by Lack of Interlocks Between Doors.Interlocks to Be Installed | | | 05000296/LER-1981-008-03, /03L-0:on 810202,RHR Pump Found Inoperable.Caused by Loose Pump 3D Breaker Trip Adjustment Nut & Adjustment Change,Causing Breaker to Trip Free on Attempting to Close. Breaker Replaced.Adjustment Locknut Tightness Checks Add | /03L-0:on 810202,RHR Pump Found Inoperable.Caused by Loose Pump 3D Breaker Trip Adjustment Nut & Adjustment Change,Causing Breaker to Trip Free on Attempting to Close. Breaker Replaced.Adjustment Locknut Tightness Checks Added | | | 05000296/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000259/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | | | 05000260/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000296/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000259/LER-1981-009, Forwards LER 81-009/01T-0 | Forwards LER 81-009/01T-0 | | | 05000260/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | |
|