05000260/LER-1981-030-03, /03L-0:on 810629,while Performing Surveillance Insp 4.5.B.1.D,valve 2-FCV-2-74-57 Became Inoperable,Making RHR Loop I Inoperable.Caused by Geared Limit Finger Base Breaking Off of Operator.Finger Base Replaced

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/03L-0:on 810629,while Performing Surveillance Insp 4.5.B.1.D,valve 2-FCV-2-74-57 Became Inoperable,Making RHR Loop I Inoperable.Caused by Geared Limit Finger Base Breaking Off of Operator.Finger Base Replaced
ML20009E526
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 07/21/1981
From: Holder G
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009E515 List:
References
LER-81-030-03L, LER-81-30-3L, NUDOCS 8107280280
Download: ML20009E526 (2)


LER-1981-030, /03L-0:on 810629,while Performing Surveillance Insp 4.5.B.1.D,valve 2-FCV-2-74-57 Became Inoperable,Making RHR Loop I Inoperable.Caused by Geared Limit Finger Base Breaking Off of Operator.Finger Base Replaced
Event date:
Report date:
2601981030R03 - NRC Website

text

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U. S. NUCLE AR REGULATU.Y COMMISSION NHCroRM M LICENSEE EVENT REPORT CON T HOL BLOCK: l l

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8 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h

,.,,; During normal operation, while performing SI 4.5.B.1.d, valve 2-FCV-2-74-57, became I (containment cooling mode) inoperable. See T.S.

g g,,7, inoperable, making RHR loop Redundant g

There was no danger to the health or safety of the public.

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43 44 47 CAUSE DESCHIPTION AND CORRECTIVE ACTIONS switch finger base broke off of the operator, making valve inoperable.

I I i j u l l Ceared limit I

l Replaced the finger base of the limitorque type SMB, size 2 valve motor operator.

liltj I i i ii 1 An investigation of the vibration problem with this valve is being conducted.

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Gene Holder PHONE.

NAMF UF PHEPAHLH

Tenne::see Valley Authority Form BF 17

- bi.. win. l'erry Nnclea I'lant f)F 15.2 G/01/81
1. I '. ! :;til l'l.I'. MENTAL. I N Fi slim A i If ie; 81030 Tr. hnical Specific.ition involved 3.5.B.7 B F i t t i.. r,0- 260,, f lieported lindur Technical S reification 6.7 2.b(2)
  • Date <tue NRC: 7/29/81 I

Date of Occurrence 6/29/81 Time of Occurrence 2030 Unit 2

hientification anij ljuseription of occurrence:

While performing SI 4.5.B.1.d., valve 2-FCV-2-74-57, became inoperable, making RilR loop I inoperable.

t'.o u itiori:. I'ri..: to ()cciarceni e Unit 1 in' refueling' outage.

Unit 2 at 99%.

11 nit 3 at 95%

Act io:: q,cufb I in-the Technical Specification Surveillance Requirements met

..ir to it]operabit e iutpraent.

Desc ribe.

Met requirements of T.S. 4.5.B.7.

Appat ent (.*aut.c of f )ccurrence Geared limit switch " red" switch finger base broke off of the operator, making the. valve inoperable.

Analywis <>f_ Qcrparrence.

There was no danger to the health or safety of the p.alic, no release of activity, no damage to the plant or equipment, and no resulting significant chain of y

4 events.

t 'urr: etice Action :

Replaced the " red" finger base of the limitorque type SMB size 2 valve on the motor operator. The vibration problem with this valve is being investigated.

Failure Dat.a:

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