05000318/LER-1981-033-03, /03L-0:on 810704,pressurizer Level Deviated Excessively from Program Level While Paralleling Main Turbine Generator.Caused by RCS Temp Swing,Not Uncommon During Paralleling Process

From kanterella
(Redirected from ML20009D759)
Jump to navigation Jump to search
/03L-0:on 810704,pressurizer Level Deviated Excessively from Program Level While Paralleling Main Turbine Generator.Caused by RCS Temp Swing,Not Uncommon During Paralleling Process
ML20009D759
Person / Time
Site: Calvert Cliffs 
Issue date: 07/15/1981
From: Junge M
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20009D754 List:
References
LER-81-033-03L, LER-81-33-3L, NUDOCS 8107240325
Download: ML20009D759 (1)


LER-1981-033, /03L-0:on 810704,pressurizer Level Deviated Excessively from Program Level While Paralleling Main Turbine Generator.Caused by RCS Temp Swing,Not Uncommon During Paralleling Process
Event date:
Report date:
3181981033R03 - NRC Website

text

---

NRC FORM 366.

U. S. NUCLFAR REGULATORY COMMISSION (771)* 0 LICENSEE EVENT REPORT CONTROL BLOCK: l l

l l

l l

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) lM l D l C l C l N j 2 l@l 0 l0 l-l0 l0 l0 l0 l0 l -l 0l Ol@M l1 11 l1 l@l l

j@

o i j.

8 9 LICENSdE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO b7 CATb8 CON'T.

101il

$$R$ l L l@l 0 l 5 l010101311 18 l@l01710141811 l@l01711 l51811 l@

7 8

60 61 DOCKET F4UMF ER 68 69 EVENT DATE 14 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o I 21.1 At 1420 while parallelino the main turbine cenerator. oressurizer level I

lo ial I deviated from the procram le' el by more than +/- 5% for 30 minutes I

! o 14 I I (T.S. 3.4.4).

LER f0-317/81-40 describes a similar event, I

lo isi i l

10 is l I I

10171 1 I

l 0 l8 l l l

80 7

8 9 t

C DE ODE SUB E

UMPONENT CODE S BC DE SU ODE l_C I B l@ lx J@ I z l@ L~ t 21 z l z l z i z l8 Lz_j@ ULj @

O 9

- 7 8

9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LE R-RO EVENT YEAR REPORT NO.

CODE TYPE NO.

O aj,g I 81 11 l-l l 0l 3l 31 l/l l0131 lL i l-l [0_j s

21 22 23 24 26 27 28 29 30 31 32 KN AC 0 ON PL NT 1E OD HOURS b

tT D FO 1 8.

SU PLIE MAN F CTURER lZl@ll]@

l Z i@

l Zl@

l 01010l 01 l NI@

[_N.j@

l Zl@

l Zl 9 l 9191@

3J 34 3b 36 3/

40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h clilOi l RCS. mperature swings of 10 i.eas are not uncocinon when paralleling j

i i l

the main generator. These temperst.re svings can result in deviations 1

, 2 l

grr.ater tisan +/- 5% from pressurizer program level. No corrective i

gl action was deemed necessary.

I i 4 I

I 80 7

8 9 ST S

% POWER OTHER STATUS IS O RY DISCOVERY DESCRIPTION

[_C_J @ l0 12 10 l @ l NA l

[ A.j@l Operator Observation l

i s ACTIVITY CON TENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOC ATION OF RELE ASE Itlcl W @ W @l NA l

l NA l

7 8 9 10 11

  • ERSONNEL EXPOSURES i

NUM8ER TYPE DESCRIPTION 39 l i ! 7 l l 0 i 010 l@[J..j@l NA l

+

PERSONNE L INJUR:ES NUVBER DESCRIPTI%

FFIR 1 I o I o I o l@l NA l

- 7 8 9 11
2 80 L OSS OF OR DAM G TO FACILITY l

[1_l2][_j@l NA 80 Z

8107240325 810715 7

s e to e

iSSUEf@OESCRIP TION [g,

l NA I

IIIIIIIIIIIll5 2 o 68 69

80. g 7

8 9 10

~

NAME OF PREPARER PHONE: