05000331/LER-1981-024-03, /03L-0:on 810616,drywell Equipment Drain Line Valve CV-3729 Did Not Give Fully Closed Indication During Testing.Caused by Seat Leakage in Solenoid Valve SV-3729. Solenoid Valve Replaced

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/03L-0:on 810616,drywell Equipment Drain Line Valve CV-3729 Did Not Give Fully Closed Indication During Testing.Caused by Seat Leakage in Solenoid Valve SV-3729. Solenoid Valve Replaced
ML20009D545
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 07/15/1981
From: Schmich A
IES UTILITIES INC., (FORMERLY IOWA ELECTRIC LIGHT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20009D538 List:
References
LER-81-024-03L, LER-81-24-3L, NUDOCS 8107240156
Download: ML20009D545 (1)


LER-1981-024, /03L-0:on 810616,drywell Equipment Drain Line Valve CV-3729 Did Not Give Fully Closed Indication During Testing.Caused by Seat Leakage in Solenoid Valve SV-3729. Solenoid Valve Replaced
Event date:
Report date:
3311981024R03 - NRC Website

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to isi i Isolation) valve CV-3729 did not give a fully closed indication. Tech.

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1 tii2, I akage through SV-3729 to the CV-3729 piston drive. The solenoid valve wa I

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