05000331/LER-1981-023-03, /03L-0:on 810611,during Surveillance Testing, Reactor Core Isolation Cooling Steam Line High Flow Pressure Differential Switch Pdis 2442,tripped at 100 Inches of Water.Caused by Instrument Drift.Switch Recalibr

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/03L-0:on 810611,during Surveillance Testing, Reactor Core Isolation Cooling Steam Line High Flow Pressure Differential Switch Pdis 2442,tripped at 100 Inches of Water.Caused by Instrument Drift.Switch Recalibr
ML20009C014
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 07/09/1981
From: Schmich A
IES UTILITIES INC., (FORMERLY IOWA ELECTRIC LIGHT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20009C012 List:
References
LER-81-023-03L, LER-81-23-3L, NUDOCS 8107200169
Download: ML20009C014 (1)


LER-1981-023, /03L-0:on 810611,during Surveillance Testing, Reactor Core Isolation Cooling Steam Line High Flow Pressure Differential Switch Pdis 2442,tripped at 100 Inches of Water.Caused by Instrument Drift.Switch Recalibr
Event date:
Report date:
3311981023R03 - NRC Website

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