ML20008F890
| ML20008F890 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 05/07/1981 |
| From: | Zufelt E POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | |
| Shared Package | |
| ML20008F889 | List: |
| References | |
| NUDOCS 8105120266 | |
| Download: ML20008F890 (7) | |
Text
1 OPERATING DATA REPORT DOCKET NO.
50-333 DATE Mav. 1981 COhlPLETED BY E.~ Z u f'elt TELEPilONE (7151 342-3840 OPERATING STATUS FitzPatrick Notes
- 1. Unit Name:
- 2. Reporting Period:
&l0401 - 810410 2436
- 3. Licenwd Thennal Power (S!Wt):
883
- 4. Nameplate Rating (Gross htWe):
821
- 5. Doign E!cetrical Rating (het 5fWe):
830
- 6. 5!asimum Dependable Capacity (Gross SIWE):
810
- 7. hf aximum Dependable Cspacity (Net 51Wei:
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, G;se Rea..sns:
NONE
- 9. Power Level To Which Restricted. lf Any (Net blWe):
NONE
- 10. Reasons For Restrictior *.lf Any:.
This 51onth Yr..t o-Date Cumulatise 719 2879 50496
- 11. Ilours in Reporting Period
- 12. Number Of ilours Reactor Was Critical 562.4 2521.2 19475.2
- 13. Reactor Resene Shutdown flours 0
0 0
- 14. Ilours Generator On-Line 541.6 2474.3,
94377.1
- 15. Unit Rearve Shutdown flours 0
0 0
- 16. Gross Thermal En-rgy Gener.ted (h!Wil) 1242936 5788368 69971962 17 Gross Electrical Energy Generated (5twil) 4 3'> 4 8 0 2022110 21852820
- 18. Net Electrical Energy Generated (htWil) 419240 1960190 21085270 75.3%
85.9%
68.1%
- 19. Unii Senice Factor 75.3%
85_95_
68E
- 20. Unit Asailability Factor
- 21. Umt Capacity Iactor (Using blDC Net) 72.0%
84.1%
61.6%
71.0%
82.9%
5 5. 7.%
22 Unit Capacity Factor (Using DER Net) 24.7%
14.1%
17,g5 23 Unit Forced Outage Rate
- 24. Shutdowns Scheduled Oser Nesi e %1onths (T)pe. Date.and Duration of Each L Re fueling and maintenance outage scheduled for_0ctober 1981.for_
a period of 110 days.
- 25. If Shut Down At End Of Report Pmod. Estimated Date of Startup:
- 26. Units In Test Status (Prior to Commercial Operation):
Forecast Achiesed INillAI. CRITICA Li FY INITIA L ELECTRICITY COhlNIERCI AL OPER ATION 8'1051206,W
f)
AVER AGE DAILY UNIT POWER LEVEL DOCKET NO.
50-333
~
c..
JAFNPP UNIT May, 1981 DATE E. Zurelt COMPl.ETEP BY TELEPlf0NE.l.311)_31L2-38 40 APRIL'1981 MONTil DAY AVER AGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MYle Net)
(MWe Net) 483 37 81ft 2
3 18 819__.
3 0
39 817 4
20 817 0
y 5
28 817 0
0 22 817
~
6 7
0 23 819 0
816 8
24 186 9
25 017 665 26 701 10 663 27 817 786 818 28 12 019 816 29 13 818 818 i4 3o 820 3:
is 818 16
SUMMARY
On AprL1 2, 1981, the FitzPatrick Unit was manually scrammed due to a seal failure in the "A" recirc pump.
The seal was replaced and the unit was back on line April 9, 1981.
50-333 DOCKET NO.
UNIT SHUTDOWNS AND POWER REDUCTIONS IJNIT N AM E JAFNPP
- DATT, May, 1981 COMPLETED BY E.
Z u t'e l t -
REPORT MONTH Anril. 1981 TELEPilONE J 415 ) 342-3480 w
e c
j.E E Licensee Cause & Corrective I'
$g r
N...
Date g
3g i
2ss Event p
gg Action to fE jgj Report a m ts Prevent Recurrence H
g 6
4 810402 F
177.4 A
2 81-029 CB PumpXX Seal failure on recire pump 02-2 PlA.
Replaced seal.
a 4
+
v 1
2 3
4 F: Forced Reason:
Method:
Exhibit G Instructions S. Scheduled A Equipment Failurc(Explain) 1 Manual for Preparation of Data B Maintenance oiTut
'2 Manual Scram.
Entry Sheets for Licensee C Refueling 3 Automatic Scram.
Event Report (LER) File (NUREG.
D Regutatury Resiriction 4-Other (Exrlain) 0161)
E Operator Training & License Examination 5
F.Ad minist rairve 4
G Operational Etrur (Explain)
Exhibit i. Same Source ll Other (F xplain)
t POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT
' NARRATIVE
SUMMARY
OP.0PERATING EXPERIENCES APRIL 1981-e On April 1,.1981, the FitzPatrick: Plant initiated.t:
normal shutdown following failure'of reactor-water recirc--
ulation pump A seal.
Reactor shutdown was completed on-
- ~ '
April 2, 1981 by initiating a manual scram at approximately
- 11 percent power when the Rod' Sequence Control System would not allow additional manual control rod insertion in order.
to complete-the normal shutdown.- The seal was replaced and the unit was returned to service at 1100 on April 9,'1981.
Power was increased at.the pre-conditioning rateEand the unit operated at near full rated thermal powsr for the j
remainder of this reporting. period.
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POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT i
SAFETY RELATED ELECTRICAL 8 MECHANICAL MAINTENANCE
SUMMARY
l
]
O S OATE SYSTEM HOW DITECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIME E
HOURS 4/6/8]
23 9065 Operations Stepped On Replaced pipe nipples & fittings 3
23-TU-2 4/6/8J 23 11061 Opc. rations wear /Use Repacked 8
MOV-60 4/6/8]
23 11835_
operations steam cut gasket Cleaned bonnet flange AOV-53 Replaced gasket 8
4 4/6/8]
03 5h02 Visual Careless welding arc Replaced nitrogen flask 12 HCU-22-11 strike.
4/6/82 23 9748 operations Wear /Use Repacked 11 MOV-16 4/6/82 02-2 11426 9091 Operations Wear /Use Replaced seal 496 i
P-1A i
4/10/t 1 13 8610 operations Turbiac would not cleaned trip linkage - could not TUL2 manually trip locate any problem.
Tested satisfactory.
16 4/6/81 02-2 9141 Operations Cracked FN housing Replaced housing cover 10 4
MOV-43A cover 4/8/8]
10 9112 Operations Motor windin6s burnt Replaced damaged contacts at MOV-18 up.
Caused acarter starter & performed EP-201 or contacts to fuse.
starter.
6 T
4/8/81 10 1463 Opernions Motor for MOV failed.
Replace motor with spart from MOV-16 warehouse.
30 h
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT MAINTENANCE
SUMMARY
APRIL 1981 I&C E
ES DATE SYSTEM HOW DETECTED CO PO E T LF U C ON MAL CI T
EC R HUS 3/30/81 02 52'9 I&C USE Connection has Replaced valve PS-134B bad threads 1.0 4
4/6/81 02-3 9134 OPS Defective Pen sticks Replaced drive LR-98 drive motor motor 8.0 3/31/S1 03 8907 OPS USS/A0E Will not select Replaced switer 12.0 Select button 26 '11 4/7/81 03 8916 0FS Unknown Will not allow Tested - Found RSCS rod movement satisfactory 32.0 4/3/81 07 12347 I&C Defective H.V.
Erratic Replaced /
SRM "C" power supply voltages repaired H.V.P. S. 32.0 4/6/81 07-7467 OPS Damaged during Downscale Replaced IRM "A" CRD changeout detector T ?A D 7 13 lub n 4/7/81 07 11433 OPS Bad detector Downscale Replaced IRM "D" Detector 100.0 IMP 7.17 4/8/81 07 8612 OPS N/A Check settings Adjusted 1.0' APRM "F" 4/9/81 07 8920 I&C N/A Repair spare Repaired &
SRM Spares power supplies tested 22.0 4/22/81 07 9408 I&C Unknown Erroneous Cleaned /
PR-46D signals lubricated 30 4/22/01 07 9405 I&C Pen sticks Black pen Repaired /
PR-46B sticks cleaned 9.0' l
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT i
MAINTENANCE
SUMMARY
APRIL 1981 I&C I
WORK REQUEST #
CAUSE OF RESULTS OF ACTION TAKEN REPAIR j
DATE SfSTEM COMPONENT #
MALFUNCTION MALFUNCTION TO PRECLUDE TIME RECURRENCE HOURS i 3/30/81 13 9067 OPS Use/ Wear Incorrect Cleaned /
FS-57 indication Tightened 22.0
! 3/27/81 17 9755 I&C Bad transistor In orrect Repaired low a
RIS-456A inuication voltage Power 16.0 mmM 4 ae
! 3/30/81 17 9025 RES N/A Erratic Flow Found OK 30 I
RM-431 Indication i 3/30/81 17 9026 RES Unknown Broken light' Replaced bulb
- 2. 0, l
RM-461 l
) 4/18/81 17 9516 OPS Unknown Erratic Tightened fuse RE-230B operation F-2 2.0 4/28/81 17 8392 I&C Use N/A Repaired spare 3
Various CKT boards 52.0 1 4/7/81 66 9736 OPS Drift Does not main-Aligned j
DPC-112 tain setpoint controller 22.0 l
4/6/81 71 8910 OPS Bad annun. card Spuricus alarm 3 Replaced card 3.0 3KR-10612
} 4/10/81 71 12345 I&C Bad annun. card Spurious alarm ; Replaced card 25.0 09-8 Annun i
I
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