ML20008F732

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Monthly Operating Rept for Mar 1981
ML20008F732
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 04/10/1981
From: Elam G
GEORGIA POWER CO.
To:
Shared Package
ML20008F731 List:
References
NUDOCS 8104210556
Download: ML20008F732 (6)


Text

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M-3M UNIT SildTDC'.'it'S A ND 701/ER REDUCTIONS DOCKET NO[

UNIT N AM liatch 1 l

DATE 4-10-8!

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Event Report (LER) File (NUREG-C. Refueling D.Regolatory Restriction 4 -Continuations 0161) 5-Icad Ibduction E-Operator Training & License Examination...

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s HATCH 1 SAFETY-RELATED MAINTENANCE REQUESTS TO BE REPORTED FOR MARCH 1981 NUMBER DATE COMPLETED DESCRIPTION 50-6174 3-5-61 Replaced amplifier units 3

and 4 in power supply 1C32-K613 and 1C32-K612 of.the feedwater controller 1C32-K638 79-5562 1-30-81 Installed LPCI' MCL normal power supply conduit supports 1R24-S018A6B per DCR 79-201 80-562 2-18-18 Visually inspected work performed in fabrication of restraints (per DCR 77-160) stored at warehouse #3 of the 1E11-C001A-D RHR service water pumps 81-1112 2-19-81 Loosened turn buckles, reset anchors, torqued all bolts to 150 ft.

Ib.

and tightened turn buckle to original posi-tion of HPC1 1E41-HPSEH-6 81-553 2-13-81 Modified RCIC pipe support of RCIC sys.

4" pipe support E51-PCSEH-15 81-621 2-19-81 Rescal heat exchange on RWCU 1G31-B001 81-78 2-16-81 Removed old security CAB annunciator system H11-P653 81-1369 3-8-81 Field tested hydraulic snub-bers 1C31 79-6939 3-13-81 Removed clamp and strut of turbine bypass hanger A35 and installed it on E2, built new support for A35, modified #36 (per DCR 79-451) turbine bypass hangers 1N11-TBH 29-35-36 81-1045 3-7-81 Repaired service water return line IP41

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1 80-6512 1-2-81 Extended walls and' ceiling to three door openings for Z43 control room Eire doors elev.

164 (per DCR 79-2) and installed C-82 fire door 4

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