ML20005A593

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Interim Deficiency Rept Re Vol Control Tank Level Instrumentation Control Sys,Initially Reported 810521.Plant Procedures Will Be Reviewed to Assure That Operator Will Be Alerted to Take Appropriate Action
ML20005A593
Person / Time
Site: Seabrook  NextEra Energy icon.png
Issue date: 06/18/1981
From: Devincentis J
PUBLIC SERVICE CO. OF NEW HAMPSHIRE
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
10CFR-050.55E, 10CFR-50.55E, SBN-164, SNB-164, NUDOCS 8106300482
Download: ML20005A593 (2)


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Attention: Office of Inspect ion and Enfo rc c,=nt 7.. f e r..n c e s : 1. "ocket ?;o . 50 t 4 3 a n d 50 ',' 4

?. Telecon of ?!ay 21, 1991 het-.en R. r; .21 10 , 'WC .nd .

D. Maidt nd , iAEC 10 CFR 50.55(e) Defici.ncy E. port on Control and P r o t e c t f .:, n S * ;m : tm Inte: ., c t ; o n Vol u.me Con t r ol ~a nk ' e vel Otar Sir:

On May 21, 1981 we reported that 'J. s t i nghou se had identi fied a control and prc.t ec t ion sys t em in te ra c t ion conce rn ir.volvi ng the Volume Control Tank (VCT) le vel ins t rumentation con t rol system. This report is bei ng fil-d in ai cordance with the thi r ty day repor ting requi rement s of 10 CFR 50.55 (e).

The f ollowi ng di scussion describes the system interaction concern. Mseme the plant is opera ting with a cent rif ugal cha rging pump performing the norral cha rgi ng f unct ion. (!;ormally one of the three a vai l a bl e cha rging pumps is ri.e.ing .!th another as standby.) A failure of the VCT level control syst-m c .e e s the letdown flow to be diverted to the li qud hol dup tank. The LCT liquid i nventory dec reaws due to normal cha rging sit hout any .<.. up to the VCT ef a Ie:dcwn. 'Ji t hou t ope ra t o r i nte rvention the VCT could pty <ausing the ep-ra ting cent rif ugal charging ptenp to he :3a. aged due to irss of soction fluid. If it is f urthe r assumed that one c% r;;ing pt:p is out of se rv ice , as alirwed by the Technical Specifications, there wcuid then be only one

r. ,ai ring .ndacated pu p available to prceide M eup to the r. actor coolant s;,4 t ea as r eq ui r ed by l e t d cwn and r oa. : v r .. <.o : an t ps -p t al ' ak ge .

The one r...u;ning ump daes not thcn eet the Cngle 'a!Iure c r i t ,- r i o n .

yolicwing the failure in the VCT level esnt rol systen, the opera t ur -oul d ha ve a;pr nirately ten minutes to transfer the chac3 ing pump suction froc the VCT i

c :' e 6T or to s Mply stop the 7:.np or to r .. s t o r e ie 2 wn to :he u.T ro
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U .S . %c: : r E< gelato ry Cormi ss *cn Fase 2 S E N--164 I f r.o e p. r a t o r .4 c t i o n . e c u r s a t this t i me , t'r.n the p u.rp in opera t ion c oul d be d- 43. d .' ae to loss of 'uction, snd t he pi ent wculd continue to lese i r. vent ory due to etdcwn. "o cver, this is a siev 'ess in wa t e r i nven t o ry. '.u t or.a t i c 1.- : ' r. vn iso'ation sh oul d c.c c u r . "v .:n e i t h ,u t : 9idesn i so a t ion or perator 2 : -- 3: 'm,  ;;pr .3: 21 y t eo .r ruid e .e ;. io r t o cc re .'c - r; . -~, e

-:vr mW, d L.,v e c o ' : ; .'. rai e t :e to 41?gn the 3- ndby ; - :p t o t*e .J ST .

It ' s 'l . s t. i j :se 's pos it ion 'd -e .v u r .4 t ti--21y ep- ator act n c.in

-ga t e t h i s sce:u r io ar.d pos i t ively dd re :s the idcntif'-d concern. Scibrcok is . c i! pr ed wi t h ins t ri.ta n t re:4 hut s ehich -nuld i ndi c at e the pro. ace of this sitestion, in addition, we have numercus alar:s which -ould be ectt ted at various tices in the event.

Plant procedures will be revie-ed to assure that the operator sould be prope rly aler t ed to this s it ua t 'on and would take the appropriate action r.ccescary to assure an adequa t e wa f e r supply to the charging penps in the e ent of a tCT evel cc nt rol svstra failure.

S' uld f urt l.er ct ion be r equi r. d as a .esult of ddit icnal NRC cc nce rns , -e sill cr ypraise e,ur positica and inforc you a . c o r s'i ng l y .

Very truly years,

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L 4,;g ((N's's

[/ / b John DeViacentis Project Manager D O!: see t

F P00R ORIGINAL

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