05000269/LER-1980-040-01, /01T-0:on 801226,removable Instrument Assembly 40 Count Rate Increased,Apparently Due to Leak in once-through Steam Generator Tube.Caused by High Cycle Fatigue.Tube Replaced.Leak Procedure Implemented

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/01T-0:on 801226,removable Instrument Assembly 40 Count Rate Increased,Apparently Due to Leak in once-through Steam Generator Tube.Caused by High Cycle Fatigue.Tube Replaced.Leak Procedure Implemented
ML20005A424
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 03/10/1981
From: Jackie Jones
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20005A421 List:
References
LER-80-040-01T, LER-80-40-1T, NUDOCS 8106300311
Download: ML20005A424 (1)


LER-1980-040, /01T-0:on 801226,removable Instrument Assembly 40 Count Rate Increased,Apparently Due to Leak in once-through Steam Generator Tube.Caused by High Cycle Fatigue.Tube Replaced.Leak Procedure Implemented
Event date:
Report date:
2691980040R01 - NRC Website

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