05000318/LER-1981-009-03, /03L-0:on 810330,during Normal Power Operation, Motor Operated Isolation Valve in Saltwater Sys Would Not Operate Electrically.Caused by Tripped Overload Devices on Phase a & C.Devices Reset

From kanterella
(Redirected from ML20004D639)
Jump to navigation Jump to search
/03L-0:on 810330,during Normal Power Operation, Motor Operated Isolation Valve in Saltwater Sys Would Not Operate Electrically.Caused by Tripped Overload Devices on Phase a & C.Devices Reset
ML20004D639
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 04/30/1981
From: Rizzo P, Wenderlich R
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20004D630 List:
References
LER-81-009-03L, LER-81-9-3L, NUDOCS 8106090604
Download: ML20004D639 (1)


LER-1981-009, /03L-0:on 810330,during Normal Power Operation, Motor Operated Isolation Valve in Saltwater Sys Would Not Operate Electrically.Caused by Tripped Overload Devices on Phase a & C.Devices Reset
Event date:
Report date:
3181981009R03 - NRC Website

text

_.

LICENSEE EVENT REPORT j

A n.. Rol block:

l l

l l

l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFoRMATION)

U 6

- ii l i M i 0 I c l c l N I 2 l@l 01 01 -l 01 01 01 01 01 -1 01 01@l 4l 11 11 il 11@l l

l@

7 8 9 UCENSEE CODE 14 15 UCENSE Nuv8ER 25 26 LICENSE TYPE JO 57 CAT 58 con'T 8

$$,5 l L l@l 0 l 510 l 010 l 311 18 l@l0 l3 13 l018 l1 l@l0 14 13 10 18 11 l@

7 8

60 61 COCKET NUM8ER 68 69 EVENT CATE 74 75 REPORT CATE 80 w

EVENT DESCRIPTloN AND PROBABLE CCNSECUENCES h 10121l During nomal power operation at 1730 a motor coerated isolation valve l

IOl2l l (2-MOV-5251) in the salt water system suoply to the circulating water l

10 a i i aump room air coolers would not ooerate electrically.

Since it would not l

IO isI I have responded properly to a SIAS signal, this is reportable under T.S.

l

!O is I I 3.7.5.1.

The overloads were immediately reset and the valve tested sat-1 IOI7i l is factorily. The redundant in-series MOV was shut during this event.

I i O is i i

Similar events

none.

l

'E'E C0$E St 8C$0E

  • ^'

F SU8C7dE Sul s E CouPONENT COOE 10isl l W l B l@ lX l@ lX l@ l V l Al L l V l O f P l@ l A l@ lZ l @

v 8

9 to 11 12

- 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LE R/RO EVENT YEAR REPORT NO.

CODE TYPE N O.

@,atg l2181 1 l l-l l 01019l l/l [0 l 3 l l LI,

l-l l0l 22 23 24 26 27 3

a 30 31 32 TA N AC O ONP NT MET HOURS 22 5 8 I U

FOR 8.

SUP PLI E MANUFACTURER lX l@lZ l@

l Z l@

l Zl@

l 0l 0l 0) l lNlg lNl@

lAl@

lLi210l0l@

33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTloN AND CORRECTIVE ACTIONS lilCi l Overload device on Phase A and C were trinced.

These were reset and the I

11 lil I valve was stroked several times while monitorino motor current.

The I

ii l 21 I valve stroked satisfactorily; current readinas were nomal. No oroblems I

iii3l l with valve coerati( n were observed.

The motor and breaker are tested I

i i 14 I annually. No further oreventive action is deemed necessary at this time.

I 1

8 9 80

'6POWEA OTHER $TATUS dis O RY DISCOVERY OESCRIPTION W [Ej @ lll 0lCJ@l NA l' lAl@l Ooerator Observation l

A!TiviTv CcTTENT l 6 I l Z l @D 07 RELEASE l_Z_j@i NA l

l NA l

RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE l1 PERSCNNEL EXPOSURES NUP.*8 E R TYPE

DESCRIPTION

l i 171 10 l 0 l 0 l@l Z l@l NA l

PERSONNEt mu'l'iES cESCRiPTiO~@

NuuSER li la l l 01010 l@l NA l

'7 8 9 11 12 90 l

LOSS OF OR CAMAGE TO FACluTY TYFE DESCRIPTICN Il9I[1]@l NA l

7 8 9 to 30 DE CR PTION I lol ISSUE @l e

NA l

ll11lillll lllj 8106 09 0 %R.

8.

10

. Wenderlich/D. r;. Rizzo 269 d776/4786

?

.:A EogppEPARER

, m e.:..