05000271/LER-1981-011-03, /03L-0:on 810507,during Normal Operation of Reactor Water Cleanup Sys,Leak Discovered in 1x34 Inch Socket Weld Reducing Fitting in tube-side Drain Line of Regenerative Heat Exchanger E-15-1A.Cause Being Analyzed

From kanterella
(Redirected from ML20004D068)
Jump to navigation Jump to search
/03L-0:on 810507,during Normal Operation of Reactor Water Cleanup Sys,Leak Discovered in 1x34 Inch Socket Weld Reducing Fitting in tube-side Drain Line of Regenerative Heat Exchanger E-15-1A.Cause Being Analyzed
ML20004D068
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 06/03/1981
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20004D065 List:
References
LER-81-011-03L, LER-81-11-3L, NUDOCS 8106080297
Download: ML20004D068 (1)


LER-1981-011, /03L-0:on 810507,during Normal Operation of Reactor Water Cleanup Sys,Leak Discovered in 1x34 Inch Socket Weld Reducing Fitting in tube-side Drain Line of Regenerative Heat Exchanger E-15-1A.Cause Being Analyzed
Event date:
Report date:
2711981011R03 - NRC Website

text

i

. NRC F5M 366 U. S. NUCLEAR REGULATORY COMMISSION (7 7H LICENSEE EVENT REPORT LER 81-ll/3L

~j CONTROL BLOCK: l l

l l

l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

l0 l 1 l l VI Tl Vl Yl SI 1l@l 0 l 0 l-l 0 l 0 l 0 l 0 l 0 l - l 0 l 0 l@l4 l1 l1 l1l1l@l l

l@

7 8 9 LICENSEE CODE 14 15 LICENSE NUMUER 25 26 LICENSE TYPE JO 57 CATSd CON'T l0ltI

"'[Rc lL @l0 l 5 I O l 0 l 0 l 2 ] 7 l 1 @l 0 l S l O l 7l 8 l 1l@l0 l6 l0 l 3 l 8 l1 l@

sO 7

6 60 61 OOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT O ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lo l2l l During normal operation of the Reactor Water Cleanup System, routine operator sur-1 I o l a i l veillance discovered a small leak in a 1" X 3/4" socket weld reducinn fitting in l

I o 141 l the tube-side drain line of Recenerative Heat Exchancer E-15-1A unstream of valve 1

l o ! s 1 LV12-41A. There were no consequences adverse to the public health and safety as a l

l o is I i result of this event.

Similar previous occurrences were reported to the Commission i I o I 7 I l as LER 79-01. 80-37 and 80-41.

l 1 o 14 ! I l

80 7

8 9 SYSTEM

CAUSE

CAUSE COMP.

VALVE CODE CODE SUSCODE COMPONENT CODE SUSCODE SUSCODE lo19l lC lC l@

h lD lh l Pl Il Pl El Xl Xlh l A lh (Z_] h 7

4 9

to 11 12 13 1s 19 20 SEQUENTI AL OCCURRENCE REPORT REVISION LER RO EVENT YE AR REPORT NO.

CODE TYPE N O.

h,ag; l8lIl l-l 10 11 11 l l/l 10 13 l lL l

[---J W

_ 21 22 23 24 26 27 28 29 30 31 J2 AK N ACT ON ON PLANT VET HOURS S8 IT FOR 4 8.

SUPPLi E R MANUFAC uRER I A l@l Z l@ U@

U@

l0 l0 l0 l0 l [N_j @

lYl@

lAl@

lE l0 l6 l5 l@

33 34 35 36 31 40 41 42 43 44 47 CAUSE CESCRIPTION AND CORRECTIVE ACTIONS h l i i o I ] Previous incidents of cracking in this system are being analyzed by an independent l

lilij l laboratory to determine the failure mode, and the results of this analysis will be l reported to the Commission in an update to the applicable LER's.

Immediate l

i,,2;

[,l3l l corrective action in this case was to replace the degraded fitting with an I

i i 141 l identical spare.

I 80 7

g 9 ST S

% POWER OTHER STATUS 015 O RY DISCOVERY DESCRIPTION NA l

lB I@l Operator Observation l

li15l d h l1l0l0l@l i2 o

44 45 48 80 A!TiviTY CO'0 TENT RELE ASED OF RELE ASE AVOUNT OF ACTIVITY LOCPION OF RELE ASE NA l

l NA I1 I6 l d h W@l F

6 9 10 tt 44 45 80 PERSONNEL. E XPOSUR ES NUMBER TYPE

DESCRIPTION

li 171 I ol of ol@W@l NA l

PERSONN E t iN2u' RIES DESCRiPT'ONh NoveER NA l

li la l l 0l 0l 0l@l 80 7

8 9 11 12 LOS3 OF OR OAVACE TO FACILITY TYPE D E SC RIPTION NA l

l i t a l l Z !@l 80 7

d 9 to PUBUCITY NRC USE CNLY TSSU Eo OESCR'PTION

{2lol W @l Daily Status Phone (5/7, 8 and 11/81)

I lll1!!1!!Ii!l*:

68 69 80 ;

7 9 9 to (802) 257-7711 E,

W. P. Murphy PHONE:

NAME OF PREP ARER 810608a 2 D