ML20003F465

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LER 81-010/03L-0:on 810322,during Power Operation,Field Breaker Failed to Open When B Rrmg Set Shut Down for Maint. Caused by Lack of Lubrication on Binding.Breaker AK-25 Lubricated
ML20003F465
Person / Time
Site: Vermont Yankee Entergy icon.png
Issue date: 04/15/1981
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20003F464 List:
References
LER-81-010-03L, LER-81-10-3L, NUDOCS 8104210310
Download: ML20003F465 (1)


Text

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l o i s i I ooeration, the Recire Pump Trio Instrumentation be operable. There were no signifi-l laesiIcant occurrences ao a result of this event. nor were there any adverse affects to I l o i 7 4 l rublic honith cr enferv. All redundant avstens vere fully co e rable . There have I losii fkann an q u41nr eventa nrevfnusiv rener**d *n *ke c~~4sefon.  !

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,ii7i I seversi times satisfactorily, was declared coerable. The breaker is a General Elec. I ii ,21lModel AK-25. These breakers will be added to the oreventative maintenance orocran. !

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