ML19352B045

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IE Insp Rept 50-312/81-04 on 810101-31.Noncompliance Noted: Piping for Diesel Generator B dc-driven Governor Oil Booster Pump Improperly Routed
ML19352B045
Person / Time
Site: Rancho Seco
Issue date: 02/27/1981
From: Canter H, Obrien J, Zwetzig G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML19352B038 List:
References
50-312-81-04, 50-312-81-4, NUDOCS 8106020601
Download: ML19352B045 (10)


See also: IR 05000312/1981004

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U.S. NUCLEAR REGULATORY COMMISSION

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OFFICE OF INSPECTION AND ENFORCEMENT

REGION V

Report No.

50-312/81-04

Docket No.

50-312

License No.

DPR-54

Safeguards Group

Licensce:

Sacramento Municipal Utility District

P. O. Box 15830

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Sacramento, California 95813

Facility Name:

Rancho Seco Unit 1

Inspection at:

Herald, California (Rancho Seco Site)

Inspection conducted:

January 1-31, 1981

Inspectors:

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H.k.' Caber,

nior Resident Inspector

' Date Signed

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-fen, Onik Ytesident Inspector

Da'te Signed

Date Signed

Approved By:

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G. B. 'wetzih Actin 9 Chief, Reactor Projects Section 2,

Date Sign d

Reactor Operations Projects Branch

Summary:

Inspection between January 1 and 31, 1981 (Repnrt No. 50-312/81-04)

Areas Inspected: Operational safety verification; monthly maintenance observations;

monthly surveillance observations; followup on regional requests; review of plant

operations (SALP inspection activities); licensee event report followup; on a

significant event; preparation for refueling; refueling activities; and independent

inspection effort. The inspection involved 217 inspector-hours by the resident

insp?ctors.

Results: Of the ten areas inspected, no items of noncompliance or deviations were

found in nine areas. One item of noncompliance was found in one area (10 CFR 50.59

Safety Evaluation not perfonned).

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DETAILS

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1.

Persons Contacted

  • R. Rodriguez, Manager, Nuclear Operations

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  • P. Oubre' , Plant Superintendent
  • D. Blachly, Operations Supervisor

N. Brock, Electrical /I&C Maintenance Supervisor

D. Cass, Mechanical Maintenance Supervisor

Q. Coleman, Quality Assurance Engineering Technician

  • R. Colombo, Technical Assistant
  • G. Coward, Maintenance Supervisor
  • D. Elliott, Quality Assurance Engineer

D. Gardiner, Senior Chemical & Radiation Assistant

  • H. Heckert, Engineering Technician

J. Jewett, Quality Assurance Engineer

F. Kellie, Plant Chemist

V. Lewis, Site Project Engineer

  • R. Miller, Chemistry / Radiological Supervisor
  • T. Perry, Onsite Quality Assurance Supervisor
  • S. Rutter, Quality Assurance Engineer

L. Schwieger, Quality Assurance Director

B. Stiver, Mechanical Engineer

T. Tucker, Outage Coordinator

  • D. Whitney, Engineering and Quality Control Supervisor

W. Wilson, Senior Chemical & Radiation Assistant

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The inspectors also talked with and interviewed several other licensee

employees, including members of the engineering, maintenance, operations,

and quality assurance (QA) organizations.

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  • Denotes those attending the Exit In.terview on January 30, 1981.

2.

Operational Safety Verification

The inspector observed control room operations, reviewed applicable

logs and conducted discussions with control roon operators.

The inspector

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verified the operability of selected emergency systems, reviewed tagout

records and verified proper return to service of affected components.

Tours of the auxiliary building and turbine building were conducted

to observe plant equipment conditions, including potential fire hazards,

fluid leaks, and excessive vibrations and to verify that maintenance

requests had been initiated for equipment in need of maintenance. The

inspector by observation and direct interview verified that the physical

security plan was being implemented in accordance with the station security

plan.

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The inspector observed plant housekeeping / cleanliness conditions and

verified implementation of radiation protection controls. The inspector

also walked down the accessible portions of the makeup and purification

system and emergency power system to verify operability, and witnessed

portions of the radioactive waste system controls associated with radwaste

shipments and barreling.

These reviews and observations were conducted to verify that facility

operations were in conformance with the requirements established under

technical specifications,10 CFR, and administrative procedures.

No items of noncompliance or deviations were identified.

3.

Monthly Maintenance Observation

Station maintenance activities of safety-related systems and components

listed below were observed / reviewed to ascertain that they were conducted

in accordance with approved procedures, regulatory guides and industry

codes or standards and in conformance with technical specifications.

The following items were considered during this review:

the limiting

conditions for operation were met while components or systems were removed

from service; approvals were obtained prior to initiating the work;

activities were accomplished using approved procedures and were inspected

as applicable; functional testing and/or calibrations were performed

prior to returning components or systems to service; quality control

records were maintained; activities were accomplished by qualified personnel;

parts and materials used were properly certified; radiological controls

were implemented; and fire prevention controls were implemented.

Work requests were reviewed to determine the status of outstanding jobs

and to assure that priority was assigned to safety-related equipment

maintenance which may affect system performance.

The following activities were observed / reviewed:

a.

"A" Diesel Generator maintenance.

b.

"B" Diesel Generator maintenance.

c.

Reset of the power to flow setpoints,

d.

Diesel driven fire pump overhaul.

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Following completion of maintenance on the above, the inspector verified

that these systems had been returned to service properly.

No items of noncompliance or deviations were identified.

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4.

gathly Surveillance _ Observations

The inspector observed technical specifications required surveillance

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testing on the CRD Mechanisms, RPS Channel D, Nuclear Service Raw Water

Loop A, and Reactor Building Cooling Fans, Channel, A and verified that

testing was performed in accordance with adequate procedures, that test

instrumentation was calibrated, that limiting conditions for operation

were met, that restoration of the affected components was accomplished,

that test results conformed with technical specifications and procedure

requirements and were reviewed by personnel other than the individual

directing the test,and that any deficiencies identified during the testing

were properly reviewed and resolved by appropriate management personnel.

The inspector witnessed portions of the test activities associated with

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the following test procedures:

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a)

SP E8.02 (1-10-81) - CRD Mechanism Exercising

b)

SP 200.08D 1-22-81) - Monthly RPS Surveillance, Channel D

c)

SP 203.07A 1-20-81) - Nuclear Service Raw Water Loop A

d)

SP 204.04A 1-16-81) - Quarterly RBS Cooling System Fans Surveillance

Test, Channel A

No items of noncompliance or deviations were identified.

5.

Followup on Regional Requests,

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During this period, personnel from the Region V office of the NRC in

Walnut Creek, California, requested information from the Resident Inspectors

regarding the operation and maintenance of the Rancho Seco power plant.

Infonnation was obtained and transmitted to the Region V office concerning:

Security procedures, diesel maintenance and shift staffing requirements.

No items of noncompliance or deviations were identified.

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6.

Systematic Appraisal of Licensee _Pgformance (SA_L_Pj_ Inspections

By letter dated August 28, 1980, J. L. Crews of Region V advised

J. J. Mattimoe of SMUD of aspects of Rancho Seco operations which would

be receiving an increased frequency and/or scope of inspection as a

result of the Region V SALP review. These areas were Design Changes and

iodifications, Quality Ass'urance Audits, Training, and Quality Control

-4 Maintenance. The inspections performed during this period pursuant

t, the SALP evaluation are reported below.

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Review"andkudits

a.

The inspector attended a safety review committee meeting. The

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inspector verified that provisions of technical specifications

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dealing with membership, review process, frequency, and qualifications

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were met. The inspector also verified that decisions made were

reflected in the meeting minutes.

b.

Training

The inspector attended one of the licensee's operator requalification

lecture series and verified that lesson plan objectives were set

and that training was in accordance with the approved operator

requalification program schedule and objectives.

The inspector verified by direct questioning of one new, one experienced.

and one temporary employee that administrative controls and procedures,

radiological health and safety, industrial safety, controlled access

and security procedures, emergency plan, and quality assurance training

were provided as required by the licensee's technical specifications;

verified by direct questioning of one craftsman and one technician

that on-the-job training, formal technical training commensurate

with job classification, and fire fighting training were provided.

No items of noncompliance or deviations were identified.

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7.

Licensee Event Report Followug

Through direct observations, discussions with licensee personnel, and

review of records, the following licensee event reports were reviewed

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to determine that reportability requirements were fulfilled, immediate

corrective actions were accomplished. and corrective actions to prevent

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recurrence had been accomplished i

iccordance with technical specifications.

LER 80-50 (open) West Perimeter TLD Readings Exceeded

LER 81-01 (closed) Degraded Grit Voltage Affecting Motor Starter Coils

No items of noncompliance or deviations were disclosed.

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8.

Followup on Significant Events

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Two significant events occurred during this reporting period:

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A.

Primary to CCW Leak

Samples of the Component Coolant Water (CCW) System taken routinely

on January 12, 1981, indicated a detectable amount of activity.

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After confirming detectable amounts of tritium, cesium, xencn,

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and iodine in the sample, an internal reportable occurrence report

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(AP-22) was written, and the licensee commenced investigation of

the source of the leak. On January 28, 1981,the licensee determined

the source to be the "A" letdown cooler.

Over the sixteen days

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that the investigation was underway, the plant continued to operate

at full power because the size of the leak, which was carefully

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monitored, was shown to be constant and very small.

The Plant

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Review Comittee, the Operations staff, and the Health Physics

and Chemistry staffs were all apprised of the situation and the

"on line" systems which indicate the leak's status were continually

monitored.

An immediate 10 CFR 50.59 review was initiated and

acted upon by the PRC.

No unplanned releases occurred,

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At the close of this report period, the licensee had not determined

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the type of followup action to repair the leak.

A new double capacity

Letdown Cooler is available for replacement of the present "A"

Letdown Cooler, but the licensee had not planned to install it

until the April 1982 outage.

This item will be followed up during a subsequent inspection (81-04-01).

B.

Unplanned Release at Less than Reportable Levels

On January 24, 1981 at approximately 9:00 p.m., Operators observed

two decreases in Makeup Tank pressure.

The total change was equivalent

to depressurization by 2.38 atm. in about 45 minutes.

Investigation of this incident disclosed the fact that at 9:30

p.m., on January 24, the Makeup Tank and the main generator had

been charged with hydrogen. Upon completion of these tasks, the

generator bypass valve was left cracked open and the vent valve

from the hydrogen manifold was opened. The hydrogen bottles were

then isolated from the hydrogen header. With the header at a lower

pressure than the Makeup Tank, fission gases leaked back into the

header and out the open vent.

Subsequent tests revealed PLS-085

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and HV-23506 (a series check valve and a solenoid valve from the

hydrogen header to the Makeup Tank) both leaked.

The temporary corrective action was to close two downstream valves

(HGS-002 and HGS-003) to provide duble valve isolation of the

Makeup Tank from the hydrogen header.

The licensee's calculations performed following the incident indicated

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that no technical specification or 10 CFR 20 limits were exceeded.

At this writing, the PRC has reviewed the 10 CFR 50.59 evaluation

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and has recommended the following:

1.

The check valve and solenoid valve should be repaired during

the present refueling outage.

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2.

A$ engineering review of the system should be perforned.

3.

A detailed review of the existing operating procedures should

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be performed to determine if revisions may be necessary.

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4.

All operating crews should be informed of this occurrence.

5.

If possible, the sJstem itself and the generator should be

checked for potential contamination.

It is the Plant Superintendent's responsibility to act on the PRC's

recommendations.

The inspector will follow up on these and other items related to

this event.

(81-04-02)

9.

Preparations for Refueling

The inspector verified prior to receipt of new fuel that technically

adequate, approved procedures were available covering the receipt, inspection,

and storage of new fuel; observed receipt inspections and storage of

new fuel elements and verified these activities were performed in accordance

with the licensee's procedures; and, followed up resolution of deficiencies

found during new fuel inspection.

The inspector also reviewed the licensee's program for overall outage

control.

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No items of noncompliance or deviations were identified.

10.

Refueling Activities

The inspector verified prior to the handling of fuel in the core, that

good housekeeping was maintained in the spent fuel building and verified

that staffing plans during refueling were in accordance with technical

specifications and approved procedures.

No items of noncompliance or deviations were identified.

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11.

Independent Inspection Effort

Discussions were held between the Resident Inspectors and operations,

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security and maintenance personnel in an attempt to better understand

problems they may have which are related to nuclear safety. These discussions

will continue as a standard practice.

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On numerous occasions, during this report period, the Resident Inspectors

attended operations status meetings. These meetings are held by the

Operations Supervisor to provide all disciplines onsite with a update

on the plant status and ongoing maintenance work.

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In addition to the above, independent inspection effort was performed

on the following items:

a.

Critical Fire Protection Area Ins 2ections,

Over the past two years, as part of the inspector's normal inspection

activities, observations of critical fire areas has taken place.

The critical fire areas include:

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Containment Penetration Valve Areas

Makeup Pump Room

Corridor to (-) 47' Level

Corridor to fiezzanine Level

Corridor to Grade Level

These locations were designated critical fire areas pending completion

of the fire protection modifications required by Amendment 19 to

the license.

The observations included housekeeping practices,

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fire equipment locations, fire suppression system operability and

use of fire watches.

In May of 1980 a QA Audit of the fire protection Amendment 19

modifications indicated that "to the best of the auditor's ability

all Amendment 19 modifications were completed prior to the Rancho

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Seco startup" on May 12, 1980. This was also documented in the

region-based inspector's Inspection Report No. 50-312/80-09.

Accordingly, those locations are no longer critical fire areas and

will be inspected in the future in accordance with normal inspection

requirements.

flo items of noncompliance or deviations were identified.

b.

Degraded Operation of the "B" Dieseljenerator_

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On April 18, 1980, licensee personnel discovered that the piping

between the DC-driven oil booster pump and the governor on the

"B" Diesel Generator was installed incorrectly. A Nonconforming

Report (flCR S-1910) was prepared, a design review was performed

and, based on this, it was determined that a 10 CFR 50.59 review

was not required. The flCR was dispositioned to accept "as is,"

and to continue operating, providing the diesel met the 10-second

starting requirement. The engineering review also recommended

replacement of the governor and piping at the next biannual

inspection

(scheduled for the 1981 outage).

The inspector's record review and personnel interviews indicated

the following:

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(1) 5e'ction 8.2.3.1 of the Final Safety Analysis Report describes

the quick starting feature of the diesel generators.

This

feature includes a DC-driven oil booster pump which provides

hydraulic oil pressure to set the governor fuel racks until

the diesel engine comes up to speed. At that time the direct

shaft-driven oil pump can provide the oil pressure necessary

to maintain the fuel racks in the set position.

(2) The governor was replaced and tiie oil booster lines improperly

installed via Work Request No. 022134 in September,1977.

(3) Tb piping installed in September 1977 represents a change

from the system as described in the FSAR.

This change allowed

the "B" Diesel to be operated in a degraded mode for over

one year.

(September,1977 to the present.)

(4) When this condition was discovered in April,1980,and a Nonconforming

Report (NCR) was prepared, therewas no record of a related

safety analysis (required by 10 CFR 50.59) being performed

which would support continued operation of the diesel in the

above described degraded mode.

(5) The Plant Review Committee (PRC) reviewed the NCR and related

documentation on April 25, 1980. A PRC member called the governor

supplier and determinedon about April 26, 1980 (according to

a licensee representative) that with the improper piping, the

governor would not perfcrm its intended function of providing

13 foot-pounds torque to sat the fuel racks quickly. The

PRC concluded, however, t'H this event was not required to

be reported.

Based on the foregoing

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x es that the licensee failed to

a red by 10 CFR 50.59 to determine

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perform the safety anab y s .

if continued operation t,7 the "G* Diesel Generator while it differed

from the system described in the Final Safety Analysis Report

constituted an unreviewed safety question.

This is an item of apparent noncompliance.

91-04-03)

c.

Followup on Unresolved Items

Item 80-38-01 (Closed).: The licensee's internal AP-22 report referenced

in inspection report 50-31c/80-38, Paragraph 8.c, described procedural

violations dealing with a failure to follow the Work Request Procedure

AP-3.

Violations were identified by the licensee, they were reported

to the Resident Inspectors and corrective action was taken within

a reasonable time. Because the inspector has not found evidence that

the violations occur as a general rule, this item is closed.

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No items of noncompliance or deviations were identified.

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12. _ Exit Interview _

The inspectors met with licensee representatives (denoted in Paragraph 1)

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throughout the month and at the conclusion of the inspection on January

30, 1981, and summarized the scope and findings of the inspection activities.

The licensee acknowledged information tendered on the monthly inspection

activities.

During the exit interview, the inspectors discussed their preparations

for TMI related inspections which are expected to be addressed by the

end of February, 1981. The following NUREG-0737 paragraphs were preliminarily

discussed:

I . A.1.3.1 - Overtime Limits

I.C.5 - Feedback of Operating Experience

I.C.6 - Verification of Operating Activities

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II.D.3.1 - Valve Position Indication

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II.E.4.2.(5b) - Containment Isolation Modifications

No conclusions were drawn on licensee compliance with these paragraphs.

The inspector asked if action had been taken on a 12/22/80 letter to

all PWR licensees from Eisenhut dealing with control of heavy loads

(NUREG0612).

A licensee representative stated that they have seen

NUREG 0612 and have assigned a cognizant engineer from the Generation

Engineering Department to prepare a reply. The inspector also asked

if action had been taken on another licensee's Part 21 Report on 1"

Hilti Kwik-Bolts. A licensee representative stated that the Maintenance

Department has been made aware of the issue.

Two LERs (80-24 and 80-49) were also discussed. These LERs deal with

diesel generator issues and appear to require further review by the

licensee because more or different information may be available than

was originally reported.

Finally, an item of apparent noncompliance

was discussed. This delt with the improper installation of piping

associated with the "B" Diesel Generator D.C. driven oil booster pump

which assists in assurin a quick-start of the diesel.

(See Paragraph

11.b for fur her details .

One item of apparent noncompliance was identified (81-04-03).

This item of apparent noncompliance was further discussed at a meeting

on February 13,1981, between Region V operations management and certain

of the licensee's senior managers. Region V representatives provided

further explanation of the basis for this item of apparent noncompliance

and for the assignment of a severity level,

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