ML19351G012

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IE Insp Rept 50-293/80-27 on 800901-30.No Noncompliance Noted.Major Areas Inspected:Licensee Actions in Response to IE Bulletins & Review of Location of Electrical Load Ctrs
ML19351G012
Person / Time
Site: Pilgrim
Issue date: 12/30/1980
From: Jerrica Johnson, Martin T, Roberts K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML19351G011 List:
References
50-293-80-27, NUDOCS 8102200778
Download: ML19351G012 (11)


See also: IR 05000293/1980027

Text

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50293-800326

50293-800701

U.S. NUCLEAR REGULATORY COMMISSf0N

50293-800814

h

0FFICE OF INSPECTION AND ENFORCEMENT

50293-800821

50293-800903

Region I

50293-800912

50293-800922

Report No. 50-293/80-27

Docket No.

50-293

License No.

DPR-35

Priority

Category

C

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Licensee:

Boston Edison Comoany

800 Boylston Street

Boston, Massachusetts 02199

Facility Name:

Pilgrim Nuclear Power Station

Inspection at:

Plymouth, Massachusetts

Inspection conducted:

September 1-30, 1980

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Inspectors:

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K. Roberts, Resident Insipector

date signed

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J. Johnson, Senior Res(dent Inspector

date signed

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Approved by:

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T. Martin, Chief, Reactor Pr'ojects Section

date signed

No. 3, RO&NS Branch

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Inspection Summary:

Inspection on September 1-30, 1980 (Recort Number 50-293/80-27)

Areas Inspected:

Routine, anannounced inspection of licensee actions on previous

inspection items, an operation safety verification, plant operations (ORC) review,

surveillance and maintenance activities, LER followup, licensee actions in response

to IE Bulletins, and a review of the location of electrical load centers. The in-

spection involved 101 inspector-hours onsite by two resident inspectors.

Results: No items of noncompliance were identified.

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Region I Form 12

(Rev. April 77)

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DETAILS

1.

Persons Contacted

W. Armstrong, Deputy Nuclear Operations Manager

R. Atkins, Staff Engineer - Electrical

E. Cobb, Chief Operations Engineer

W. Deacon, Senior Electrical Engineer

R. Fairbank, Senior I&C Engineer

R. Machon, Nuclear Operations Manager - Pilgrim Station

C. Mathis, Deputy Nuclear Operations Manager

T. McLoughlin, Compliance Engineer

P.'0'Brien, Construction Management Group Leader

R. Silva, Staff Engineer - Mechanical

P. Smith, Chief Technical Engineer

R. Smith, Chemistry Supervisor

The inspectors also interviewed other licensee personnel including members

of the Operations, Maintenance, and Security staffs.

2.

Followup on Previous Inspection Findinos_

(Closed) Unresolved Item (293/80-25-03): Temperature Effects on R.V. Level

Instrumentation.

The inspector reviewed the calculations / data Iised as a

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basis for the recomendation to recalibrate the reactor vessel level instru-

mentation.

Following this review and discussions with the licensee's staff

engineers, the licensee determined that this event was reportable and sub-

mitted LER 80-32.

(0 pen) Unresolved Item (293/80-26-10):

HPCI Exhaust Line Snubbers. The

licensee has continued to experience HPCI exhaust line support problems.

LERs 80-34 and 80-53 describe several events.

On September 18, 1980, the

inspector questioned the licensee concerning plans to resolve the problems

of snubber integrity and transient loads (water hamer) being experienced

during system operation. The licensee replaced two additional (3 Kir',

snubbers nos. S-23-3-36 and S-23-3-37 with higher capacity (20 Kip) snubbers

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on Septerrber 22, 1980.

Plans to resolve thesa problems were also discussed

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during telephone conversations between NRC:IE:HQ D.d Boston Edison Company

NED personnel. The licensee confirmed plans to instrument the HPCI exhaust

line and use the data gathered during system operations to give operational

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loading information.

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The licensee stated that a followup report to the NRC would be provided

detailing the results of the transient analysis and actions to resolve the

problems with water hamer.

(Closed) Unresolved Item (293/79-21-03): The licensee has taken action to

reduce the number of control room annunciators permanently in alarm. The

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inspector has, however, noted on several occasions where more attention may

be necessary. These coments have been provided to the licensee managment

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and actions initiated to resolve them.

The insoector will continue to

review this area during the routine inspection program.

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(Closed) Follow Item (293/78-SB-01):

The licensee has installed an auto-

matic reactor fead pump trip on high reactor vessel water level (60 inches)

in accordance with PDCR 79-14. This modification is also discussed in a

letter (annual report of modifications) oded October 20, 1980 to the NRC.

3.

Operational Safety Verification

a.

Scope

The inspector observed control room operations, reviewed applicable logs

ard conducted discussions with control room operators during the month

of September, 1980. The inspector verified the operability of selected

emergency systems and compliance with limiting conditions for operations.

Tours of the Reactor Building, Turbine Building, Process Buildings,

Security Fence, and Diesel Generator Rooms were conducted to observe

plant equipment conditions including potential fire hazards, fluid leaks,

and excessive vibrations. The inspector also observed implementation of

physical security in the protected and vital areas.

The inspector observed the licensee's action involving a shipment of

radioactive waste on September 18, 1980. This review included the

following items:

Shipping paper documentation; BECO #80-368

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Loading of package (cask / liner) on vehicle

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Radiochemical isotopic analysis.

Liner No. 80-68

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Package (cask) marking / labeling

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Vehicle placarding

Cask certificate / specification

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Radiation / contamination surveys

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Completed procedure check off sheets

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b.

Findin g

(1) During a tour of the ' A' Emergency Diesel Generator (EDG) room

on September 4, 1980, the inspector questioned the Watch Engineer

accompanying him concerning the status of a low lube oil alarm

module that was not in operation. The inspector verified that the

problem had already been identified by the licensee during the daily

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EDG surveillance (OPER 27), that maintenance request no. 80-2778 had

been issued to correct the problem, and observed satisfactory level

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of lube oil in the sump (dip stick).

The inspector had no further questions.

(2) During the review of activities involving the radwaste shipment the

inspector questioned the licensee concerning the location of tamper

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seals on the cask. The licensee had already identified that the

seals should be relocated and corrected this item prior to the

shipment.

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No itams of noncompliance were identified.

(3)

During a tour of the control room the inspector questioned the

operators on shift a- to the cause/ condition of various annunciators

that were in alam or raeded repair.

The inspector aiscussed the status of the control room annunciators

with the licensee management oN stated that apparently many

could be corrected. The licensee acknowledged the inspector's

comments and stated that increased attention would be given to

correcting these items.

On subsequent tours of the control room the inspector noted some

improvements in the numbers of annunciators in alarm and will

continue to monitor the licensee's activities in this area during

future routine inspection.

No items of noncompliance were identified.

(4) The inspector reviewed the station's internal problem / event

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ports (Failure Malfunction Repoits - FMRs) Nos. 80-01 through 90-

143.

The inspector questioned the licensee on several reports as

to the justification for not reporting the events to the NRC.

The licensee representative reviewed the list of FMRs in question

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and provided acceptable reasons / justification for not reporting

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each one.

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No items of noncompliance were identified, however, the inspector

will review the licensee's system for issuing, reviewing FMRs and

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reporting events to the NRC in a future inspection (293/80-27-

01).

c.

Standby Gas Treatment System (SGTS) Charcoal Filters

On September 12, 1980, the licensee identified that the methyliodide

laboratory analysis required by T.S. 4.7.B.1.a.6 (for the data stated

in T.S. 3.7.B.1.b.2) had not been performed. This event is described

in LER 80-59. The licen ae took 1 mediate steps to have the sample

taken and analysis performed.

The inspector questioned the licensee concerning the justification for

continued operation while preparations were being made to remove a

sample of charcoal and investigate vendors capable of performing the

off site analysis. The licensee stated that the efficiency tests (hydro-

carbon) had nct shown any degradation of the filters.

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The inspector stated that because the licensee had not been able to

account for accurate run times on both trains of charcoal and because

a definite correlation between the hydrocarbon test and the methyliodide

test could not be shown, that additional actions were necessary to justify

continued operation.

Duriig i telephone conversation with NRC.iE: Region I personnel and the

licenree representative on September 19, 1980, the licensee agreed to

take 'he following actions by 2400 hours0.0278 days <br />0.667 hours <br />0.00397 weeks <br />9.132e-4 months <br /> on September 25, 1980:

'(1)

Demonstrated the methyliodide removal capability of the charcoal

absorber banks of each SBGTS train satisfy Technical Specification (TS) 3.7.B.1.b(2); or,

(2)

Declared one SBGTS train inoperable and made the other SBGTS train

operable, the latter with a charcoal absorber tank of known

elemental iodine and/or methyliodide removal efficiency of at least

95%; or,

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Initiated actions to be in cold shutdown in 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />.

These actions are described in a letter from the NRC Region I Director

to Boston Edison Company, dated September 19, 1980.

On September 23, 1980, the licensee notified the inspector of the satis-

factory results of the laboratory analysis performed on September 22 1980.

The inspector subsequently reviewed the documentation of the laborato .

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analysis on samples from both trains of charcoal which showed conformance

with T.S. 3.7.B.1.b.2.

The licensee stated that further action would be taken to accurately

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account for run times on each train, and that surveillance procedures

would be developed for ensuring that this analysis was accomplished

as required in the future.

Pending review of the licensee's action to accurately account for run

unresolved (293/80-27-02)plement surveillance procedures, this item is

times and, develop and im

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4.

Plant Operations - Operations Review Committee

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a.

Scope

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The inspector attended an Operations Review Committee (ORC) meeting no.

'80-103 on September 3, 1980 in order to verify membership and frequency

requirements as stated in the Technical Specifications and to observe

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overall conduct of the meeting.

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During this meeting the ORC reviewed plant nadifications, procedure

changes, licensee event reports, and failure / malfunction reports.

b.

Findings

No items of noncompliance were identified however the inspector ex-

pressed concern over not issuing a meeting agenda prior to the meeting,

and the level of detail of items presented during the meeting.

The licensee acknowledged the inspector's statement and agreed to publish

an agenda prior to, and increase the detail of presentations during

future ORC meetings.

The inspector subsequently observed written ORC agenda being issued

and, through conversations with staff members, identified that items

were being presented in greater detail.

The inspector had no further comments in this area.

5.

Surveillance Observations

The inspector observed Technical Specification required surveillance testing

in order to verify that the testing was performed in accordance with approved

station procedures and met the Technical Specification limiting conditions

for operation.

Portions of testing on the following systems were reviewed:

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'A', 'B' RBCCW heat exchanger out of service for cleaning (redundant

equipment testing)

'A' EDG fuel line failure - (redundant equipment testing)

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' A' SBGTS fan failure - (redundant equipment testing)

No items of noncompliance were identified.

6.

Maintenance / Material Preservation

a.

Salt Service Water Piping

During a routine tour of the Intake Structure on September 5, 1980, the

inspector noted significant corrosion on the Salt Service Water system

piping. The inspector discussed the licensee's long term plans for

preservation of the piping and also expressed his concern about the ex-

tent of the through-wall corrosion.

The licensee acknowledged the inspectors concern and stated that an ultra-

sonic examination of the SSW piping would be performed.

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The inspector reviewed results of QC Inspection Report I-80-724

perfonned September 7,1980.

No deficiencies were identified by

the licensee during the UT examination which showed that the piping

wall thickness remaining was between .370 and .435 inches.

The inspector had no further questions in this area.

b.

'A' Emergency Diesel Generator Fuel Line Repair

During a routine surveillance on September 3, 1980, the 'A'

Emergency

Diesel Generator (EDG) was shutdown when a fuel line fitting cracked.

The attending operator immediately noted the failure, notified the

control room, and posted a fire watch.

A priority maintenance request (MR 80-5774) was issued and recundant

components tested in accordance with Technical Specification 3.9.B.3.

The inspector verified that the repair was effected by qualified per-

sonnel using certified material, a properly completed work request with

QC concurrence and appropriate safety tagging.

The 'A' EDG was satisfactorily retested and declared operable at 3:15

a.m. on September 4, 1980.

No items of noncompliance were identified.

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7.

Location of Eiectrical Load Centers

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Because of problems identified at another reactor site, the inspector was

requested to determine whether or not electrical controls for energizing /

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deenergizing valves, which needed to be operated during shutdown to cold

conditions, were located inside primary containment.

The inspector interviewed licensee management, reviewed appropriate electrical

distribution and equipment location drawings and determined that there were

no motor control centers inside the primary containment.

The inspector had no further questions in this area.

8.

Licensea Event Report (LER) Followup

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Through direct observations, discussions with licensee personnel, and review

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of records, the following LERs were reviewed to detennine whether reporting

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requirements were fulfilled, and that corrective actions had been accomplished

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in accordance with the Technical Specifications.

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-80-32; Drywell Temperature.

The licensee iioted higher-than-design tempera-

tures on the drywell and on the reactor vessel level yarway reference columns.

The licensee recalibrated the reactor vessel level instrumentation in July

1980.

The station management did not report this in an LER because of the

initial belief that the calculations were overly conservative.

Following

discussions with the licensee's corporate engineering staff and a review

of the calculations relating level effects to temperature changes, the in-

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spector stated that this event should be reported in an LER.

(See IE In-

spection Report 293/80-25 and Paragraph 2., Unresolved Item 80-25-03, of

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this Report)

-80-53; HPCI Snubber Severed.

(See Paragraph 2 of this Report - Unresolved

Item 80-26-10)

-80-55; RCIC Steam Suoply Valve.

(M0 1301-62) - During surveillance testing

the valve's thernal overload device generated an alarm. Testing revealed no

failed components, however, the thermal overload device was replaced as a

precaution.

The inspector verified that the overload device provides an alarm

only, and that the motor normal running current is less than the motor's rating.

The licensee is investigating why the thermal overload device is set at a lower

current than the normal running current for the motor.

-80-59; Failure to Sample the SBGT System Charcoal Filters (See Paragraph

3.c)

-80-62; ' A' Emergency Diesel Generator (EDG) - During normal surveillance

testing the fuel line 'T' connector fitting failed. The EDG was secured,

a fire watch initiated, redundant testing performed, an inkind replacement

made, and post repair testing completed.

(See also Paragraph 6.b of this

Report)

No items of noncompliance were identified during the review of these LERs.

9.

IE Bulletin Followup

The inspector reviewed the licensee's activities in response to the IE

Bulletin listed below.

-80-06; Engineered Safety Feature (ESF) Reset Controls

The inspector reviewed the licensee's response dated June 27, 19801 Para-

graph 2 of the Bulletin requested a schedule for testing to demonstrate that

equipment remains in the emergency mode after removal of the actuating signal

and/or manual resetting. The licensee's response stated that testing would

be completed prior to startup from the next refueling outage.

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Following questioning by the inspector, the licensee provided a revised

schedule for this testing in an internal memorandum dated September 23,

1980.

The following schedule is described:

Action

Completion Date

1.

Review surveillance / tests

September 30, 1980

2.

Write new procedure and develop

March 31, 1981

testing sequence

3.

Initiate testing

fiay 1,1981

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Complete testing program

Prior to startup following

refuel outage no. 5

This Bulletin remains open pending~ completion of the testing program and

review by the NRC.

-80-07; BWR Jet Pump Failure

The inspector reviewed the licensee's response dated June 19, 1980. This

response describes the inspection performed and replacement of three jet

pump beams.

The licensee also issued LER 80-11 describing the replacement

of the jet pump beams.

During the review of the licensee's surveillance procedure for taking data

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to identify jet pump degradation, the inspector noted that not all the data

required by the Bulletin was being taken. The licensee's procedure only

required individual jet pump d/p to be taken if the recirculation pump speed

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vs. flow showed an anomaly.

The inspector stated that this did not meet the requirements of the Bulletin

and asked for justification for not taking all the required data. The licensee

acknowledged the inspector's statement and stated that the data required by

the Bulletin would be taken, and the surveillance procedure revised accordingly.

This Bulletin remains open pending a review of the revised surveillance pro-

cedure and the implementation thereof.

-80-15; Possible Loss of ENS System with Loss of Off-Site Power

The inspector verified that the correction made to the ring circuit in the NRC

trailer were made as described in the licensee's response dated October 8,

1980.

Tests to date have been made on the ENS extensions in the control room, ECC

trailer, and NRC trailer.

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The licensee plans to install an ENS circuit in the Technical Support

Center (bottom of main guard house) and the new Emergency Offsite Facility

(new trailer comple.x near shorefront road).

This Bulletin remains open pending installation and testing of these phone

circuits.

-80-17; Failure of Control Rods to Fully Insert Durina a Scram at a BWR

The inspector reviewed the licensee's responses to date with resoect to the

B111etin, and supplements, and the actions taken in response to the inspector's

previous connents in this area.

The following items were discussed:

Original Bulletin

Paragraph 2.d - revised response was still pending

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correcting the time for automatic scram.

Paragraph 4 - no documentation of complete training

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concerning procedure revisions was available

Paragraph 6.b - a procedure revision was necessary

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to require all available cooling when torus tempera-

ture exceeded 800F.

The licensee acknowledged the inspector's coment and stated that a revised

response would be issued correcting the scram data, full training on pro-

cedure revisions would be completed and documented by October 15, 1980, and

that a procedure re,ision for torus cooling was in progress and expected to

be approved i.ne n n t day.

Supplement 1

Paragraphs B.1,2 - the licensee's response dated

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August 14, 1980, did not adequately address the

concerns stated in the supplement.

The licensee

subsequently submitted resconses dated Seotember 16,

1980 and September 25, 1980, which describe the equip-

ment to be installed (including indications that will

be available in the control room) and that UT examina-

tions would be performed once per shift versus daily

until the permanent equioment was installed.

This Bulletin remains open pending completion of the required actions and

verification by the inspector.

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10.

Possible Excessive Hardening of Stainless Steel Bolts Durina Heat Treatmert,

On September 29, 1980, the inspector informed the licensee of possible ex-

cessive hardening caused by heat treatment and susceptibility of stress

corrosion cracking of stainless steel bolts used on specific Anchor Darling

valves.

flaterials thought to be included may have been ordered under pur-

chase order 6498-M-132 BC.

The licensee was asked to identify any systems where the subject bolts were

installed and whether in place- hardness tests could and would be performed.

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The licensee stated that a review of the subject valves ordered under the

specific purchase order indicated that the 8 inch RCIC system exhaust swing

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check valve was the only one with stainless steel bolts, that the valve is

located in the torus compartment, and that no specific in-place hardness

testing was planned.

The inspector acknowledged the licensee's statement and had no further

questions at this time.

11. Unresolved Items

Areas for which more information is required to determine acceptability are

considered unresolved.

Unresolved items are discussed in paragraphs 2 and

3.c.

12. Exit Interview

At periodic intervals during the course of the inspection, meetings were held

with sr.nior facility management to discuss the inspection scope and findings.

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