ML19351F601

From kanterella
Jump to navigation Jump to search
Monthly Operating Rept for Dec 1980
ML19351F601
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 01/07/1981
From: Zufelt E
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
Shared Package
ML19351F598 List:
References
NUDOCS 8101130558
Download: ML19351F601 (6)


Text

.

b O

OPERATING DATA REPORT DOCKET NO.

5C-333 DATE January 1981 COMPLETED BY E.

Zufeit TELEPHONE <215)442-3340 OPE.R ATING STAT 1]S Fit 7. Patrick Notes I. Unit Name:

2. Reporting Period:,

801201-801211

3. Licensed Thermal Power (MWt):

24]6 oe3

4. Nameplate Rating (Gross MWe):
5. Design Electrical Rating (Net MWe):

821

6. Maximum Dependable Capacity (Gross MWe):

830 810

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Last Report, Give Reasons:

NONE NONE

9. Power Level To Which Restricted,if Any (Net MWe):
10. Reasons For Restrictions,If Any:

This Month Yr to.Date Cumulative 7##

870N kIb17 I1. Hours In Reporting Period

12. Number Of Hours Reactor Was Critical 744 6283 8 32914
13. Reactor Reserve Shutdown Hours 0

0 0

14. Hours Generator On-Line 744 6164.8 31902.8
15. Unit Reserve Shutdown Hours 0

0 0

16. Gross Thermal Energy Generated (MWH) 1755702 12995400 64183594
17. Gross Electrical Energy Generated (MWH) 614520 4475810 21829510
18. Net Electrical Ee.igy Gene sted (MWH) 505225 4934505-21125080
19. Unit Serv' e Factor 100%

70.2%

67.O%

20. Unit f.vailability Fac,3, 100%

70.2%

67.O%

21. Ur.st Capacity Facey (Using MDC Net) 98.8%

61.5%

60.1%

97.4%

60.1%

54.On

22. anit Capacity Facter(Using DER Net) -

l

23. Unit Forced Outage Rate 0%

4.O%

18.2%

24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Eacht:

Scheduled snubber inspection and maintenance outage in early February, 1951 for approximately 10 days.

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation):

Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 810113055%

1

. ~_

~

AVER ACE DAILY UNIT POWER LEVEL 50-333 DOCKET NO.

JAFNPP WIT DATE January. 1981 E. Zufelt CO\\tPLETED BY (315 h42-3840 7ttgp3,oss DECEMBER 1980

$10ND{

DAY AVER ACE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (h!We Net) stWe Ner) 819 821 37 821 021 2

822 19 R9n 3

823 20 820 4

821 824 2:

s 820 821 22 6

822 829 23 7

823 823 24 s

023 820 25 9

822 820 26 to 684 820 27 820 821 2s 12 822 530 2,

13 021 647 30 34 829 767 3:

15 010 16

SUMMARY

Unit operated at near 100% rated thermal power for this reporting period with two reductions in power for rod pattern change and scram testing.

4 L--

---.-.-w.

. ----w<

50-333 DOCKET NO.

UNIT SilUTDOWNS AND POWER REDUCTIONS UNIT N AME

.I A b,111,i, DATE

'3 HD"4 PV i 1901 COMPLETEDg sii t

REPORT MONTil DECEMBER, 1980 i

e, C

w

!E 3

yY}

Licensee Eg g*3 Cause & Corsective Daic h

3g

(

2ie Event g?

Action to gV Psevent Recurrence

$ I, 5

j ;y, g Report ar mV g

c5 19 801213 3

0 11 14 t;/A

!!/A fl/A Power reduced for control rod sequence excliange.

20 801227 S

0 11 14 t1/A ti/A ti/A Power reduced for scram discharge volume test per flRC Bulletin 80-17 Supp. 14.

I 2

3 4

F: Forted Reason:

Method:

Ealubii G - Insisucianis S: Scheduled A Equipment Failure (Emplain) 1 Manual fo Piepasation of Data B Maintenance ci Tes 2 Manual Scram.

Entry Shecis l'or Licensee C. Refueling 3 Automatic Scram.

Event Repose (I f R) File (NURI C-D. Regulatory Restricsion 4-Other (E mplai 0 0161)

L Operator Training & License Examination F.Adnunist rative 5

G-Opesaisonal Escur (Emplaud Estubii 1 Sanw Souice ll Other I E m plaui)

i t

POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT NARRATIVE

SUMMARY

OF OPERATING EXPERIENCES DECEMBER, 1980 During this resorting period, the unit operated at near 1007.

of its rated c:1ermal power.

There were two power reductions during this reporting period.

The first was on December 13, 1980 for a control rod sequence exchange and the second reduction was on December 27, 1980 for scram dischstge volume testing per NRC Bulletin 80-17 Supplement No. 4.

POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT

~

t SAFETY RELATED ELECTRICAL & MECHANICAL MAINTENANCE

SUMMARY

REPAIR WORK REQUEST #

DATE SYSTtEM HOW DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIME COMPONENT #

HOURS 12/4 11 10434 Visual Leaking Packing.

Tightened Packing.

4 P-2B 12/11 76 10348 Operations Faulty local heat Replaced faulty heat detector.

2 IFPSN42 detector gave false alarm.

12/11 23 10505 Operations Torque switch gear pin Replaced tocque switch, adjusted 50 MOV-16 sheared on valve opera-valve travel, and rewound burned

tor, motor.

12/15 93 10528 Visual Burnt panel lamps.

Replaced burnt lamps.

1 ECP-A,D 12/12 24 10524 Operations Failed solenoid coil Replaced coil.

3 EOD-1 on electric door.

12/19 23 10213 Operations Defective wires to Repaired wires - P.M. performed on 10 P-141 spare motor heater.

motor.

12/19 14 10499 Audio Defective motor Replaced bearings.

44 P-2A bearing.

12/21 93 10515 Visual None - suspected exhaust Ran engine - no leak.

2 EDG-A leak.

I l

l l

l

POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT

~

MAINTENANCE

SUMMARY

DECEMBER 1980 I&C ACTION TAKEN REPAIR CAUSE OF RESULTS OF WORK REQUEST #

DUEG ED DATE SYS TEM COMPONENT #

MALFUNCTION MALFUNCTION R CU R RS 12/16 02-3 10523 I&C Mechanical lock Erratic Repaired lock 8.0 DPIS-101D screw setpoint screw 12/16 03 10455 I&C Design Spurious high Replaced coax 105.0 UTSC A,B,C,D alarms w/triax cable 12/16 17 10379 OPS Age /Use fligh alarms Replaced 25.0 PS-001A metering valve 12/6 27 10185 I&C Unknown OR-80-225 Calibrated 14.0 HAZ-101A/B 12/6 27 10215 Maintenance De fective No heat Replaced Q4 15.0 DTS-102A Transistor tracing ggkedzero&

i m"

e

- -