ML19350B387

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Forwards IE Info Notice 81-06, Failure of Ite Model K-600 Circuit Breaker. No Response Required
ML19350B387
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 03/11/1981
From: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Hines E
DETROIT EDISON CO.
References
NUDOCS 8103200389
Download: ML19350B387 (2)


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NUCLEAR REGULATORY COMMISSION 1

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P 7M ROOSEVELT ROAD j

GLEN ELLYN, ILLINOIS 60137 March II, 1981 Gentlemen:

The enclosed IE Information Notice No. 81-06 contains information that may be applicable to your facility regarding the failure of an ITE Model K-600 circuit breaker. No specific action or response is requested at this time; however, pending the results of NRC staff evaluations of this matter, further licensee actions may be requested.

Should you have any questions regarding this information notice, please contact this office.

Sincerely, f $Ar D

.w' James G. Keppler Director

Enclosure:

IE Information Notice No. 81-06 8103200 q

I SSINS No.:

6835 Accession No.:

8011040269 IN 81-06 UNITED STATES NUCLEAR REGULATORY COMMISSION O

g m' 7-J 0FFICE OF INSPECTION AND ENFORCEMENT o o c:

WASHINGTON, u.C.

20555 March 11, 1981 IE Information Notice NO. 81-06:

FAILURE OF ITE MODEL K-600 CIRCUIT BREAKER

Purpose:

The purpose of this information notice is to provide early notification of a matter that could adversely affect the safety of nuclear power plants.

Toward this end, this information notice alerts holders of operating licenses and construction permits of a possibly generic deficiency involving Model K-600 circuit breakers manufactured by ITE.

Description of Circumstance:

By letter dated February 20, 1981, the Sacramento Municipal Utility District informed us that, while performing preventive maintenance on electrical circuit breakers at its Rancho Seco facility, an ITE Model K-600 breaker was observed not to trip.

An investigation revealed that a tripping coil wire had slipped out of its terminal.

Further examinations revealed that the coil wire size was AWG 20, whereas the mating lug was sized for AWG 16-14 wire. A check of other ITE electrical breakers indicated that the problem may be generic.

Subsequent to the letter, the Sacramento Municipal Utility District informed us orally that ITE Model K-1600 breakers have the same deficiency and that Model K-3000 breakers may be similarly affected.

The information provided by the Sacramento Municipal Utility District is pre-lirinary and will be followed by a complete report.

Consequently, we have not yet evaluated the safety significance of this event.

Nevertheless, the information herein is being provided as an early notification of a possibly significant event.

Although no specific action or response is requested at this time, recipients should review the information for possible applicability

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to their facilities.

If NRC evaluations so indicate, further licensee actions l

may be requested.

If you have any question regarding the information contained herein, please contact the Director of the appropriate NRC Regional Office.

Attachment:

l Recently issued IE Information Notices l

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Attachment IN 81-06 March 11, 1981 RECENTLY ISSUED IE INFORMATION NOTICES Infornation Date of Notice No.

Subject Issue Issued to 81-05 Degraded DC System at 2/10/81 All power reactor Palisades facilities with an OL or CP 81-04 Cracking in Main Steam 2/27/81 All power reactor Lines facilities with an OL 81-03 Checklist for Licensees 2/12/01 All power reactor Making Notifications of facilities with an Significant Events in OL Accordance with 10 CFR 50.72 81-02 Transportation of 1/23/81 All Radiography Radiography Devices licensees 81-01 Possible Failures of 1/16/81 All power reactor General Electric Type facilities with an HFA Relays OL cr CP.

80-45 Potential Failure of 12/17/80 All PWR facilities BWR Backup Manual Scram with an OL or CP Capability 80-44 Actuation of ECCS in the 12/16/80 All PWR facilities Recirculation Mode While with an OL or CP in Hot Shutdown 80-43 Failures of the Continuous 12/5/80 All power reactor Water Level Monitor for facilities with an the Scram Discharge Volume OL or CP at Dresden Unit No. 2 80-42 Effect of Radiction on 11/24/80 All power reactor Hydraulic Snubber Fluid facilities with an OL or CP 80-41 Failure of Swing Check 11/10/80 All power-reactor Valve in the Decay Heat facilities with an

' Removal System et Davis-OL or CP Besse Unit No. 1

'OL = Operating Licenses CP = Construction Permits

t Docket No. 50-341 The Detroit Edison Company ATTN: !!r. Edward liines, Ass is tant Vice President and ?!anager Quality Assurance 2000 Sect,nd Avenue Detroit, ?!I 48226 cc w/cac1:

Central Files AD/ Licensing AD/ Operating Reactors AEOD Resident Inspector, RIII PD' acal PDR NS1C TIC k/ '

Ronald Callen, flichigan Public t-Service Commission x

Eugene B. Thomas, Jr., Attorney S

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