05000260/LER-1981-017-03, /03L-0:on 810409,unit 2 Reactor Zone Ventilation Sys Found Isolated.Caused by Temporary Alteration Which Bypassed Isolation During Relay Replacement.Controlled Shutdown Initiated

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/03L-0:on 810409,unit 2 Reactor Zone Ventilation Sys Found Isolated.Caused by Temporary Alteration Which Bypassed Isolation During Relay Replacement.Controlled Shutdown Initiated
ML19347E638
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 05/05/1981
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19347E635 List:
References
LER-81-017-03L, LER-81-17-3L, NUDOCS 8105130162
Download: ML19347E638 (2)


LER-1981-017, /03L-0:on 810409,unit 2 Reactor Zone Ventilation Sys Found Isolated.Caused by Temporary Alteration Which Bypassed Isolation During Relay Replacement.Controlled Shutdown Initiated
Event date:
Report date:
2601981017R03 - NRC Website

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U.S. NUCLEAR REOULATCRY COMMISSION NRC FORM 364 (7 77) i.lCENSEE EVENT REPORT

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(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI l o l t l l A l L l B l R l F l 2 l@15l 0 l 0 l - l 0 l 0 l 0 l 0 l 0 l-l 0 l 0 l@l 4 l 1 l 1 l 1 l

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8 60 68 DOCKET NUMSER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROSABLE CONSEQUENCES h l o 12 l l During normal operation, at full power _ esdv state, the unit 2 reactor zone I

l o t a l I vent 11ation system 5.solated. The isolation wac, bypassed and a controlled shutdown l

lo ;4l lwas begun. Upon completion of repairs and return of the ventilation system l

loisl l to normal, the shutdown was terminated. (T.S.3.2. A Note G.)

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t o is l l on the health or safety of the public. One chennel in a redundant system was l

to(7l l operable.

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35 36 31 40 41 42 43 44 47 33 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h l i l o l l During replacement of a relay a temporary alteration was employed which bypassed l

ti1il lthe isolation. Initiated IP-2 unusual event.

Initiated controlled shutdown i

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jwhich was terminated upon completion of repairs and return of the system to normal.

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Tenncss:2 -Valley Authority Form BF-17

- Browns Ferry Nuclear Phnt BF 15.2 3/24/81 i

LER SUPPLEMENTAL INFORMATION BFRO 260 /

8117 Technical Specification Involved 3.2.A, Note G Reported Under Technical Specification

6. 7.2. b( 2) i Date of Occurrence 4/9/81 Time of Occurrence _,0100 Unit 2

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Identification and Description of Occurrence:

Reactor zone ventilation isolation was bypassed.

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Conditbns Prior to Occurrence:

Unit 1 at 95%

Unit 2 at 100%

Unit 3 at 100%

i Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment. Describe.

Checked RM's - they were all normal. Checked circuits, 16AK61A burned up.

(Started down) TACF to get R.B. vent back to prevent a hard scram.

r-t Apparent Cause of Occurrence:

While replacing relay, temporary alteration was employed which bypassed isolation.

Analysis of Occurrence:

There was no damage to plant equipment. There was no activity release, no personnel exposure or injury and no dange.r to the health or safety of the public.

Corrective Action

Unusual event initiated controlled shutdown.

IP 2 was initiated, repairs

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were made and upon completion of repairs and return of the ventilation system to nor=al, the shutdown was terminated.

Failure Data:

NA

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  • Retention : Teriod - Lifetime; Responsibility - Document Control Supervisor
  • Revision:

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