ML19347D291

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AO 10-75:on 750513,external Piping Could Not Be Adequately Drained Prior to First Cut During Preparations for Moving Primary Core Spray Sys Valves to Higher Elevation.Cause Not Known But Leak Suspected at Lower Pipe Fitting
ML19347D291
Person / Time
Site: Big Rock Point File:Consumers Energy icon.png
Issue date: 05/13/1975
From: Sewell R
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
AO-10-75, NUDOCS 8103110752
Download: ML19347D291 (2)


Text

sA 091 LL 1100RMD VEDZ78(10DI)(1-0. 343C134)PD 05/14/75 0954 TLX CONSPO*4ER JKN

,*a ZCZC 205 DLY JACKSON MICHIGAN 5-14-75 EE PMS USNRC E$

ATT MR J G KEPPLER dy 799 ROOSEVELT ROAD GLEN ELLYN, IL 60137 RE DOCKET 50-155 LICENSE DPR-6 N

THIS REPORT IS SUBMITTED TO CONFIRM THE TELEPHONE REPORT TO MR XILEY In UF YOUR OFFICE ON MAY 13, 1975.

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REPORT NO-A0-10-75 DOCKET NO 50-155 g

2A. REPORT DATE-MAY 13, 1975

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28. OCCURRENCE DATE-MAY 13, 1975 3.

FACILITY-BIG ROCK POINT PLAUT 4.

IDENTIFICATION OF OCCURRENCE-SUSPECTED LEAK IN CORE SPRAY Q

SPARGER PIPING CONNECTION INSIDE THE VESSEL.

5.

CONDITIONS PRIOR TO OCCURRENCE-PLANT IN COLD SHUTDOWN FOR b~M MAINTENANCE AND MODIFICATION ACTIVITIES ASSOCIATED WITH POST-()

INCIDENT SYSTEM ENVIRONMENT DEFICIENCIES (AO-1-75).

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DESCRIPTION OF OCCURRENCE-DURING PREPARATIONS FOR MOVING Tl!E y(!)

PRIMARY CORE SPRAY SYSTEM VALVES TO A HIGHER ELEVATION, IT WAS NOTED 3

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TlilS DOCUMENT CONTAINS l

POOR QUAUTY PAGES

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Tb El,0 i dB THAT THE EXTERNAL PIPIT!G COULD NOT BE ADEQUATELY DRAINED PRIOR 'f0

- MAKIN'3 THE FIRST CUT.

SINCE THE WATER IN THE VESSEL VAS BELOW THE N

SPAR 3ER BUT NOT BELOV THE LOWEST CONNECTION ON A SHORT " CLAMPED h '

LOWER FITTIN3.

FITTIN3" PIPING SECTION IN THE VESSEL, A LEAK IS SUSPECTED AT THE 7:

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b5 7.

DESIGNATION OF APPARENT CAUSE OF OCCU9RENCE-EXACT CAUSE UN-(*t KNOWN.

8.

ANALYSIS OF OCCURRENCE-PRELIMINARY DATA INDICATES A LEAK OF b !

APPROXIMATELY 22 GALLON / HOUR AT STATIC VESSEL HEAD OF APPROXI!!ATELY C2 1.3 PSIG.

THE SUSPECTED LEAK POItJT IS APPROXIMATELY 3-1/2 FEET ABOVE THE FUEL AND THUS REPRESENTS NO HAZARD TO UNCOVERING THE FUEL

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JE; d5f IN THE VESSEL.

IN ADDITION, THE PIPIN3 SECTION IN QUESTION IS !!07 fn.3 c

I A PORTION OF THE PRESSURE BOUNDARY.

THE HEAD IS ON THE VESSEL VITl!

THE BACKUP CORE SPRAY SYSTEM AVAILABLE FOR THE MODIFICATION VORK IN l

PROGRESS.

THE DRAINING PROCESS VAS BEING DONE INSIDE CONTAINEEUT La ;

AND WATER IS THUS PROCESSED IN THE RADWASTE FACILITY.

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9.

CORRECTIVE ACTION-INVEUTIGATIVE ACTION IS IN PROGRESS'TO DE-i (J)

TERMINE NATURE OF LEAKAGE AND SUBSEQUENT ANALYSIS AND CORRECTIVE M

KACTION.

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IC. QFAILURE DATA - N/A 4

l CORRECTIION ON NUMBER 8.

SECOND - HAVE A PILE UP ON FIRST WORD

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SHOULD BE APPROXIMATELY 22 GALLON / HOUR, ETC (El

[.3 VV3VM CC DIRECTORATE OF LICENSING WASHINGTON DC FM...l C J HARTf1AN BIG ROCK NUCLEAR O

m R B SEWELL l@

l NUCLEAR LICENSING ADM

~,n CONSUMERS POVER CO 1945 V PARNALL RD JACKSON, MI 49201 g1 I

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