ML19346A413
| ML19346A413 | |
| Person / Time | |
|---|---|
| Site: | Rancho Seco |
| Issue date: | 06/05/1981 |
| From: | Colombo R SACRAMENTO MUNICIPAL UTILITY DISTRICT |
| To: | |
| Shared Package | |
| ML19346A408 | List: |
| References | |
| NUDOCS 8106190288 | |
| Download: ML19346A413 (3) | |
Text
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I OPERATING DATA REPOP.T DOCKETNO. 312 DATE 81-05-31 COMPLETED BY _R. W.
Colombo TELEPHONE (01 M 642-3211 OPERATING STATUS Notes
- 1. Unit Name:
Rancho Seco Unit 1
- 2. Reportir'; Penod:
Mav. 1o01 Cycle V began @ 0048 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />
- 3. Licensed Therma! Power ($1hri:
2772 on 5-10-81.
- 4. Namep! ate Ratin; 4Grn3$ AlWet:
363
- 5. Desi;n Ele:trical Retin; # Net.'th ei:
918 I
- 6. Sf aximum Dependaele Capaci:y tG m \\ihei:
917
- 7. Slaximum Depend.:ble Capacity 4 Net.\\la t:
873 e
- 8. If Chan;es Occur in Capacity Ra:inp !!:em> Number 3 Throu;h 7) Since Last Report. Gise Ressor.o N/A
- 9. Power Lese! To Which Restr:eted. If Any (Net \\lh e):
N/A
- 10. Reasons Fer Restrictions. If Any:
N/A This >!onth Yr.-to.Dat e Cumulative o
- 11. Hours in Repor:in; Period 74L 3 671 G1 66L
- 12. Number Of Hour, Reactor Was Critical 214 954.2 32.450.4
- 13. Re.:etor Resene Shutdown !!ours 0
0 4.L69.6
- 14. Hours Generater on.Line 168.1 889.4 11.115.0
- 15. Unit Resene Shutdown Hours 0
0 1.210.2
- 16. Gross Th :rmal Ener;y Generated (SIWil) 275.851 7.270.701 79.242.956
- 17. Grow Electrical Ener;> Generated a\\lk H, 83.990 754.358 26.702.072
- 13. Net Electrica! Ener;y Generated i\\!h M)
__69.959 709.683 25.235.808
- 19. Unit Senice Factor 22.6 24.5 G8.0
- 20. Unit Assi!ahili:y Facroe 22.6 24.5 60.3
- 21. Unit Capacity Factor tC3in;ilDC Ne:1 10.8 22.L 53.9
- 22. Unit Capacity Factor IC.:; DER Net) 10.2 21.3 51.2
- 23. Unit Forced Outage Rate 68.1 28.8 29.3
- 24. Shutdowns Scheduled Our Neu c3.itonths tty pe. Date and Duratien of Exh t:
H/A
- 25. If Shut Down At End Of Report Peri.d. E> tim.ited D;:e of Startuy June 30. 1981
- 26. Unit > In Test Status tPrior :o Commere:at Operatmn)-
Forecast Achiesed INITI \\ L CRIT!C \\ LITY N/A N/A INITI \\L ELE ( TRICin N/A _
N/A CO\\l\\1ERCI \\ L GPia \\ r!ON N/A-N/A 81m w n P00R ORIGINAL
AVERAGE DPiLY UNIT POhER LEVEL DOCKET NO.90-112 UNIT Rancho Seco Unit 1 DATE 81-05-31 COMPLETED BY R. W. Colombo TELEl HONE (916) 452-3211 MONTH May. 1981 l
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWEP. LEVEL IMWe-Net I (MWe Net)
I n
17 16 2
0 is 0
3 0
19 0
4 0
0 20 5
0 21 0
6 0
22 0
7 0
23 0
g 0
24 0
9 0
25 0
10 223 26
'O II 279 27 0
12 182
- g 0
13 479 29 0
14 506 30 0
15 616 33 0
16 730 INS 11tUCTIONS On this format. list the eerage daily unit power leselin \\tWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
(4 /77 )
DOCKET NO. 50-312 UNITSilUTDOWNS AND POWER REDUCTIONS UNIT NAME Rancho Seco Unit i DATE 81-05-31 COMPLET ED llY R W.
Colombo REPORT MONTil May. 1981 TELEPil0NE 1916) 452-3211 E
15
.E_ E "g
$.Y 5 Licer.sce
,E r, f.
Cause & Corrective No.
Date g
3g
.3 g &
Event j"y a-3 Action to
$~
j'. @ ='
Report 4
<d u
!O Prevent Recurrence H
s o
a 1
81-05-01 S
216.8 C
1 N/A N/A N/A Fourth refueling outage ended @
0048 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> on 81-05-10.
2 81-05-17 F
359.1 A
1 81-026 01 T CC HTEXCH OTSG tube leak.
Four tubes plugged, i
2 3
4 F: Forced Reason:
Method:
Exhibit G Instructions S: Scheduled A Equipment Failure (Emplain) 1 Manus' for Preparation of Data H-Maintenance of Te:;
2-Manualderam.
Entry Sheets fur Licensee C Refueling 3-Automatic Scram.
Event Report (LER) File (NUREG-D llegulatory Restriction 4-Other (Explain) 0161)
E Operator Training & License Examination F Administrative
'S G Operational Error (Explain)
Exhibit I - Same Source (9/77)
!8 Other (Explain)
~
.e REFUELING INFORMATION REQUEST l
11.
Name of Facility:
Rancho Seco Unit 1 2.
Scheduled date for next refueling chutdown:
April. 1082 l
3.
Sdheduled date for restart following refueling:
October. 1082 4.; Technical Specification change or other license amendment required:
a) 1 Change'to Rod Index vs. Power Level Curve (TS 3.5.2) b)
Change to Core Imbalance vs. Power Level Curve (TS 3.5.2) c) Tilt Limits (TS 3.5.2) 5.
Scheduled date(s) for submitting proposed licensing action:
Febraurv. 1082 6.
Important licensing considerations associated with refueling:
None
' 7,
. Number of fuel assemblies:
a)
In the. core:
177 b)
In the Spent Fuel Pool:
196 L
I
-8.
Present licensed spent fuel capacity:
579 l
9.
Projected date of the last refueling that can be discharged to the Spent Fuel Poo'1:
1987 m
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