ML19345D658
| ML19345D658 | |
| Person / Time | |
|---|---|
| Site: | Vermont Yankee File:NorthStar Vermont Yankee icon.png |
| Issue date: | 12/09/1980 |
| From: | Bernard D, Burger F VERMONT YANKEE NUCLEAR POWER CORP. |
| To: | |
| Shared Package | |
| ML19345D657 | List: |
| References | |
| NUDOCS 8012160432 | |
| Download: ML19345D658 (8) | |
Text
O VERMONT YANKEE NUCLEAR POWER STATION MONTHLY STATISTICAL REPORT 80-11 FOR THE MONTH OF NOVEMBER, 1980 l
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1 8012160fdA
OPERATING DATA REPCRT DOCKET NO. 50-271 DATE 801209 COMPLETED ST D. Bernard I
TELEPHONE 617-366-8811, X2215 OPERATING STATUS Notes
- 1. Unit Name:
Vermont Yankee
- 2. Reporting Period:
November
- 3. Licensed Thermal Power (Wt):
1593
- 4. Nameplace Racing (Gross We):
540
- 5. Design Electrical Racing (Net We): 514(open)SO4(closed)
- 6. May h nm Dependable Capacity (Gross We): 535
- 7. Wmma Dependable Capacity (Net We):
504
- 3. If Changes Occur in Capacity Ratings (Items Number 3 Through 7)Since Last Report, Give Reasons:
- 9. ?over Level to Which Restricted,If Any(Net We):
- 10. Reasons For Restrictions, If Any:
This Month Tr-to-Date Cumulative
- 11. Hours In Reporting Period 720.00 8040.00
- 12. Nu=ber Of Hours Re.'ctor Was Critical 0.00 6266.89 57425.28
- 13. Reactor Reserve Shut town Hours 0.00 0.00 0.00
- 14. Hours Generator On-Lit.S 0.00 6200.10 55527.88
- 15. Unit Reserve Shutdown Riurs 0.00 0,00 0,00
- 16. Cross Thernal Energy Gens raced (WE) 0.00 9347971.00 78572584.00 i
- 17. Gross Electrical Energy G6'erated(WH) 0.00 3136006.00 26105676.00 i
- 18. Net Electrical Energy Generc ed(W R) 0.00 2972808.00 24741173.00
- 19. Unit Service Factor 0.00 77.12 77.30
- 20. Unic Availability Factor 0.00 77.12 77.30 l
- 21. Unit Capacity Factor (Using MDC Net) 0.00 73.36 68.34
- 22. Unit Capacity Factor (Using DER Net) 0.00 71.94 67.01
- 23. Unit Forced Cutage Rate 100.00 4.31 6.28
- 24. Shut:fowr.s Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
Refueling in progress.
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- 25. If Shut Down At End Of Re. port Period, Esti=ated Date of Startup:
Late December j
- 26. Units In Test Status (?rior to Cc:mnercial Operation):
Forecast Achieved l
INITIAL CRITICALITY I
INITIAL ELECTRICITY COMMERCIAL OPERATION 1
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AVERAGE DAILY UNIT POWER LEYEL
~
DOCKET NO.
50-271 UNIT Vermont Yankee DATE
,.jp COMPLETED BY F.J.
. ger TELEPHONE 802-257-7711.X137 MONTH vov mher DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY P0hTR L3'IL (MWe-Net)
(MWe-Net) 1.
0 17.
n 2.
0 18.
0 3.
0 19.
o 4.
0 20.
0 5.
0 21.
0 6.
0 22.
0 7.
0 23, o
8.
0 24.
0 0
9.
25.
0 0
10.
26.
0 0
11.
27.
0 0
12.
28.
0 13.
0 29.
n 14.
0 30.
n 15.
0 31.
16.
O INSTRUCTIONS:
On this format, list the average daily unit power level in MWe-Net for each day in the reporting :onth. Compute to the nearest whole megawatt.
1 UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO 50 271 UNIT NAME Vermont Yankee j
REPORT HONTH November COMPIETE B F
Bur g TELEPIM)NE _ 802-257-7711,X137 j
i 07 m
% ** o N
Cause & Corrective No.
Date g
g g
fg License g4 htion to 8
Re rtl IH
- r:
u O
80-21 800926 S
720 C
1 N/A RC FUElXX N/A 80-22 801124 F
162 A*
4*
80-37/IT CG PIPEXX The pipe cracking is believed to have been i
caus<d by ICSCC. The Sweep-0-Let is under-
- sang a failure analysis to determine the cause of the cracking.
The Sweep-0-Let and piping are being replaced with materials which meet the intent of Section II of NUREC 0313,Rev.1, 3
dated October.1979.
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)
- See LER 80-37/IT 4
i F: Forced Reason:
Hethod:
Exhthit G-Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Haintenance or Test 2-Manual Scram Entry Sheets for I.icensee C-Refueling 3-Automatic Scram Event Report (I.ER) File D-Regulatory Restriction 4-Other (Explain)
(NUREG 0161) 1 E-Operator Training & License Examination F-Administrative 5 Exhibit I - Same Source l
G-Operational Error (Explain)
II-Other (Explain) i 7/80
DOCKET NO.
50-271 UNIT Vermont Yankee DATE 801209 COMPLETED BY F.J. Burger TELEPHONE 802-257-7711, X137 SAFETY RELATED MAINTENANCE Page 1 of 3 NATURE OF MALFUNCTION ER OR O WACE EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION Electrical Penetration Corrective N/A Worn Components Leakage Repaired By Vendor X101A MR 79-837 RilR Valves V10-34A Corrective N/A Set Point Drif t Valves Would Adjusted Torque Switch and 39A HR 80-352 Not Go Fully Settings Shut Instrument Isolation Corrective N/A Worn Packing Leakage Repacked Valve Valve RV-12B MR 80-508 Contaliunent Atmosphere torrective N/A Worn "O" Rings Leakage Replaced "O" Rings Control Valve V16-20-20 MR 80-975 MSIV 80-D Air Correctfve N/A Worn "0" Rings Air Leakage Replaced "O" Rings Pilot Valve Mk 80-1087 "B" Diesel Generator Corrective N/A Dirt in Selector Therraocouple Cleaned Switch
- 4 Cylinder Thu ocouple MR 80-1096 Switch Inoperable H.lR Service Water Corrective N/A Nonnal Operation Loose Nut, Tightened and Adjusted Pipe llanger 11-133 MR 80-1129 Excessive Hanger Movement IRM "C" Corrective N/A Failed Preamp Failed IRM Replaced Components MR 80-1145 e
DOCKET No.
50-271 UNIT Vermont Yankee DATE 801209 COMPLETED BY F.J. Burger TELEP110NE 802-257-7711, X137
[
SAFETY RELATED MAINTENANCE i
Page 2 of 3 NATURI: OF MALFUNCTION ER OR OW ACF.
EQUIPMENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION RPS/Analor, Trip System Corrective N/A Failed Component Failed Power Replaced Power Supply Power Supply 25-6A 32 MR 80-1152 Supply liCU 06-35 Corrective N/A Failed "0" Rings Leakage Replaced Accumulator MR 80-1172 Fuel Pool Coaling Corrective N/A Not Isolated During Needs Calibra-Calibrated Pressure Indicator MR 80-1173 Ilydro tion PI-69A I
RilR lleat Exchanger Corrective N/A Failed Sasket Leakage Replaced Casket E-14-1A MR 80-1179 P,cactor Recircula*. ion Preventive N/A N/A N/A Repacked Valve V.lve V2-65A MR 80-1191 RCIC Valve V12-15 Corrective N/A Switch Broken N/A Replaced Switch Torque Switch MR 80 1197 While Preforming Maintenance on Valve Operator "B" Diesel Cencrator Corrective N/A Normal Operation /
Faulty Indica-Repaired As Necessary Pyrometers #1 & #6 MR 80-1201 Vibration tion t
.=
DOCKET NO.
50-271 UNIT Vermont Yankee DATE 801209 COMPLETED BY F. J. Burger TELEPHONE 802-257-7711, X137 SAFETY RELATED MAINTENANCE Page 3 of 3 NATURE OF MALFUNCTION ER OR M AGE EQUIPsENT MAINTENANCE NUMBER CAUSE RESULT CORRECTIVE ACTION "A"
SBCT Corrective N/A Dirt High AP at Cleaned As Necessary MR 80-1211 Demister MSIV 80-D Corrsctive N/A Normal Operation Dry Bushings Lubricated Bushings MR 80-1216 "A" Diesel Generator Corrective N/A Worn Parts Air Leakage Replaced Valve Air Start System Relief MR 80-1218 Valve
~
Service Air Valves Preventive N/A N/A N/A Disassembled and Cleaned V72-76 A & B, V72-78 A-D, MR 80-1222 Valves, Replaced Caskets V72-80 A-D, for the Diesel Generator Air Start System "A"
& "C" RllR Service Corrective N/A Set Point Drift Leakage Disassembled & Cleaned Water Pump Relief Valves MR 80-1247 Valves, Replaced Parts as Necessary k
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DOCKET No.
50-271
.1 UNIT Ver:nont Yrnkee DATE 801209 COMPLETED BY F. J. Burger TELEPHONE 802-257-7711,X137 REPORT MONTH November
SUMMARY
OF OPERATING EXPERIENCES During the reporting period, the plant was shutdown for refueling and maintenance.
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