ML19345D417

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Monthly Operating Rept for Nov 1980
ML19345D417
Person / Time
Site: Cooper Entergy icon.png
Issue date: 12/03/1980
From: Ballinger P
NEBRASKA PUBLIC POWER DISTRICT
To:
Shared Package
ML19345D416 List:
References
NUDOCS 8012150081
Download: ML19345D417 (4)


Text

. _ . _ __ _. _ ._ . _ __ ._.__ _ ___ _. _ . _ _ _ _. . . _ _

O OPERATING DATA REPORT 1 DOCKET NO. 050-0298 DATE 12-3-80 COMPLETED BY P. L. Ballinger

TELEPHONE 402-825-3811 OPERATING STATUS Cooper Nuclear Station N0!:5

, 1. Unit Name:

2. P.eporting Period: November 1980
3. Licenwd Thermal Power (MWr): 2381
4. Nameplate Rating (Gross MWe): 836
5. Design Electrical Rating (Net MWe): N
6. Maximum Dependable Capacity (Gross MWe): 787
7. Maximurn Dependable Capacity (Net MWe): 764
8. If Channes Occur in Capacity Ratings (Items Number 3 Thmugh 7) Since Last Report Give Reasons:

None -a*

l

9. Power Level To Which Restricted,if Any (Net MWe): 645 MVe (Net)
10. Reasons For Restrictions,1f Any: Temporary Turbint- Modifications This Month Yr. to Date Cumulative
11. Hours In Reporting Period 720.0 R.040.0 56.2R1.0
12. Number Of Hours Reactor Was Critical 598.4 5.608.1 46.845.4
13. Reactor Reserve Shutdown Hours 0.0 0.0 _

0.0

14. Hours Generator on-Line 582.8 5,498.2 45,973.8 0.0 0.0 0.0 r
15. Unit Reserve Shutdown Hours
16. Gross Thermal Energy Generated (MWH) 1 241.664.0 11.879.1 %.0 89.061.862.0
17. Gross Electrical Energy Generated (MWH) 346.095.0., .
3. 4 5 6. 3,,_Q 27.995.203.0
18. Net Electrical Energy Generated (MWH) 333,481.0 3,321,940.0 26,980,217.0 l
19. Unit Senice Factor _

80.9 68.4 81.7

20. Unit Availability Factor 80.9 68.4 81.7
21. Unit Capacity Factor (Using MDC Net) 60.6
  • 54.1 62.7
22. Unit Capacity Factor (Using DER Net) 59.5 53.1 61.6
23. Unit Forced Outage Rate 7.6  ?.4 4.3  !
24. Shutdowns Scheduled Over Next 6 Months (Type.Date,and Duration of Eacht:

Refueling and V '*tenance Outage, May 3, 1980, 8 weeks l 25. If Shut Down At End Of Report Period. Estimated Date c (Startup:

26. Units in Test Status IPrior to Commercial Operationi: Forecast Achiesed INITIAL CRITICALITY l INITIAL ELECTRICITY COMMERCIAL OPERATION l

8012150 0 0

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 050-0298 Coope. Nuclear Statios 3.IT DATE 12-3-80 COMPLETED BY P. L. Ballinger TELEPRJNE 402-825-3811 MONTH Mova"har 1980 DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe-Net) iMWe-Net) 1 619 g7 0 610 g3 0 3 3 631 ;9 0 630 0 4 20 5 d16 23 252 6 612 22 432 7 615 3 535 614 530 3 24 610 495 9 25 to 630 26 625 3g 626 27 612 12 615 33 616 13 616 39 417 g4 615 564 30 15 199 31 16 0 INSTRUCTIONS On this format. list the average daily unit power levelin MWe Net for each day in the reporting month. Compute to de nearest whole megawatt. (4/77)

IX)CKEI NO. 050-0298 UNIT SilUIDOWNS AND POWER REDUCllONS UNII N AME Cooper Nuclerir Station DALE 12-1-80 COMPLE1ED BY P. L Ral l i nger REPOR T MON 111 November 1980 TELEPilONE 402-825-1811 l O c

                                                  .$ g      3  $ $5
                                                               .5 g 5 I ii.cnsee   ,E$,         .

h"3 CJNe & C"'ICLiive blion la No. Date i 58 4 Even 3,7 gU H Q-

s I y U= Report c mO u

o Paeven Recurrence 2 * =! 6 80-12 801115 F 48 G 3 50-298-80-44 IIE INSTRU During performance f a surveillance procedure checking )he APRM trip set-tings, operators tripped both Reactor g Protection Trip Channels causing a re-p g actor scram. An unrelated malfunctiori in the Turbine Control System caused M the main steam bypass valves to fail open allowing a rapid vessel depres-O surization and cooldown. A bad tur-bine control computer circuit board g

was replaced to correct the malfunctic t. S c) The plant remained stitdown for a S 89.2 B N/A N/A N/A N/A 7 scheduled maintenance outage. N 8G-13 801129 S 0 11 N/A N/A N/A N/A Reduced power to adjust the control ro l J pattern, 3 4 i 2 Method: IN!nbit G . Insimctions i: l'or ced Iteason: to: Picparation of Data S: Sche.luled A-Liguipment Failure (Esplain) 1 -Manual ll Maintenance of Test 2-Manual Scram. Ento Slicess for l_icensec 3 Automatic Scram. Esent Repois 11 I RIl'ile INURI G. C Refueling D-Regulatory Restriction 4-Other (Explain) 0161) I Operator Training & l.icense 1:xatnination 5 I -Administ rative INInbit 1 - Same Somte G-Oper ational I nos (Explain) 19/77) 11 Other (Explaini

4 OPERATIONS NARRATIVE November 1980 The plant operated at steady state power through the 14th. During surveillance test of the APRM trip settings, operators improperly i tripped both Reactor Protection System trip channels causing a reactor scram on the 15th. A malfunction in the Turbine Control System allowed the main steam bypass valves to open causing a rapid vessel depressur-ization and couldown of the vessel. A bad turbine control computer circuit board was replaced to correct the malfunction in the Turbine Control System. A maintenance outage scheduled for the 20th was taken at this time to repair steam leaks on the turbine and perform various maintenance activities. The reactor was started up on the 20th and the generator was synchron-ized to the grid at midnight. The reactor operated at steady state conditions until the 29th. Power was reduced to adjust the control rod pattern and the reactor was returned to normal power operation. 1 - ) i 4 i t l l 9 t t}}