ML19344B155

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Monthly Operating Rept for Jul 1980
ML19344B155
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 08/13/1980
From: Merson S
BALTIMORE GAS & ELECTRIC CO.
To:
Shared Package
ML19344B152 List:
References
NUDOCS 8008250657
Download: ML19344B155 (6)


Text

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O OPERATING DATA REPORT DOCKET NO. 50-317 DATE 8 /11/m C05tPLETED BY " 0 "a m n TELEPHOSE ?ri 73t_ uco e

OPERATING STATUS Calvert Cliffs No. I hotes

1. Unit Name:
2. Reporting Period:

h1v-1080

3. Licensed Thermal Power (5tht):

2.700 918

4. Nameplate Rating (Gross SlWe):

845

5. Design Electrical Rating INet SlWe):

m

6. 5!aximum Dependable Capacity IGross alwel:

810

7. Staximum Dependable Capacity tNet SlWe):
8. If Changes Occur ir ^apacity Ratings litems Number 3 Through 7) Since Last Report.Give Reasons:

~

9. Power Level To which Restricted. if Any INet StWe):
10. Reasons For Restrictions,if Any:

This Stonth Yr..to.Date Cumulative

11. Hours in Reporting Period

^

45,87e.0 744.0 5,111.0 744.0 4,547.0 36,936.6

12. Number Of Hours Reactor Was Critical 0.0 38.3 1,098.8
13. Reactor Resme Shutdown Hours 744.0 4,477.6 36,179.6
14. Hours Generator On.Line 0.0 0.0 0.0
15. Unit Resene Shutdown flours 1,918,570 10,547.749 85.A84.738 i
16. Gross Thermal Energy Generated 15tWH) 600,635 3.324.784 28.137.314
17. Gross Electrical Energy Generated IMWH) 573,183 3,156,959 26,806,165
18. Net Electrical Energy Generated (5thH) l 100.0 87.6 78.9
19. Unit Senice Factor 100.0 87.6 73.9
20. Unit Availability Factor 95.1 76.3 72.1
21. Unit Capacity Factor iUsing MDC Nerl 91.2 73.1 69.2
22. Unit Capacity FactorIUsing DER Net) 0.0 4.1 3.5
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Oser Next 6 Months IType. Date.and Duration of Eacht:

So.1 Plant scheduled for a planned outace startinn 10/17/80 until 12/15 /80 for refueling, unit general inspection and TMI Modifications.

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units in Test Status IPrior to Commercial Operation):

Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 8 008350 g

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-317 Calvert Cliffsd1 8/13/80 DATE COMPLETED BY S.D.!!erson 301-234-5240 TELEPHONE July, 1980 MONT11 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net)

(MWe Net) 810 816 g

g7 808 732 2

gg 813 3

674 39 809 01I 4

20 679 5

21 810 812 6

761 22 7

81 4 23 813 8

642 24 793 641 810 9

25 757 10 620 26 33 712 27 781 793 804 12 28 789 802 13 29 l4 806 30 782 812 792 15 3g 805 16 INSTRUCTIONS On this format. list the average daily unit power levelin MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.

(9/77) l

l l

50-317 UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.

UNIT NAME C'Ivere ciitis#1

  • DATE 8/13/80 COMPLETED BY % D.tferson REPORT MONTH lis 1 v.1 *m o TELEPHONE 101-?14-4?40 j

1 4 e. 3 5

e r.

.2 _e s

7sx Licensee E*

g%

Cause a Corrective No.

Date k

5@

2s5 Event sT

[q Actiusi to

$E j di g Report *

  • E 0 Prevent Recurrence d

i 80-1(.

800708 F

28 A

S XX Z7.ZZZZ Repair Condenser Tube Leak.

i Operated at various forced reductions.

,i 1

l I

i i

i e

1 a

i 1

1 2

3 4

F: Forced Reason:

Method:

Exhibit G - Instructions l

S: Scheduled A-Equipment Failure (Explain)

I-Manual for Preparation of Data 1

B-Maintenance of Test 2-Manual Scram.

Entry Sheets for Licensee C Refueling 3 Automatic Scram.

Event ReporI(LER) File (NUREG-j D Regulatory Restriction 4 Continuation 0161)

E-Operator Training & Ucense Examination 5-l.oad Rusction a

j F Administrative u-Od.er 5

G Operational E:ror (Explain)

Exhibit I-Same Source (9/77) 11 Other (Explain)

I; I

l

8/10/80 REFUELING INFORMATION RE0 VEST 1.

Name of Facility: Calvert Cliffs Nuclear Power Plant, Unit No.1 2.

Scheduled date for next Refueling Shutdown:

October 17, 1980 3.

Scheduled date for restart following refueling: Novernber 27, 1980 4.

Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?

Resumption of operation after refueling will require changes to Technical Specifications. The changes will be such as to allow operation of the plant with a fresh reload batch and reshuffled Core.

5.

Scheduled date(s) for submitting proposed licensing action and supporting information.

August 29, 1980 6.

Important licensing considerations associated with the refueling.

Reload fuel will be similar to that reload fuel inserted into the previous cycle.

7.

The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool.

(a) 217 (b) 364 Soent Fuel Pools are common to Units 1 & 2 8.

The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies.

~

1056 Licensed 728 Currently Installed 774 Licensed Addition is Planned 9.

The projected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity, October, 1983

~.

StFMARY OF U? LIT 1 OPERATIrlG EXPEPIEf!CE - JULY 1980 7/1 At the beoinnino of this reportina period Unit I was operating at 850 !Ye with the reactor at 100% nower.

7/3 At 0200 load was decreased to 610 PMe to clean condenser water boxes. Load was increased to capacity (850 MWe) at 1800.

7/5 At 0500 load was reduced to 690 MWe to investigate saltwater leakage into the main condenser.

7/6 After plugging one condenser tube resumed full load operation (850 fNe) at 1000.

7/8 At 0350 load was reduced to 660 MWe to investigate saltwater leakage into the main condenser.

7/9 Increased load to capacity (840 P!e) at 0800 after pluoqing one condenser tube. At 1600 load was reduced to 605 MWe to investiaate saltwater leakage into the main condenser.

7/11 After pluggina four condenser tubes resumed full load operation (345 !?!e) at 0030. At 1200 load was reduced to 605 fele to investigate saltwater leakace into the main condenser.

Increased load to capacity (840 M!e) at 2210 afte plugging one condenser tube.

l 7/12 At 2100 load was reduced to 725 ! ale to investigate saltwater leakage into the main condenser.

7/13 After pluoping one condenser tube resumed full load operation (840 !*4e) at 0750.

7/14 At 1130 load was decreased to 780 f4!e for troubleshooting an electrical problem with #11 Main Circulating Water Pump.

l Resumed full 'oad operation (850 FNe) at 1600.

1 1

SUMMARY

OF U!!IT 1 OPEPATI!!G EX? ERIE!!CE - JULY 1980 7/17 At 0005 load was decreased to 740 MWe to clean condenser water-boxes.

Increased load to 850 MWe at 0730. At 2250 load was reduced to 740 MUe to investigate saltwater leakage into the main condenser.

7/18 Increased load to capacity (830 MWe) at 2230 a'ter plugging one condenser tube.

7/24 At 0140 load was reduced to 740 MWe to investigate saltwater leakage into the main condenser. Load was increased to 850 MWe at 0610 when indications of saltwater leakage disappeared.

7/26 At 0300 load was reduced to 715 MWe to investigate saltwater leakage into the main condenser. After olugging one condenser tube resumed full load operation (840 MWe) at 1300.

7/27 At 0300 load was reduced to 715 MWe to investigate saltwater leakage into the main condenser. Load was increased to 845 MWe at 1600 when indications of saltwater leakage disappeared.

7/30 At 2040 load was reduced to 730 "We to investigate saltwater leakage into the main condenser.

7/31 Load was increased to 845 MWe at 0300 when indications of saltwater leakage disappeared. At the end of this reporting period Unit I was operating at 845 MWe with the reactor at 100% power.

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