05000271/LER-1980-034-03, /03L-0:on 801013,discovered Monthly Interval Was Exceeded by Four Days for Operability Test of Plant Fire Pumps.Caused by Misinterpretation of Test Interval by Personnel.Test Performed & Personnel Reinstructed

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/03L-0:on 801013,discovered Monthly Interval Was Exceeded by Four Days for Operability Test of Plant Fire Pumps.Caused by Misinterpretation of Test Interval by Personnel.Test Performed & Personnel Reinstructed
ML19343B000
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 11/12/1980
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19343A997 List:
References
LER-80-034-03L, LER-80-34-3L, NUDOCS 8011240412
Download: ML19343B000 (1)


LER-1980-034, /03L-0:on 801013,discovered Monthly Interval Was Exceeded by Four Days for Operability Test of Plant Fire Pumps.Caused by Misinterpretation of Test Interval by Personnel.Test Performed & Personnel Reinstructed
Event date:
Report date:
2711980034R03 - NRC Website

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